05000346/LER-1981-010-03, /03L-0:on 810202,MSIV Bypass Valve Ms 100 a Failed to Close.Probably Caused by Component Failure.Actuator Spring Adjusted to Increase Tension Until Valve Would Close

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/03L-0:on 810202,MSIV Bypass Valve Ms 100 a Failed to Close.Probably Caused by Component Failure.Actuator Spring Adjusted to Increase Tension Until Valve Would Close
ML20008E756
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 03/04/1981
From: Trautman D
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20008E751 List:
References
LER-81-010-03L, LER-81-10-3L, NUDOCS 8103090568
Download: ML20008E756 (2)


LER-1981-010, /03L-0:on 810202,MSIV Bypass Valve Ms 100 a Failed to Close.Probably Caused by Component Failure.Actuator Spring Adjusted to Increase Tension Until Valve Would Close
Event date:
Report date:
3461981010R03 - NRC Website

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8 60 61 DOCK ET NUVSER 6d 63 EVENT DATE 14 75 REPORT DATE 80 EVENT DESCRIPTIO J AND PROBA8LE CONSEQUENCES h foTil I (NP-33-81-09) On 2/2/81 at 0345 hours0.00399 days <br />0.0958 hours <br />5.704365e-4 weeks <br />1.312725e-4 months <br /> during the performance of the Main Steam Isola-i l o [ 3 ] I tion Valve Closure Test ST 5073.01, operations personnel noted that the Main Steam l

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J TOLEDO EDlSON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-81-09 DATE OF EVENT:

February 2, 1981 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:

Failure of MS 100 A to close during performance of Surveillance Test ST 5073.01, Main Steam Isolation Valve Closure Test Conditions Prior to Occurrence: The unit was in Mode 3 with Power (MWT) = 0 and Load (Gross MWE) = 0.

Description of Occurrence: On February 2, 1981 at 0345 hours0.00399 days <br />0.0958 hours <br />5.704365e-4 weeks <br />1.312725e-4 months <br /> during the performance of ST 5073.01, Main Steam Isolation Valve Closure Test, operetions personnel noted that MS 100 A, Main Steam Isolation Valve Bypass Valve, failed to close. This event placed the unit in the actic a statement of Technical Specification 3.6.3.1 which requires this valve, MS 100 A, to be operable in Modes 1, 2, 3, and 4.

The unit was in Mode 3 at the time of the occurrence. MS 100 A was closed to satisfy the action statement requirement.

Designation of Apparent Cause of Occurrence:

Initial belief was that limit switches were out of adjustment, however, further investigation proved this not to be the problem. Adjustment was made to the actuator spring to increase tension slightly which allowed the valve to achieve stroke distance as was previously specified in instrument records.

Inreation relating to this occurrence is still being evaluated.

This cause is being attributed to component failure.

Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. At the time of the occurrence there was no primary to secon-dary leakage and therefore would have posed no threat to the health and safety of the public or station personnel.

Corrective Action

Maintenance Work Order IC-234-81 was written and the above men-tioned adjustments were performed under this maintenance work order.

Failure Data:

Similar occurrences were reported in Licensee Event Report h7-33-80-104 (80-082) which included two events.

LER #81-010

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