ML20009A094
| ML20009A094 | |
| Person / Time | |
|---|---|
| Site: | Pilgrim |
| Issue date: | 02/06/1981 |
| From: | Jerrica Johnson, Martin T NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20009A092 | List: |
| References | |
| 50-293-80-03, 50-293-80-3, NUDOCS 8107080080 | |
| Download: ML20009A094 (16) | |
See also: IR 05000293/1980030
Text
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U.S. NUCLEAR RicVLATORY COMMISSION
0FFICE OF INSPECTION AND ENFORCEMENT
50293-801106
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50293-801107
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Region I
50293-801113
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Report No. 50-293/80-30'
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Docket No. 50-293
Category
C
License No. DPR-35
Priority
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Licensee:
Boston Edison Company
800 Boylston Street
Boston, Massachusetts 02199
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Facility Name:
Pilgrim Nuclear Power Station
Inspection at:
Plymouth, Massachusetts
Inspection conducted:
0 tober 31, 1980 - November 26, 1980
Znscoctors:
4
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J. Johnson, Senior 5:itfe'ntInspector
date' signed
date signed
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date sigaed
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Approved by:
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T. DMartid, Chief, React <fr Projects
cate signed
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Section No. 3, RO&NS Branch
Inscection Summary:
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Inspection on October 31 - November 26, 1980 (Report No. 50-293/80-30)
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Areas Inspected:
Routine unannounced inspection of plant operations including
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an operational safety verification, followup on previous inspection findings,
followup on the 'A' Safety Relief Valve (SRV) inadvertent opening on October 31,
1980, maintenance activities, licensee's actions in response to IE Bulletins,
containment vent and purge operations, staff working hours and overtime, a
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review of seismic instrumentation, and a review of the design of containment
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cooling systems.
The inspection involved 84 hours9.722222e-4 days <br />0.0233 hours <br />1.388889e-4 weeks <br />3.1962e-5 months <br /> by the resident inspector.
Results: Two deviations were identified in two areas (failure to limit contain-
ment vent and purge operations to 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> per year, Paragraph 7; and failure to
limit a control room operator's working hours, Paragraph 8).
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8207080080 810212 h
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PDR ADOCK 050002934
G
PDR)
Region I Form 12
(Rev. April 77)
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DETAILS
1.
Persons Contacted
W. Armstrong, Deputy Nuclear Operations Manager
R. Belanger, QC Inspector
E. Cobb, Chief Operating Engineer
F. Famulari, QC Supy-"isor
J. Fiumara, Cr puter Engineer
E. Graham, Compliance Engineer
R. Machon, Nuclear Operations Manager (Pilgrim Station)
C. Mathis, Deputy Nuclear Operations Manager
P. O'Brien, Construction Management Group Leader
W. Olsen, Senior Nuclear Training Specialist
R. Reposa, QC Inspector
J. Seery, Staff Assistant - Nuclear Safety
P. Smith, Chief Technical Engineer
P. Williard, I&C Engineer
E. Ziemanski, Management Services Group Leader
The inspector also interviewed membus of the Operations, Security, Tech-
nical and Maintenance Staffs.
2.
Followup on Previous Inspection Findings
(0 pen) Unrasolved Item (293/80-29-03):
During a telephone corversation
between NRC:IE: Region I management and Boston Edison Company management on
November 17, 1980, the licensee agreed to take the following action with
respect to certsin TMI Task Action Plan Category ' A' Requirements:
Implement station approved procedure (s) for taking and handling a
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containment atmospheric sample by November 28, 1980.
Implement station approved procedures for converting high range noble
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gas effluent monitor readings (R/hr) to effluent release rates (Ci/sec)
by November 28, 1980, and
Correct the operation of control switches for containment vent and
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nitrogen makeup valves (A0 5033 A&C, A0 5041 A&B, A0 5043 A&B) to
allow operation between 'open' and 'close' positions without a key and
require a key to get in the ' emergency open' position, by January 1,
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1981.
These commitments were confirmed in a letter from the Director, NRC, Region
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I to Boston Edison Company fit-d November 18, 1980.
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This item remains open pending a review of the completed actions.
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3.
Operational Safety Verification
a.
Scope
The inspector observed control room operations, reviewed applicable
logs, conducted discussions with control room operators, and verified
proper lineup of selected portions of emergency systems.
Tours of the
station yard, reactor building, control room, and intake structures
were conducted to observe equipment condition including potential fire
hazards, housekeeping, physical security and the implementation of
radiation protection controls.
These reviews were conducted to verify conformance with the code of
Federal Regulations, Technical Specifications, and the licensee's
procedures.
b.
Events
(1) On October 31, 1980, the licensee notified the inspector of an
error in the original seismic analysis for the Salt Service Water
(SSW) System. This analysis took credit for a seismic anchor
located outside of the system isolation valves.
The anchors
were, in fact, the screenwash pumps, which are locatad outside
the missile protected area and would jeopardize the operability
of the SSW system if a tornado induced missile should impact the
screenwash pumps.
The inspector informed the licensee that relief from Technical Specification 3.5.b was required to permit continued operation.
The reactor wa: shutdown at 11:52 a.m. on October 31, 1980 (for
an unrelated problem with ' A' Safety Relief Valve) and the licensee
immeciately requested temporary relief from TS 3.5.b to allow
operation while modifications were made to the seismic anchors.
At 9:30 p.m. on October 31, 1980, NRC:NRR waived the requirements
of TS 3.5.b until November 7,1980, since the only cause of
system inoperability would be damage to the screenwash pumps due
to a tornado.
A reactor startup was comenced at 10:29 p.m. on October 31, 1980
and routine operations continued while modifications were performed.
The inspector toured the intake structure on November 7, 1980,
observed the installation of the new supports and verified com-
pletion of the modification through discussions with the cog-
nizant irplementing engineer (construction group leader).
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The inspector had no further questions in this area.
This event
is described in LER 80-78.
(2) Drywell Unidentified Leakage
A plant shutdown was initiated at 3:10 p.m. on November 6, 1980,
to investigate and repair reactor coolant system (RCS) unidentified
leakage calculated to be 5.9 gpm.
Investigation revealed packing
leakage on 'B' recirculation pump discharge valve, 'C'
Inboard
MSIV, and RCIC Valve No. 1301-16.
After startup on November 8, 1980, following repairs and pressuri-
zation, packing leakage was observed on both 'C'
and 'D' inboard
MSIV's.
While power and RCS pressure was being reduced, a reactor
scram occurred due to reactor vessel level low and difficulty
controlling level at low steam flows.
During a drywell inspection with the RCS at 900 psig on November
13, 1980 (following repairs to 'C'
and 'D' MSIV's), a pinhole
leak was observed at a coupling weld on the 2 inch line from the
reactor vessel drain to the clean up system.
The reactor was
again shutdown to repair the defective weld.
The reactor was started up and the unit returned to service on
November 14, 1980.
The inspector reviewed the licensee's actions to ensure compliance
with the Technical Specifications and station procedures.
Items
reviewed included control room instrumentation, logs and records
and r;iscussions with licensee personnel.
The inspector reviewed
sta: tup and shutdown check lists, verified placing the alant in
cold shutdown within the required time, satisfactory completion
of se'lected valve operability tests following repairs, and veri-
fied RCS leakage measurements on November 15-17, 1980 to be
within TS limits.
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Maintenance activities involving the weld repair are described in
Paragraph 5.
These events are described in LER's 80-84 and 80-87.
c.
Findings
No items of noncompliance were identified during this review of routine
operations and the events described above.
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4.
Inadvertent Opening of
'A'
Safety Relief Valve (SRV) at Power
a.
Description of the Event
At about 11:45 a.m. on October 31, 1980, the ' A' SRV inadvertently
opened at full power. Operators isolated the nitrogen supply to the
drywell instrumentation and placed the drywell instrumentation on
station compressed instrument air.
Reactor power was decreased to
approximately 50% and with the air supply pressure about 110 psig,
attempts were made to : hut the 'A' SRV by cycling the control switch.
The relief valve failed to shut and the reactor was manually tripped
frou. 50% power, and a cooldown was initiated to investigate and correct
the problems.
b.
Review / Investigation / Resolution of Concerns
The inspector reviewed the events, held discussions with the operators
and licensee management, observed instrumentation and reviewed records.
It was identified that high nitrogen supply pressure (about 160 psig)
was the cause of the opening of the
'A' SRV and that once the accumu-
lators are charged to this pressure, a time delay is experienced
before this pressure decreases and allows the SRV to reclose.
A similar event took place on October 7, 1980.
Following that event
the licensee had been monitoring the nitrogen supply pressure once per
shift to keep it below a value which would cause leakage by the solenoid
valve.
No specific failure of the pressure regulators had been identi-
fied.
It was also noted following this event on October 31, 1980 that a
delivery of liquid nitrogen had been made immediately prior to the ' A'
SRV opening.
It is suspected that a cause of the rapid rise in nitrogen pressure
may have been due to liquid nitrogen passing by the ambient vaporizor,
freezing an in-line regulator in the open position, and causing high
supply pressures (greater than 160 psig) to be transmitted to the
solenoid actuator.
During a telephone conversation between NRC:IE: Headquarters, Regional
management personnel and Boston Edison Company management personnel on
October 31, 1980, the licensee agreed to take the following actions.
The nitrogen supply system to the SRV's will remain isolated and
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tagged.
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The frequency of containment air sampling will be increastd to
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once per sitift for 7 days.
The implementation of these two items, above, would be verified
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by the resident inspector prior to the resumption of operation,
and
That the NRC will be provided documentation of an evaluation of
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system modifications and testing, for review and concurrence,
prior to restoration of the nitrogen system to in service.
These commitments were confirmed in a letter from the Director, NRC,
Region I, to Boston Edison Company dated October 31, 1980.
c.
Findings
At 5:10 p.m. on October 31, 1980, the inspector verified that the two
inch nitrogen supply valve to the drywell instrumentation (SRV's) was
isolated and tagged, and that the tag was logged in the Watch Engineer's
tag log book.
The inspector also verified an entry made in the Watch
Engineer's Instruction Log requiring a drywell and torus oxygen sample
once per shift.
Thase actions were taken prior to the re amption of
plant operation at 10:39 p.m. on October 31, 1980.
The inspector reviewed entries in N operations log and additional
data sheets from October 31,1980 '.c November 6,1980 to ensure that
oxygen samples were being taken on e per shift and concentrations were
within the Technical Specification limits with instrument air being
saoplied to the drywell instrumentation.
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No items of noncompliance were identified.
Pending the completion of
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the licensee's testing of the nitrogen supply system, system modifica-
t. ions, evaluation of these actions by the NRC, and restoration of the
nitrogen system to service (for drywell instrumentation), this item is
unresolved (293/80-30-01).
This event is described in LER 80-80.
5.
Maintenance Activities
a.
Scope and Acceptance Criteria
The inspector reviewed the licensee'< t-tivities surrounding the weld
repair of a two inch stainless steel i;ne from the reactor vessel
drain to the cleanup system performed on Novembr
, 1980 in order to
verify conformance with the ASME Code, the Tect ma l Specifications,
and the licensee's procedures.
The following records were reviewed:
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Maintenance Request No. 80-8023, and Maintenance Summary Sheets
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Welding and Testing Specification 6498-M-305, Revision 10
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Visual Inspection Record
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QAD Field Weld Check List
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Weld Rod Withdrawal Sheets
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Liquid Penetrant Test Results
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Welder Qualification Records
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-, NDE Qualification Records
b.
Findings
No items of noncompliance were identified however the inspector had
the following comments:
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The weld number designation and welder identification number were
inconsistent on several of the documents reviewed.
The licensee
agreed to review and correct the documents.
During th review of the post repair inspection sheets, the
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inspector informed the licensee that instructions, should include
reference to specific minimum required test pressures, and should
be provided to station personnel to ensure that the correct test
pressures are used.
The licensee acknowledged the inspector's
comments and stated that the appropriate actions would be taken
to include references to specific test presssures as required.
ihe inspector had no further questions in this area.
6.
Inspc. tion and Enforcement Lulletin Fo(lowup
The inspector reviewed the licensee's activities in response to the IE
Bulletins described below.
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a.
80-07:
BWR Jet Pumo Failure
The inspector reviewed implementation of station procedure TP 80-67
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Revision 1, " Jet Pump Operability surveillance IEB 80-07", dated
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October 22, 1980.
This procedure was revised (to include all the data
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required to be taken by the Bulletin) in response to the inspector's
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comments (Inspection Report 50-293/80-27).
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No items of noncompliance were identified.
The inspector had no
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further questions at this time and considers this Bulletin closed.
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b.
80-17:
Failure of Control Rods to Fully Insert During a Scram at
a BWR
Original Bulletin Pph 3.a; Procedure No. 2.1.6, "Reacter Scram"
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Revision 11 was revised to include a requirement to connect an
air hose to the one inch vacuum breakers on the east and west
headers and verify that air blows out the vent lines after each
scram was reset. The inspector spot checked the implementation of
this procedure and no problems were identified.
Original Bulletin Pph 3.b; Procedure No. 2.1., "Startup froe Cold
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Shutdown", OPER 01 Startup check list was revised to include a
check to verify that the S.D.V. was free of water prior to startup.
Original Sulletin Pph. 6.b; Procedure No. 2.2.86, " Residual Heat
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Removal", was revised to require all available containment cooling
if during 41grmal continuous operation the torus temperature
exceeded 60 F.
Supplement 1, Pph. A.2; Procedure No. 2.2.24; " Standby Liquid
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Control System", was revised deleting the requirement for station
supervision approval prior to initiation of the.SBLC system.
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Supplement 1. Pph. A.4; Procedure No. 1.3.10, " Key Control", was
revised to require the $8LC initiation key to be located on the
main control panel 905 above the switch.
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Supplement 3, Pph. 1.1.; Alarm Response Procedure No. 2.3.2.8,
was revised to require a scram if the scram air header pressure
reached 60 psig.
Emergency Procedure No. 5.3.8 " Loss of Intru-
ment Air", was also revised requiring a scram if the air pressure
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decreased to the point where it caused a feed regulating valve
lock up (as i ndicated on the main control panel 905 by red indi-
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cating lights on push buttons).
Based on information received
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from the licensee, the lock up occurs at a pressure of 64/65 psig
and clears at 74 psig.
The inspector had no further questions
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concerning this item.
Su;;plement 3, Pph.1.b.1; Procedure No. 2.4.3, " Rod Drift", was
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revised requiring immediate reactor scram if two rods in a nine
rod array start drifting in.
Supplement 3, Pph. 1.b.R; Procedure No. TP80-74, Revision 0,
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" Determination of Leaky Rod Drive Outlet Valves", was developed.
The licensee monitors the withdraw header temperature when a
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control rod high temperature alarm comes in (greater than 20gg)
and weekly thereafter.
This procedure requires a shutdown if 36
total rods indicate lgaking outlet valves (withdraw header temper-
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ature greater than 50 F above ambient).
The inspector spot
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checked implementation of this procedure and identified no problems.
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Supplement 3, Pph. 2; Procedure No. 2.1.6, " Reactor Scram", was
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revised requiring a verification of actuation of the six scram
dischrage instrument volume limit switches prior to bypassing the
S.D.V. high level scram, and a subsequent clearing of all six
limit switches following reset.
During a telephone conversation between NRC:IE, NRR and BECo
management personnel on November 24, 1980, the acceptability of
this method to detect damaged floats was discussed.
This licensee agreed to modify computer inputs to include recordings
for all six limit switches and to revise station procedures to
add specific acceptance criteria (time to reset) for limit switch
operability.
The licensee stated that these modifications and
procedure changes were expected to be in place by December 19,
1980 and that in the interim, surveillance procedure no. 8.M.1-20
(limit switch set point check) would be performed prior to startup
if a scram should occur.
The licensee's proposal was found to be acceptable and the inspector
had no further questions in this area at this time.
Confirmatory Order dated October 2, 1980:
The inspector questioned
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the licensee concerning whether the once per-shift UT checks of
the scram discharge volume (S.D.V.) had been performed for several
shifts between October 28, 1980 and November 6, 1980 for which no
entry had been made in the operations log.
The licensee provided
verification to the inspector that they had been performed. The
licensee also determined that all checks had not been performed
at greater than six hour intervals and immediately issued clari-
fying instructions in the Watch Engineer's Log.
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The inspector subsequently reviewea the operations log entries
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from November 6-14, 1980 to verify the implementation of these
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once per-shift UT checks of the S.D.V.
No discrepancies were
identified.
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80-14:
Degradation of BWR Scram Discharge Volume (SDV) Capability
The licensee issued a revised response (dated September 10, 1980)
because of orevious NRC concerns that the original response (dated
July 30, 1980) did not adequately address periodic testing and notifi-
cation.
The inspector reviewed the following station procedures:
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Revised procedure no. 2.2.17 " Communications Systems", Revision
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6, which requires an ENS report to the NRC for any inoperable
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S.D.V. vent / drain valve or if any S.D.V. vent / drain valve is
closed for more than one hour in any 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period.
Normal operating procedure no. 2.2.87, " Control Rod Drive System",
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Revision 8, which requires that the S.D.V. vent and drain valves
be normally open.
Revised su.reillance procedure 8.M.1.20, Revision 7, "High Water
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Level Scram Discharge Tank", which requires any inoperability to
be reported to the NRC within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
The licensee's September 10, 1980 response stated that a procedure for
periodic (once per cycle) operability testing would be prepared by
January 1,1981.
This Bulletin remains open pending a review of the implementation of a
surveillance procedure to perform periodic operability testing of the
S.D.V. vent and drain valves.
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No items of noncompliance were identified during the review of
these IE Bulletins.
7.
Containment Vent and Purge Operations
a.
Scope and Acceptance Criteria
The inspector reviewed the licensee's activities concerning containment
vent and purge operations with respect to the criteria established by
NRC:NRR and the commitments made by the licensee in the following
documents.
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NRC
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Letter from NRR to BECo. dated November 29, 1978, " Containment
Purging During Normal Operation".
Letter from NRR to BECo. dated October 22, 1979, " Containment
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Purging and Venting During Normal Operation".
Letter from NRR to BECo. dated September 9, 1980, " Confirmation
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of Commitment to Staff's October 23, 1979 INTERIM POSITION ON
CONTAINMENT Purging and Venting".
BECO
Letter from BECo to NRR dated January 9, 1979, No. 79-22.
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Letter from BECo to NRR dated August 21, 1979, No.79-158.
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Letter from BEco to NRR dated December-19, 1979, No.79-270.
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Letter from BECo to NRR dated May 27, 1980, No. 80-94.
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Letter from BECo to NRR dated May 27, 1980, No. 80-95.
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The inspector's review included the following items:
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Station procedures.
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Plant Design Change Request (PDCR) 3033, " Modify Containment Vent
and Purge Valves".
Completed maintenance requests.
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Completed valve operability surveillance tests.
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Discussions with station personnel.
b.
Findings
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(1) The licensee stated in the December 19, 1979 response to NRR that
permanent modification would be made to the isolation logic to
ensure at least one uninhibited isolation signal was provided to
the containment vent and purge isolation valves in the event
another signal was bypassed or blocked.
The inspector had verified on October 28, 1980 (during a review
of actions in response to the TMI Action Category ' A' Requirement)
through a review of preop. test procedures that changes to the
isolation logic had been performed.
The acceptance criteria in these tests included the following for
valves:
A0 5033A
A0 5033C
5035A
5035B
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5036A
5036B
5041A
5041B
5042A
5042B
5043A
5043B
5044A
5044B
All valves isolate on h? drywell pressure and/or lovt reactor
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vessel water level, if the control switch is in the 'open'
position.
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For valves A0 5033A, 33C (1" nitrogen makeup valve)
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A0 5041 A&B, A0 5043 A&B (2" drywell and torus
vent valves)
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Isolate on Lolo reactor vessel water level if the control
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switch is in the ' emergency open' position.
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(2) The licensee stated (in the May 27, 1980 letter BECo No. 80-95)
that the containment vent and purge valves are 20" butterfly
valves,thatanalysishasshownoperabflityintheeventofa
LOCA if their opening is limited to 45 , and that
difications
have been implemented limiting their opening to 45
During the review of PDCR 80-33, and the associated maintenance
requests, the inspector verified that six of the eight 20" con-
tainment vent and purge valves had been modified to limit their
opening by installing physical stops on the operator.
No records
of modifying the two outbcard 20" purge inlet valves (A0 5035B
and A0 5036B) were available.
Also, in the May 27, 1980 response from the licensee, a 4" nitrogen
purge isolation valve, A0 5033B was not addressed.
This information pertaining to the two outboard 20" purge inlet
valves and the 4" nitrogen makeup valve is under further review
by NRC and remains unresolved (50-293/80-30-04).
(3) The licensee stated that in order to maintain the drywell-torus
d/p required by Technical Specification that the two inch series
drywell and torus vent valves (A0 5041 A,B and A0 5043 A,B) would
not be limited in their use during normal operation.
The licensee further stated that purge and vent isolation valves
were used to inert the containment within the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period
allowed by Technical Specification after startup.
..u to ceinert
the containment in the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period prior to shutdown also
allowed by Technical Specifications.
The licensee did state, however, (in the August 21, 1979 and
December 19, 1979 responses to NRR; that operation of containment
purge isolation valves (other than those used for drywell-torus
d/p control) would be limited in their use to 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> per year
during power operation.
On November 20, 1980, the inspector requested the licensee to
show how the 90 hour0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> limitation was being implemented since the
station procedure controlling containment purge and vent operations,
No. 2.2.70, Revision 14, dated August 13, 1980, " Primary Con-
tainment Atmospheric System", did not include methods to imple-
ment this limitation.
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It was determined on November 21, 1980 that administrative controls
had not been implemented to limit the opening of purge and vent
valves (other than those used for drywell-tort
d/p control) to
90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> per year during power operation and also that there was
no mechanism for keeping track of the running total of length of
time opened.
'
The licensee determined from a review of the station operations
log that since plant startup after the January-May,1980 refuel-
ing outage that the 20" purge valves had been opened for approxi-
mately 145 hours0.00168 days <br />0.0403 hours <br />2.397487e-4 weeks <br />5.51725e-5 months <br /> during power operation (greater than about 1%
power).
The licensee stated that actions would be taken in the following
areas:
administrative controls would be implemented to not start
--
deinerting until suberitical and to minimize the time spent
inerting on stari.up during power operation.
i
implement a method for keeping track of total opening times
--
of the 20" purge valves.
initiate a request for modification to assirt in these con-
--
trols (possibly using meters to keep track of opening times,
and separate controls / interlocks on the 20" valve control
switches).
re-evaluate the 90 hour0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> / year limitation and determine what
--
actions should be taken, if any, if the limit is exceeded.
The inspector acknowledged the licensee's statement and stated
that the failure to limit the opening of the 20" containment
purge valves was considered a deviation from the licensee's
August 21, 1979 and December 19, 1979 commitments (50-293/80-30-
02).
8.
Interim Criteria for Shift Staffing
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The inspector reviewed the licensee's actions in response to a letter from
NRR to all operating plants dated July 31, 1980 which specified criteria
for shift staffing and li;nitations on working hours.
.
The inspector reviewed the licensee's October 15, 1980 response to this
issue which stated that the interim criteria for shift staffing would be
!
I
implemented no later than July 1, 1981 but that meeting all the limitations
,
on working hours and overtime would place an excessive burden on the oper-
l
ating organization.
The licensee did state, however, that a member of the
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'
.
-
14
required shift staff would be limited to 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> straight while performing
safety related control room duties.
On November 24, 1980, the licensee management identified that a control
room operator had been continuously on watch for an excessive length of
time (32 hours3.703704e-4 days <br />0.00889 hours <br />5.291005e-5 weeks <br />1.2176e-5 months <br />). On watch supervisors were unable to acquire a relief by
calling off watch operators at home.
. On November 26, 1980, the inspector attended an Onsite Review Committee
(ORC) meeting which included a review of this event.
The licensee stated
that subsequent to October 15, 1980, several operators were transferred
from the operations department to other positiens, and that further nego-
tiations with the local bargaining unit were needed because of the sensitivity
of replacing union watch standers with supervisory personnel.
The inspector questioned the licensee management concerning the actions
that would be taken to implement the commitment to limit working hours. The
licensee stated that instructions would be placed in the Watch Engineer's
(W.E.) Instruction Log to inform the W.E. that licensed operators would be
limited to 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> consecutive control room duty and that upper management
approval would be requi ed to exceed this limit. The licensee further
stated that station po cy limiting working hours would be included in a
.
station administrative document by January,1981.
The inspector acknowledged the licensee's statements and stated that the
failure to limit length of time that the control room operator was on watch
was considered a deviation from the licensee's October 15, 1980 commitment
(50-293/80-30-03).
9.
Seismic Monitoring Instrumentation
Although the Technical Specifications do not place any requirements on
seismic instrumentation, the inspector questioned the licensee on November
14, 1980, about concerns expressed by a vendor representative (Kinemetrics,
Inc.) involving the operation of recently installed seismic monitoring and
support equipment.
The concerns focused on the status of the antenna which
picks up a time signal from a remote national station and transmits this
time signal to a WWV receiver mounted in the seismic intrumentation panel
in the rear of the control room.
The inspector reviewed Plant Design Change Request No. 78-24-1, Seismic
Monitoring Equipment, and observed selected portions of the installed
instrumentation. This modification included the installation of three up-
graded SMA3 seismic accelerometers in the reactor building, tape recorder
units, a WWV radio receiver, and playback units in the rear control panel,
and an outside antenna for the WWV receiver.
Tbi WWV receiver provides a
time signal on an additional tape recorder unit to be able to automatically
record event time.
.
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The licensee stated that because several problems had been identified with
the operation of the WWV receiver and the antenna, that the receiver had
been previously shipped to the vendor for repairs and that a new antenna
had been authorized by BECo Engineering Department.
The licensee further
stated, that at the time of the vendor representative's site visit, that a
misunderstanding resulted concerning which antenna was to be used and that
the entire modification had not yet been verified and signed off as complete.
The inspector observed satisfactory operation of the WWV receiver on November
19, 1980 and had no further questions.
No items of noncompliance were identified.
10.
Susceptibility of Contaiment Flooding
The inspector was requested to review the design of Pilgrim's containment
with respect to susceptibility of flooding because of a problem at another
reactor site.
The inspector reviewed system drawings, observed indications available at
the main control room panel, and radwaste control room panel, and inter-
viewed licensee personnel. The following information includes details
about the system design:
There is a high level alarm for each of the drywell equipment and
--
floor drain sumps at the radwaste control panel.
D ywell equipment and floor drain containment isolation valves are
--
cuntrolled from, and position indication are displayed in the main
control room.
--
Sump pump running indication is provided at the radwaste control
panel.
A sump pump integrator for both of the sumps is located at the radwaste
--
control panel.
Drywell components are cooled by Reactor Building Closed Cooling Water
--
(RBCCW), a closed system, with instrumentation available to determine
inventory changes.
The main control room has a single annunciator which alarms if a local
--
alarm at the radwaste control panel is not reset /is not acknowledged.
This information was forwarded separately to NRC:IE for review.
No items of noncompliance were identified during this review.
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4
11. Unresolved Items
Areas for which more information is required to determine acceptability are
considered unresolved.
Unresolved items are discussed in Paragraphs 4.c
and 7.b.
12.
Exit Interview
At periodic intervals during the course of the inspection, meetings were
held with senior facility management to discuss the inspection scope and
findings.
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