LER-1981-016, /03L-0:on 810206,diesel Generator 2B-B Breaker Tripped Twice While Attempting to Synchronize W/Tva Power Grid for Surveillance Test SI-7.Caused by Overcurrent During Paralleling Operation.Target Reset & Parallel Repeated |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3271981016R03 - NRC Website |
|
text
...... --............
y,.
~
h (PLEAsE raint on Tvrt Att nEathiato ineonuationi conTaot si.ocx: Il l
l l
l l
ITTTl IT lN IS IN le li QI n i o l I n f o l o l o lo I lo lo l@l 4111 i l i l il@L l' I g i
8 9 LICENSEg CQQE l.
86 UCENSE NUM9 ER 29 26 UCENSE Tvrt 40 63 cas w i cou r
~~
lolil
,"l,$$ d lo 15 lo 10 I o l 31217 @l o f 2 l O l 6 l 811 @l 0131 ni s l a li l@
t 8
60 60 OOCatET NUUS EM GS 69 EVENT DATE 3.
76 ftEPOAT DAT E so
^
" ' EVEN* DESCRIPTION AND PAOB A8LE CONSECUENCES h D'TT1 I At 0915 (c) on 2/6/81. with toit 1 in mode 4 at 2100F and cooling to s de 5, diesel I.
lo ls] l generator (D/C) 2B-B' breaker tripped twice while attempting to synchronize with the l
I o 14 l l TVA power crid for ' Surveillance Test SI-7.
The diesel generator startdd and accelerated l [oisl l properiv; however.tfie diesel generator breaker tripped on overcurrent relay opera
l o 6 l This is reportable per Technical Specification 3.8.1.1 and 6.9.1.13.b.
There was no l
loTTl I danger to the health and safety of the public.
l 10181I l
so r..
es SYST E M CAUSE,
CAUSE
Cou*.
vatyt CODE CODE SUSCQUE Cou*CNENT CODE SUSCODE SUSCCOE l E l'E lh Wh l Z lh l.C l K I T l B lR lK lh l A lh 'lZ l @
l019l 9
iO 18 12 IJ 18 19 20 3
0 SE QUE NTI AL OCCUARENCE
- ftE POR T REVf33.N LE EVENTYEAR REponT No.
. cons TYPE No O",aj;mino I 811I l_I Io il l6 [
y l oi 31 g
g g,
- g
_2.
n u
2.
n n
n n
n 2.
u n'J," 'ACWe!
o'A'ST
$0'Wa" lo lo lo @lo I
^'J.'1"M'
,K"id..
'",'",h',ir-of "IfCTU.'E.
Nouas E
LsJ@l zi@
l zi@
lzl@
L.Ll@
lN l@
W@
l1 [2 l0 l2 l u
2 n
n 2,
o u
o CAUSE DESCRIPrf 0N AND CORRECTIVE ACTIONS I i i o 1 I Th6 'dle.,el ' cenerator breaker trinned immediately after closing dkiring manual syn *chroni-
)
L'_L.i_j l zation of the D/G to the TVA power grid. The D/G alienment was checked: however, on a
^
g l second attempt to parallel, the breaker tripped again on overcurrent. The target was Iii3l l reset and the diesel generator was successfully paralle' led with the grid. The over-11,.; l current relay. synchroscone,and voltmeters were checked and verified to operate correctly.
I s %
SO
's^r'MiE ovnEnsTATus @ $isEviN s PowEn oiscovEnv oEsCniPTioN M l,,Hlh l0l0IOl@l NA l
l A lhl operator Observation I
' 9 Co'0 RENT ActiveTv RELE ASED or nELEast AMoVNT OF ACTivlTY LOCATION CF AttEASE l i l 6 l [2] h l Z lhl NA I
l NA e 9 io is u
.s so pen 50NNEL EXPosumEs NVUS E R TYPE DESCRIPTICN li121lolofol@lzl@l l
NA
~
l 7
8 9 14 82 la to PERSONNE L INJUfttES Nuve E m DESCmiPTION lololol@l NA l
i 7
8 9 it 12 90 LOSS OF on OauaCE TO 8ACsLITY Q Tv'E CESCnie TION v
M LzJ@l l
NA l
l 7
8 9 to
" ' " ~
~*
Punt eCITV 1'
NRC USE ONL v 17 l a l WhlOESCmePflON 955Uto wi l
llltif11IIIll e 9 io es e9 Name of Preparer S.C.Maddox/J.M.McGriff Phone (615) 842-8317 _
l
@l 0810 056Y
Tennessee Valley Authority Sequoyah Nuclear Plant LER SUPPLEMENTAL INFORMATION SQRO-50-327/81016 Technical Specification Involved:
3.8.1.1 Reported Under Technical Specification:
6.9.1.13.6, 4.8.1.1.4 Date of Occurrence: 2/6/81 Time of Occurrence: 0915 CST Identification and Description of Occurrence:
During the conduct of Sarveillance Instruction SI-7 to verify operability of diesel generator (D/G) 2B-B, the D/G was started on a simulated loss of off-site power signal. The D/G started and accelerated properly; however, when the diesel was being synchronized with the TVA grid, the D/G breaker tripped twice. The breaker remained closed on the third attempt and the D/G was successfully loaded.
Conditions Prior to Occurrence:
Unit 1 in mode 4 at 210 F and cooling to mode 5.
Apparent Cause of Occurrence:
The D/G breaker apparently tripped on overcurrent during the paralleling operation which ties the D/G to the TVA grid for loading of the D/G for Surveillance Test SI-7.
Analysis of Occurrence:
During the performance of SI-7, the D/G started properly in response to a simulated loss of of fsite power signal. The D/G was being manually synchronized with the TVA grid when the D/G breaker was closed. The D/G breaker tripped immediately. The paralleling operation was attempted again and the breaker tripped again. On the third attempt the breaker remained closed and D/G 2B-B was successfully loaded.
Corrective Action
The immediate corrective action takenwas to verify that the D/G system align-ment was correct. The overcurrent relay, synchroscope and voltmeters were checked and verified to be correct. No further corrective actions are planned.
The overcurrent-relay and synchronizing circuits are cut out of the diesel generator control and logic for an emergency condition.
. Failure Data:
The following additional information is submitted in accordance with Technical Specification 4.8.1.1.4 and Regulatory Guide 1.108:
D/G Involved: 2B-B
a.
Failure Data: (Continued)
Failure No: N/A. The diesel generator breaker tripped on an overcurrent relay operation. This circuit and the synchronizing circuit are cut out during the emergency operation of the diesel generator. This was classified as an invalid test in accor-dance with Regulatory Guide 1.108, Position C.2.3.(2).
Cause of Failure: The D/G breaker tripped on an overcurrent relay operation.
The exact cause for the overcurrent condition is unknown.
The diesel generator system alignment was verified Corrective Measures:
The overcurrent relay, synchroscope,and volt-to be correct.
meters were verified to operate properly.
Length of Tine Inop:
34 minutes Surveillance Frequency: The present frequency is every seven (7) days.
This is in compliance with Regulatory Position C.2.d of Regulatory Guide 1.108 for three (3) failures in the last 100 valid tests.
t l
l l
l f
I-L
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000327/LER-1981-001-03, /03L-0:on 810102,condensate Storage Tank Level Channel 0-L-2-230 Declared Inoperable When Control Room Indicator Failed Low.Caused by Disconnected Instrument Sense Line Due to Improperly Tightened Compression Fitting | /03L-0:on 810102,condensate Storage Tank Level Channel 0-L-2-230 Declared Inoperable When Control Room Indicator Failed Low.Caused by Disconnected Instrument Sense Line Due to Improperly Tightened Compression Fitting | | | 05000327/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000327/LER-1981-002-03, /03L-0:on 810109,two Intermediate Deck Doors in Ice Condenser Found Frozen Closed.Caused by Water Leaking from AHU-3A Defrost Drain Line Flange Due to Loose Flange Bolts.Bolts Retightened | /03L-0:on 810109,two Intermediate Deck Doors in Ice Condenser Found Frozen Closed.Caused by Water Leaking from AHU-3A Defrost Drain Line Flange Due to Loose Flange Bolts.Bolts Retightened | | | 05000327/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000327/LER-1981-003-03, /03L-0:on 810105,main Feedwater Flow Channel F-3-35B Failed Low.On 810112 Feedwater Channel F-3-35B & F-3-90B Failed.Caused by Freezing of Inadequately Protected Instrument Sense Lines.Lines Thawed | /03L-0:on 810105,main Feedwater Flow Channel F-3-35B Failed Low.On 810112 Feedwater Channel F-3-35B & F-3-90B Failed.Caused by Freezing of Inadequately Protected Instrument Sense Lines.Lines Thawed | | | 05000327/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000327/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000327/LER-1981-004-03, /03L-0:on 810112,RWST Instrument Channel L-63-54 Failed.Caused by Sense Lines Freezing Due to Insufficient Insulation Around Lines & on Sides of Cabinet Housing Level Transmitter.Heaters in Use Until Insulation Can Be Added | /03L-0:on 810112,RWST Instrument Channel L-63-54 Failed.Caused by Sense Lines Freezing Due to Insufficient Insulation Around Lines & on Sides of Cabinet Housing Level Transmitter.Heaters in Use Until Insulation Can Be Added | | | 05000327/LER-1981-005-03, /03L-0:on 810114,capacitor C1A in A10 Power Supply & Control Card RB-8 Failed While in Svc.Caused by Failure of Vital Inverter 2-II.Components Replaced & Inverter Returned to Svc on 810114 | /03L-0:on 810114,capacitor C1A in A10 Power Supply & Control Card RB-8 Failed While in Svc.Caused by Failure of Vital Inverter 2-II.Components Replaced & Inverter Returned to Svc on 810114 | | | 05000327/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000327/LER-1981-006-03, /03L-0:on 810114,stroke Test Not Performed Following 800929 Repair of Leaking Valve 1-FCV-63-38.Caused by Inadequate Procedure.Procedure Being Revised | /03L-0:on 810114,stroke Test Not Performed Following 800929 Repair of Leaking Valve 1-FCV-63-38.Caused by Inadequate Procedure.Procedure Being Revised | | | 05000327/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000327/LER-1981-007-03, /03L-0:on 810116,level Channel for Steam Generator 3 (L-3-97) Declared Inoperable.Caused by Failure of Trip Bistable 1-LS-3-97F to de-energize.Module Replaced,Calibr & Returned to Svc | /03L-0:on 810116,level Channel for Steam Generator 3 (L-3-97) Declared Inoperable.Caused by Failure of Trip Bistable 1-LS-3-97F to de-energize.Module Replaced,Calibr & Returned to Svc | | | 05000327/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000327/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000327/LER-1981-008-03, /03L-0:on 810116,three Intermediate Deck Doors to Ice Condenser,Under Air Handling Units 6A,8A & 8B,found Frozen Closed.Caused by Frozen Water in Drain Lines Due to Fuse Failure in Heat Tape Controller.Ice Removed | /03L-0:on 810116,three Intermediate Deck Doors to Ice Condenser,Under Air Handling Units 6A,8A & 8B,found Frozen Closed.Caused by Frozen Water in Drain Lines Due to Fuse Failure in Heat Tape Controller.Ice Removed | | | 05000327/LER-1981-009-03, /03L-0:on 810127,containment Sump Level Loop L-63-177 Declared Inoperable.Caused by Calibr Drift Due to Problem W/Level Transmitter.Transmitter Replaced | /03L-0:on 810127,containment Sump Level Loop L-63-177 Declared Inoperable.Caused by Calibr Drift Due to Problem W/Level Transmitter.Transmitter Replaced | | | 05000327/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000327/LER-1981-010-03, /03L-0:on 810128,notification Received That During Ieb 79-14 review,180-1b (Light) Weight Discrepancy Discovered,Altering Support Design Requirements.Caused by Incorrect Weights Being Used in Computer Analysis | /03L-0:on 810128,notification Received That During Ieb 79-14 review,180-1b (Light) Weight Discrepancy Discovered,Altering Support Design Requirements.Caused by Incorrect Weights Being Used in Computer Analysis | | | 05000327/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000327/LER-1981-011-03, /03L-0:on 810130,vital Inverter & Vital Instrument Power Board 1-I Declared Inoperative.Caused by Severance of Conduit & Cable B30I Supplying Power to Inverter.Cable & Conduit Replaced | /03L-0:on 810130,vital Inverter & Vital Instrument Power Board 1-I Declared Inoperative.Caused by Severance of Conduit & Cable B30I Supplying Power to Inverter.Cable & Conduit Replaced | | | 05000327/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000327/LER-1981-012-03, /03L-0:on 810126,RCS Tave Decreased Below Limits. Caused by Operator Failure to Coordinate Turbine Loading Rate.Turbine Load Reduced & RCS Tave Increased | /03L-0:on 810126,RCS Tave Decreased Below Limits. Caused by Operator Failure to Coordinate Turbine Loading Rate.Turbine Load Reduced & RCS Tave Increased | | | 05000327/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000327/LER-1981-013-03, /03L-0:on 810203,liquid Radwaste Monitor, 0-RE-90-122,declared Inoperable.Caused by High Background Count Reading Due to Leak in Brooks Rotameter.Rotameter Seals Replaced,Sample Chamber Cleaned & Monitor Flushed Out | /03L-0:on 810203,liquid Radwaste Monitor, 0-RE-90-122,declared Inoperable.Caused by High Background Count Reading Due to Leak in Brooks Rotameter.Rotameter Seals Replaced,Sample Chamber Cleaned & Monitor Flushed Out | | | 05000327/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000327/LER-1981-014-03, /03L-0:on 810123,testing Procedure SI-158 for Containment Isolation Valves 1-FCV-62-72,73 & 74 Was Determined to Be Inadequate.Caused by Failure to Take Into Account back-pressure in Line.Procedure Changed | /03L-0:on 810123,testing Procedure SI-158 for Containment Isolation Valves 1-FCV-62-72,73 & 74 Was Determined to Be Inadequate.Caused by Failure to Take Into Account back-pressure in Line.Procedure Changed | | | 05000327/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000327/LER-1981-015-03, /03L-0:on 810216,during Surveillance Testing,Ice Condenser Basket Bays 1,18 & 24 Were Found Below Limits for Average Basket Weight.Caused by Sublimation.Ice Added Throughout Ice Condenser | /03L-0:on 810216,during Surveillance Testing,Ice Condenser Basket Bays 1,18 & 24 Were Found Below Limits for Average Basket Weight.Caused by Sublimation.Ice Added Throughout Ice Condenser | | | 05000327/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000327/LER-1981-016-03, /03L-0:on 810206,diesel Generator 2B-B Breaker Tripped Twice While Attempting to Synchronize W/Tva Power Grid for Surveillance Test SI-7.Caused by Overcurrent During Paralleling Operation.Target Reset & Parallel Repeated | /03L-0:on 810206,diesel Generator 2B-B Breaker Tripped Twice While Attempting to Synchronize W/Tva Power Grid for Surveillance Test SI-7.Caused by Overcurrent During Paralleling Operation.Target Reset & Parallel Repeated | | | 05000327/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000327/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000327/LER-1981-017-03, /03L-0:on 810212,welder Accidentally Blew Pin Hole in Pipe Sleeve,Releasing Low Level Activity Xe-133.Caused by Thin Wall Pipe & Restricted Access.Pin Hole Repaired | /03L-0:on 810212,welder Accidentally Blew Pin Hole in Pipe Sleeve,Releasing Low Level Activity Xe-133.Caused by Thin Wall Pipe & Restricted Access.Pin Hole Repaired | | | 05000327/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000327/LER-1981-018-03, /03L-0:on 810205,discovered That SI-137.2,RCS Water Inventory,Not Performed within 72-h Per Surveillance Requirements.Caused by Steady State Conditions Not Being Established Long Enough for Performance Before Reactor Trip | /03L-0:on 810205,discovered That SI-137.2,RCS Water Inventory,Not Performed within 72-h Per Surveillance Requirements.Caused by Steady State Conditions Not Being Established Long Enough for Performance Before Reactor Trip | | | 05000327/LER-1981-019-03, /03L-0:on 810211,inside Containment Isolation Valve 1-33-704 on Svc Air Header Discovered Omitted from Drawing.Valve Added | /03L-0:on 810211,inside Containment Isolation Valve 1-33-704 on Svc Air Header Discovered Omitted from Drawing.Valve Added | | | 05000327/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000327/LER-1981-020, Forwards LER 81-020/03X-1 | Forwards LER 81-020/03X-1 | | | 05000327/LER-1981-020-03, /03X-1:on 810207,w/unit in Mode 5 & Auxiliary Bldg Gas Treatment Sys Train B Fan Discharging Through Shield Bldg Exhaust Vent,Radiation Monitor for Exhaust Path 2-RM-90-100 Discovered Inoperable.Cause Not Stated | /03X-1:on 810207,w/unit in Mode 5 & Auxiliary Bldg Gas Treatment Sys Train B Fan Discharging Through Shield Bldg Exhaust Vent,Radiation Monitor for Exhaust Path 2-RM-90-100 Discovered Inoperable.Cause Not Stated | | | 05000327/LER-1981-021-03, /03L-0:on 810211,reactor Coolant Pumps 1 & 2 Were Stopped.Caused by RCS Pressure Going to Zero After RHR Containment Spray Isolation Valve Inadvertently Opened.Pumps Returned to Operable Status in Approx 1-h | /03L-0:on 810211,reactor Coolant Pumps 1 & 2 Were Stopped.Caused by RCS Pressure Going to Zero After RHR Containment Spray Isolation Valve Inadvertently Opened.Pumps Returned to Operable Status in Approx 1-h | | | 05000327/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | | | 05000327/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000327/LER-1981-022-03, /03L-0:on 810219,w/unit in Mode 5,chlorine Detector O-CLAN-43-205A Declared Inoperable.Caused by Electrolyte Used to Drip Onto Sensor Becoming Stopped Up in Felt Filter.Filter Replaced & Detector Returned to Svc | /03L-0:on 810219,w/unit in Mode 5,chlorine Detector O-CLAN-43-205A Declared Inoperable.Caused by Electrolyte Used to Drip Onto Sensor Becoming Stopped Up in Felt Filter.Filter Replaced & Detector Returned to Svc | | | 05000327/LER-1981-023-03, /03L-1:on 810303,four Undersized Pipe Sleeves Associated W/Seal Injection Water Lines to Reactor Coolant Pumps Identified.Caused by Incorrect Installation.Workplan 9073 Issued to Reshape Subj Piping Sleeves | /03L-1:on 810303,four Undersized Pipe Sleeves Associated W/Seal Injection Water Lines to Reactor Coolant Pumps Identified.Caused by Incorrect Installation.Workplan 9073 Issued to Reshape Subj Piping Sleeves | | | 05000327/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000327/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000327/LER-1981-024-03, /03L-0:on 810314,problems Were Experienced W/Steam Supply Controls to steam-driven Auxiliary Feedwater Pump 1A-S.Probably Caused by Initial Pressure Spike & Bias Error Due to Clog in Sense Lines Causing Steam Supply Isolatio | /03L-0:on 810314,problems Were Experienced W/Steam Supply Controls to steam-driven Auxiliary Feedwater Pump 1A-S.Probably Caused by Initial Pressure Spike & Bias Error Due to Clog in Sense Lines Causing Steam Supply Isolation | | | 05000327/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | | | 05000327/LER-1981-025-03, /03L-0:on 810217,during Surveillance Instruction SI-7,diesel Generator 1B-B Failed to Load Properly.Caused by Blown Fuse in Governor Potentiometer Circuit.Fuse Replaced | /03L-0:on 810217,during Surveillance Instruction SI-7,diesel Generator 1B-B Failed to Load Properly.Caused by Blown Fuse in Governor Potentiometer Circuit.Fuse Replaced | |
|