ML20005E648

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Insp Repts 50-424/89-33 & 50-425/89-38 on 891028-1201. Violation Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Maint,Surveillance,Security,Technical Support,Quality Programs & Administrative Controls
ML20005E648
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 12/28/1989
From: Aiello R, Brockman K, Rogge J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20005E645 List:
References
50-424-89-33, 50-425-89-38, NUDOCS 9001100051
Download: ML20005E648 (15)


See also: IR 05000424/1989033

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- UNITED STATES

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. NUCLEAR REGULATORY COMMISSION .

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101 MARIETTA STREET,N.W.

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ATLANTA, GEORGI A 3o323 :

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' Report Nos.:

50-424/89-33 and 50-425/89-38

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JLicensee: ' Georgia. Power Company

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P. 0. Box 1295.-

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Birmingham, AL- 35201.

Docket Nos.:

50-424 and 50-425

License Nos.: NPF-68 and NPF-81

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Facility Name:

Vogtle' Units

and 2-

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. Inspect' ion _ Conducted: October 28 - December 1, 1989-

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/A # 8' <T-/

Inspectors:

M

J. Fdo je,- Senior ResidenVAnspector

Date Signed

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REAiello, Resident Inspe'ctor

Date Signed

Accompanied by:

.D

Starkey

. Approved By:

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K. E. Brockman, Chief

Datd Signed ~

Reactor Projects Section 3B

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Division of Reactor Projects

SUMMARY

-Scope:

-This routine inspection entailed resident inspection in the following

areas:

plant

operations,

radiological

controls,

maintenance,

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surveillance, security, technical support, and quality programs and

administrative controls affecting quality.

Results: One violation was identified in the area of ' administrative controls

affecting quality.

This violation involved a failure to ensure

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legibility of control room ~ drawings (paragraph 2.b(1)).

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The report notes responsiveness of the radiological controls

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department in lowering the alarm setpoints of the personal dosimetry

devices to afford better control (paragraph 2.b(4)).

000 00OCV 0500o424

051 891229

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DETAILS

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1.

Persons Contacted

Licensee Employees

  • J. Aufdenkampe, Plant-Engineering Supervisor

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  • G. Bockhold, Jr. , General Manager - Nuclear Plant

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C. Coursey, Maintenance Superintendent

  • G. Frederick, Safety Audit and Engineering Group Supervisor

H. Handfinger, Manager Maintenance

  • W. Kitchens, Assistant General Manager -' Plant Operations
  • R. Legrand, Manager - Chemistry:and Health Physics

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  • G. McCarley, . Independent Safety Engineering Group Supervisor

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  • A. Mosbaugh, Plant Support Manager

W. Mundy, Quality Assurance Audit Supervisor

  • R. 0 dom, Nuclear Safety and Compliance Manager
  • J. Swartzwelder, Manager - Operations

Other licensee employees contacted included technicians, supervisors,

engineers,~ operators, maintenance personnel, quality control inspectors,

and office personnel.

  • Attended Exit Interview

n alphabetical list of acronyms and initialisms is located in the last

paragraph of the inspection report.

2.

Operational Safety Verification - (71707)(93702)

The facility began this inspection period with both units at full power.

Unit 1:

The unit remained at full power with the exception of minor power

reductions for maintenance through the end of this inspection period.

Unit 2:

On November 5, 1989, an operator manually tripped the reactor due to

decreasing levels in all four SGs. The loss of level in the SGs was due

to the tripping of "B" MFP on loss of suction pressure. Later that same

day, the unit entered Mode 2 (Start Up). On November 6, the reactor went

critical, entered Mode 1 (Power Operation), and synchronized to the grid.

The unit remained at full power with the exception of minor power

reductions for maintenance through the end of this inspection period.

On November 26, 1989, during the performance of a surveillance on

containment radiation monitor 2RE-003, a CVI occurred.

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Control Room Activities

- Control. Room tours and observations were performed to verify that

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facility operations were being safely conducted .within ' regulatory

requirements.

These inspections consisted of one or. more of- the

following attributes, as appropriate at the time of the inspection:

' proper control room staffing;

- control room access and operator behavior;

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- adherence to approved procedures for activities in progress;

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- adherence to technical specification.LCOs;

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- observance ~of instruments and. recor6er traces of safety-related and

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important-to-safety systems for abnormalities;

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- review of annunciators alarmed and action in progress for

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' correction;

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- control board walkdowns;

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~- safety parameter display and the plant safety monitoring system

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operability status;

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- discussions and interviews with the On-Shift Operations Supervisor,

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~ Shift Supervisor, Reactor Operators, and the Shift Technical .

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Advis'or (when stationed) to determine the plant status, plans,

and to assess operator knowledge; and

- review of the operator logs, unit logs, and shift turnover sheets.

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.No violations or deviations were identified,

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Faci.lity Activities

Facility tours and observations were performed to assess the

effectiveness of the administrative controls established by direct

observation of plant activities, interviews and discussions with

licensee personnel, independent verification of safety systems status

and LCOs, licensee meetings, and facility records.

During these

inspections, the following objectives were achieved:

(1)

Safety System Status - Confirmation of system operability was

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obtained by verification that flowpath valve alignment, control

and power supply alignments, component conditions, and support

systems for the accessible portions of the ESF trains were

proper. The inaccessible portions are confirmed as availabil'ity

permits.

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On November 22, 1989, the control room drawings were inspected.

for legibility. . The . inspection- included a review of a major

portioniof Unit 1 and 2- control room drawings.

The following

. drawings and as-built-notices were determined to have legibility

problems' severe enough to restrict their use by. control room

-personnel:

ABN 87-V1E0325A002 T

1X4DB164-2

1X6AA02-234-7

ABN 87-01000A351 T

1X4DB167-1

2X3D-AA-A005

IX4DB162-1

1X4DB167-2

2X3D-AA-805A

1X4DB162-2

1X408167-4

2X3D-AA-F16A

1X4DB163-1

1X4DB171-4

2X3D-AA-F24A

1X4DB163-2

2X4DB179-2

2X3D-AA-G060

1X4DB163-5

IX6AA02-228-7

2X3D-AA-H018

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IX4DB163-6

1X6AA02-239-7

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IX4DB163-7-

IX6AA02-236-7

The inspector's initial- findings were elevated to the General

Manager and NRC Regional Management.

The General Manager

directed a review to commence immediately.

On November 27,

1989, the licensee discussed its findings with NRC regional

management.

These findings indicated that approximately 5 to-

7. percent of control room and ' clearance tagging drawings were

illegible.

The cause of illegibility is attributed to poor

reproduction and poor drafting.

With the exception of two

drawings for which aperture cards had'to be remade, all drawings

in these two areas were corrected.

The licensee also

established a long-term corrective action to review all

satellite document stations.

Administrative procedure 00101-C, " Drawing Control," Rev. 7,

Step 3.4.4, requires that drawing. legibility be ensured prior to

-distribution, and engineering procedure 50009-C, "As-Built

Notices," Rev

7, Step 4.6.3, requires ABNs to be legible and

reproducible.

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Failure to ensure the legibility of control room drawings

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constitutes a violation of administrative procedure 00101-C and

engineering procedure 50009-C.

This

violation

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identified

as

50-424/89-33-01

and

50-425/89-38-01, " Failure To Implement Procedures 00101-C And

50009-C Concerning Legibility Of Control Room Drawings."

(2) Plant Housekeeping Conditions

Storage of material and

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components and cleanliness conditions of

various

areas

thr oughout the facility were observed to determine whether

safety and/or fire hazards existed.

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~ (3) Fire Protection'

Fire protection activities, staffing, and

equipment were observed to verify that fire brigade staffing was

appropriate and that fire alarms,_ extinguishing equipment,

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actuating. controls,' fire

fighting

equipment,

emergency

equipment, and fire barriers were operable.

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. (4) . Radiation' Protection

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Radiation ~ protection

activities,

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staffing, and equipment were observed to -verify proper program.

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. implementation. The inspection included a~ review of the plant's;

program effectiveness.

Radiation. work permits and personnel

compliance ~ were reviewed during the daily plant tours.

Radiation Control Areas were observed to verify proper

identification and implementation.

On November 8,

1989, the manager of. radiological protection

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informed the

inspector of new _ personnel ~ dosimetry alarm

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setpoints which would- be utilized in controlling dose. When a'

worker receives a dosimetry alarm, he is to leave the.

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radiological area and report to health physics,

In the past,

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the alarm was set at 200 ' mrem. - During a recent maintenance

actfvity,' a worker received' 135 mrem dose when a 40 mrem dose

had been expected. The radiation work permit allowed ~for a 200'

mrem dose. The inspector noted to the licensee that a' fixed.

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alarm at 200 mrem did not function to - limit dosage.

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example, a visitor would be expected to get no- more than 1 mrem.

In response to the issue, the licensee pursued a change to the

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computer sof tware and implemented the following:

RWP No.

Dose Alarm

20, 21, 23, 24, 26, 27

25 mrem

65 (Visitor)

10 mrem

Others

1/20 of remaining quarter

(50 mrem)

The inspector considers the responsiveness of the radiological

department to be noteworthy.

(5) Security - Security controls were observed to veri fy that

security barriers were intact, guard forces were on duty, and

access to the Protected Area was controlled in accordance with

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the facility security plan.

Personnel were observed to verify

proper display of badges and that personnel requiring escort

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were properly escorted.

Personnel within Vital Areas were

observed to ensure proper authorization for the area. Equipment

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operability or proper compensatory activities were verified on a

periodic basis.

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(6) Surveillance _(61726)(61700) -- Surveillance tests'were observed

to verify that approved procedures were being used, qualified

personne1' were conducting the tests, tests were adequate to

verify equipment operability, calibrated uquipment was utilized,

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and TS requirements were followed.

The inspectors observed

portions of the. following surveillance > and/or reviewed

completed data against acceptance criteria:

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Surveillance No.

Title

14806-1, Rev. 5

Containment _ Spray .0 ump anc

Check Valves Inservice

Test

14807-2(1), Rev. 2(6)

MDAFW Pump. Inservice Test

14804-2, Rev. 2

Safety Injection Dump

Inservice Test-

14825-1, Rev. 11

Quarterly Safety Injection

System Valve Inservice Test

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14420-1, Rev. 8

SSPS Train A(B) Operability

Test

14980-2, Rev. 2

Diesel Generator Operability

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Test

PORV surveillance testing.was examined in support of'a regional

inspection conducted during this reporting period.

A potential

violation of TS was identified in that a portion of the

electrical circuitry for the automatic function of the PORV was-

not tested as required by TS 4.4.4.

The circuitry for manual

operations had been properly tested.

The inspector interpreted

the surveillance requirement to include the " automatic"

function.

However, the' licensee's interpretation was that the

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manual mode swas adequate for operability because of the

following reasons:

1.

action statement "a" of this LCO (if there was excessive

seat leakage) would allow indefinite plant operation with

both block valves closed

(i.e., without the PORV automatic

. function);

2.

the language of the Vogtle FSAR, Chapter 15, does not

require (nor use) the PORV automatic actuation; and

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under severe accident conditions, the PORVs will be used in

the manual mode.

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The licensee agreed that the surveillance of- the automatic

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circuitry was - inadequate. ,They did. not, however, intend to

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immediately rectify this rhortcoming.

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The reasons the licensee wanted to delay this test were to avoid-

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an additional PORV block valve stroking and because the part of

the circuit which had not been tested was a circuit of very high

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reliability.

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The inspector's review of the accident analysis noted that the

licensee took credit for the automatic function of the PORVs for

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the following reasons:

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TS 3/4.4.4 bases states that the PORVs and steam bubble-

function to relieve RCS pressure during all design

transients, up to and including the design step load

decrease with steam dump.

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Two cases, for both the minimum and maximum reactivity

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feedback, are analyzed in the FSAR, Chapter 15, paragraph

  • 15. 2. 3. 2.1.

One case takes full credit for the effect of

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pressurizer spray and power-operated relief valves in

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limiting the coolant pressure with safety

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valves av+t able,

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3.

-The FSAR, Chapter 15, Table 15.2.3-1, indicates that with

and without offsite power available for a feedwater system

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pipe break, pressurizer PORVs are expected to actuate ire

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19.5 seconds.

4.

One of the major assumptions in the FSAR, Chapter 15,

paragraph 15.2.8.2.1, used for a double ended rupture of

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the largest feedwater pipe at full power is that credit is

taken for the pressurizer PORVs and the safety relief

valves.

No credit is taken for pressurtzei spray.

5.

FSAR-Q,

Question

420.19,

states,

"Using

detailed

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describe

the

design

of

pressurizer

power-operated relief valve control and the block valve

control, and verify that no single failure will preclude

the automatic actuation logic for all modes of operation."

On November 17, 1989, at 10:00 a.m. , a conference call took

place between the licensee and NRC management regarding this

issue. The purpose was to review the NRC staff position, which

concluded that the automatic function was required and should be

immediately tested.

In response to this, the licensee tested

both remaining PORVs on November 17, 1989.

Details cf this

issue are available in NRC Inspection Report Nos. 50-424/89-31

and 50-425/89-36.

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('7) Maintenance Activities (62703)

The inspector observed

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maintenance -activities to verify that correct equipment

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clearances were in effect; work requests and fire prevention

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work permits, as required, were issued and being followed;

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quality control

personnel 'were available for inspection

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activities 'as required; retesting and return of systems to

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service was prompt and correct; and TS requirements were being

followed.

The Maintenance Work Order backlog was reviewed.

Maintenance was observed and/or work packages were reviewed for

the.following maintenance activities:

MWO No.

Work Description

28905765

Repair Packing Leak On Main Steam Valve

2LV-6191

28905799

Clean And Repair EHC Fuller's Earth

Filter Due To Leaking Filter Canister

Caps.

18905983/

Increase The " Low Hydraulic Pressure"

28906212

Pressure Switch Set Point To The SG ARV

Actuators Due To Insufficient Stored

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Energy To Operate The Valves During

Worst Case Conditions.

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18903554

Repair Auxiliary Steam Leak On

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Auxiliary Steam Supply Valve To The

TDAFW Pump (1-1301-U4-264)

One violation was identified in paragraph 2.b(1) above.

3.

Review of Licensee Reports (90712)(90713)(92700)

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In-Office Review of Periodic and Special Reports

This inspection consisted of reviewing the below listed reports to

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determine whether the information reported by the licensee was

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technically adequate and consistent with the inspector knowledge of

the material contained within the report.

Selected material within

the report was questioned randomly to verify accuracy and to provide

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a reasonable assurance that other NRC personnel have an appropriate

document for their activities.

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Monthly Operating Report - The report dated November 10, 1989, was

reviewed.

The inspector had no comments.

(Closed)

Special Report dated October 16, 1989, " Loose Part

Detection System."

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On October 16, 1989, plant personnel discovered that- the channel

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calibration for the Loose Part Detection System was not performed as

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specified in the FSAR, Section 16.3, Requirement 3.

A Maintenance

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Work Order generated under the Preventive Maintenance Program was

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initiated on July 27, 1988, to perform the 18-month channel

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calibration during the first refueling outage for Unit 1.

The MWO

was erroneously voided due to the belief it was not required to be

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included in- the scope of the refueling outage. The FSAR commitment

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to demonstrate the operability of the Loose Part Detection System was

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not properly identified in- the PM program which resulted in the MWO

not being worked during the outage.

For corrective. action, the

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channel calibration for the Loose Part Detection System has been

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entered into the Technical Specification Surveillance Tracking

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Program. .Since this surveillance can only be performed in Mode 5,

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the operability of the Loose Part Detection System will be

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. demonstrated during the next refueling outage for Unit 1 (IR2).

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Additionally, it should be noted a channel operational test has been

performed at least once per 31 days in accordance with FSAR Section

16.3.

The inspector has no further questions.

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b.

Deficiency Cards and Licensee Event Reports

Deficiency Cards and Licensee Event P.eports were reviewed for

potential generic impact, to detect trends, and to determine whether

corrective. actions appeared appropriate. Events which were reported

pursuant to 10 CFR 50.72, were reviewed following occurrence to

determine if the technical specifications and other regulatory

requirements were satisfied.

Each LER was reviewed for enforcement

action in accordance with 10 CFR Part 2, Appendix C, and where the

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violation was not cited,-the criteria specified in Section V.G of the

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Enforcement Policy were satisfied.

Review of DCs was performed to

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maintain a realtime status of deficiencies, determine regulatory

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compliance, follow the licensee corrective actions, and assist as a

basis for closure of the LER when reviewed. Due to the numerous DCs

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processed, only those DCs which result in enforcement action or

further inspector followup with the licensee at the end of the

inspection are listed below.

The DCs and LERs denoted with an

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asterisk indicate that reactive inspection occurred following- the

event and prior to receipt of the written report.

(1) The following Deficiency Cards were reviewed:

(a) DC 1-89-1544, "TS Violation Regarding Excessive Tendon

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Grease Void".

During performance of the third year tendon surveillance a

tendon was found with a grease void exceeding 5 percent.

This is a violation of TS 3. 6.1.6.b and 4. 6.1. 6.1.d . 2.

This item will be further followed up when submitted as a

special report.

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(b) DC 1-89-1562, " Degradation Of Containment Structural

Integrity."

During performance _. of _ third year tendon surveillance,

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grease was emitted into level C of- the' auxiliary building

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.while regreasing horizontal tendon #6. This-resulted in:a

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violation of_ TS section - 4.6.1.6.1.d.4.

This item will be-

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further followed up when submitted as a special report.

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(c) DC 1-89-1579, "Rosemont Transmitters Supplied To VEGP_Were

Of Manufacturing Groups That'Are Susceptible To Failure Due

To Oil Loss."

It was identified that a group' of Rosemont Transmitters

supplied to VEGP contain a defect which, given a ' failure

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due to oil . loss, would possibly lead to a ' substantial

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safety hazard. This, item is under review for applicability

and reportability as a Part 21 report.

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(d) *DC 2-89-1490, " Manual Reactor Trip Due To SG Levels

Approaching The Lo-Lo Level Setpoint."

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On November 5, 1989, an operator manually tripped the

reactor due to the steam generators approaching the Lolo

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level setpoint. Operators were placing a heater drain tank

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1evel control valve in service when the valve opened,

causing a low suction pressure to the steam generator. feed

pumps'. The standby' condensate pump failed to start and the

feed pump tripped on low suction pressure.

This resulted

.in a partial loss of feedwater to the steam generators.

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All control rods fully inserted, main feedwater isolated

and AFW actuated on the trip. All systems functioned as

required.

This item will be further followed up when

submitted as a LER.

(e) *DC 2-89-1508, " Containment Ventilation Isolation Due To

Containment Radiation Monitor 2-RE-003."

During the performance of a Surveillance on Containment

Radiation Monitor 2RE-003,

a Containment Ventilation

Isolation occurred.

Operators verified proper Isolation.

Radiation levels were checked to be at normal values.

Computer printouts indicated that the monitor returned to

" Normal" during the surveillance.

All radiation levels

were checked to be normal and the system was returned to

normal operating status.

This event will be further

followed up when submitted as a LER.

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(2) The following LERs were reviewed'and closed.

(a) 50-424/88-37, Rev.

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"0-Ring Found Missing In Post

Accident Monitoring RTD's Junction Boxes."

On November 16, 1988, while performing Maintenance Work Order 18808056, 0-rings were discovered missing from four-

CONAX T-8= Head junction boxes. Three of. the boxes service

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resistance temperature detectors that provide reactor

coolant.T-hot wide range temperature indication for post

accident monitoring.-

The detectors were in an untested

configuration.

Technical Specification 3.3.3.6, " Accident

Monitoring Instrumentation," requires that these detectors

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be operable during plant operation.

On November 4, 1988,

while reviewing environmental qualification documentation,

it was noted that installation of 0-rings was required in

the tested configuration to seal the CONAX T-8 Head

junction boxes.

A check of material inventory revealed

that no 0-rings had been ordered as replacement spares. An

MWO was written to inspect the subject boxes. During the

  • inspection, four 0-rings were discovered missing.

This

event occurred because the 0-rings were not installed

during initial

installation.

All the CONAX T-8 Head

junction boxes were inspected under MWO 18808056.

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missing 0-rings were replaced and the boxes sealed.

Environmental qualification documentation has been updated

to clarify the requirements for 0-rings and maintenance

procedures have been revised to address their replacement.

Inclusive in this review was a Westinghouse review of the

issue. The inspector's questions regarding the corrective

actions' completeness were resolved.

Enforcement action

was discussed in NRC Inspection Report No. 50-424/89-25.

(b) 50-424/88-47,

Rev.

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" Error In Procedure Leads To

Technical Specification 3.0.3. Entry."

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On June 14, 1988, while the unit was at 100 percent power,

handswitches for manual actuation of Containment Isolation

Phase A and Containment Ventilation Isolation were

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tested. Each handswitch was taken out of service, tested,

and returned to service.

On October 13, 1989, while

preparing to perform the test, a system engineer identified

an error in the procedure which resulted in simultaneously

disabling both handswitches. This condition is in conflict

with the requirements of Technical Specification Table

3.3-2 which requires both handswitches to be operable in

Modes 1, 2, 3, and 4.

Although, durin0 the previous test,

LCO entries had been made for each handswitch being out of

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service, it was not recognized that both handswitches were

out of service at the same time.

This condition resulted

in entry into TS 3.0.3.

Automatic actuation capability was

not affected by the testing and was available, if required.

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Procedures 54708-1 and 54708-2 have been revised to ensure

that the manual actuation handswitches will

not be

simultaneously disabled.

(c) *50-425/89-20, Rev. O, " Loss Of Power To NI Channel Causes

Reactor Trip During Surveillance Test."

On May

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1989, while personnel were performing

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surveillance of nuclear instrument channel N44, a two out

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of' four Hi Flux rate trip coincidence signal was received,

causing an automatic reactor trip. Power range channel N43

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experienced a momentary' loss of power, which tripped the

Rate- Trip bistable on N43.

The control room operator

acknowledged the alarm for the tripped bistable, but failed

to notice that the wrong bistable had tripped for the work

being performed.

A step of the surveillance procedure,

which was being performed for N44, requires the fuses to be

pulled.

This action tripped the Rate Trip bistable for

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N44. . The N43 and N44 tripped bistables satisfied the two

out of four logic for a power range reactor trip.

All

automatic systems functioned as designed.

The causes of

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this event were the loss of power to channel N43 and the

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failure of control room operators to notice that the wrong

bistable had tripped. Extensive troubleshooting of N43 was

performed.

The cause for the power loss could not be

determined.

The

operations

requalification

training

program includes increased emphasis on recognizing the

cause of the alarm being acknowledged. Nuclear instrument

calibration procedures were revised to require reactor

operator signoff (in addition to instrument technician

signoff presently required) prior to manually tripping

bistables or removing instrument power. The inspector has

no further questions.

(d) *50-425/89-27, Rev. O, " Reactor Trip On High Flux Rate Due

To Rod Drop."

On October 12, 1989, an automatic reactor trip occurred

with the reactor in stable operation at 58 percent of rated

thermal power. Following a review of computer printouts of

data associated with the trip, the first out annunciator

was identified as a high flux rate trip annunciator.

Operability testing of the control rods then indicated that

a problem existed with rod K-2 in control bank

B.

Investigation of the control rod circuitry identified a

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failedi diode which had. apparently resulted in a loss of

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current to the stationary gripper ~ coil.

This allowed the

rod to drop into the core and initiate a negative flux rate

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. trip, . Corrective action. included replacing the diode for

rod-K-2.

The inspector reviewed the post trip data and

monitored.the repair and restart' activities. The inspector

~has no further questions.

'

V

.~ 50-425/89-28,

Rev.-

0,

" Arcing Power Cable Leads to

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,

"

Containment Ventilation Isolation."

g

On 0ctober 16,.1989, . a technician was preparing to eplace

'

a faulty circuit board in -a containment vent effluent

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radiation monitor panel.

While performing this work, he

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contacted a power cable and arcing occurred at the thermal

"

connection.

The arcing resulted in power fluctuations at

'

the Input / Output circuit board which subsequently failed.

'

This led to a Containment Ventilation Isolation actuation.

LThe. cause of this event was an inadequate design.

The

screw on the radiation monitor terminal block was too short

  • to adequately engage the threaded opening and provide a=

~

tight, permanent connection with the attached power cable.

When the technician's hand contacted the cable, the

connection was loosened and arcing occurred.

This screw,

and a similar screw in Unit I have been replaced.

The

inspector has no further questions.

No' violations or deviations were identified..

4-

Actions on Previous Inspection Findings - (92701)(92702)

,

,

a.

(Closed) IFI 50-424/88-21-02 and 50-425/88-31-02, " Update Posted TSC

F

Facility Layout With Existing -Operations Area Confirmation And

' Designated Work Stations."

'

-The inspector verified that the postings had been updated. The setup

of the Technical Support Center was verified during the July exercise

-

to be in accordance with the new posting. Th s verification was made

as

a' followup to that documented in NRC Inspection Report

Nos. 50-424/89-01 and 50-425/89-01.

b.

(Closed) VIO 50-424/89-14-01 and 50-425/89-15-01, "Six Examples Of

,

Failure To Establish Or Implement procedures."

h

The inspector reviewed the licensee's response dated July 12, 1989,

and correction letter dated September 18, 1989, against the clesure

documentation assembled by the licensee.

The inspector determined

that the actions are adequately complete.

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c.

(Closed)

VIO 50-424/89-19-01, '" Failure To Implement ' Operations

Procedure.10001-C As Required By TS 6.7.1.a To Verify Proper

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Operation Of Control Room Chart Recorders."

L.

The licensee committed to full compliance on August 31, 1989,.in the

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licensee's response dated-August 30, 1989. All corrective actions

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were found to be satisfactory.

This verification was ' made - as a

[

followup

to . that ' documented

in

NRC . Inspection

Report

[

.Nos. 50-424/89-01 and 50-425/89-01,

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5.

Management Meetings -'(30702)

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b

This activity involves inspector participation.and preparation in support

of the following meetings which presented site readiness.

r

On October 26, 1989, the inspectors attended a licensing issues status

meeting cor. ducted on site.

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6.

Exit Interviews - (30703)

The inspection scope and findings were summarized on December 1,1989,

L

with _ those persons indicated in paragraph 1 above.

The inspectors

b

described the areas inspected and discussed in detail the_ inspection

L

results.

No dissenting comments were received from the licensee.

The

licensee did not ~ identify as proprietary any of the materials provided to

or reviewed by ' the inspector during this inspection. . Region based NRC

exit interviews were attended during the inspection period by a resident

. inspector.

This inspection closed two violations '(paragraphs 4.b and

4.c), one inspector followup item (paragraph 4.a), and five Licensee Event

Reports- (paragraph 3.b(2)).

One new item was identified during this

inspection:

j

Violation 50-424/89-33-01 and 50-425/89-38-01, " Failure Tc Itnplement

Procedures 00101-C - And 50009-C Concerning Legibility On Co;. trol Room

Drawings" - Paragraph 2.b(1).

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7..

. Acronyms And Initialisms

ABN

As Built Notice

AFW

Auxiliary Feedwater System

ARV

Atmospheric Relief Valve

CFR

Code of Federal Regulations

CONAX

(trade name)

CVI

Containment Ventilation Isolation

DC

Deficiency Cards

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EHC

Electrohydraulic Control

ESF

Engineered Safety Features

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FSARI

. Final Safety Analysis Report

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s.

. IFI"

Inspector Followup Item

F

LCO'

Limiting-Conditions for Operations

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E

LER-

Licensee Event Reports

,

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_MDAFW:

Motor Driven AFW Pump

.

'MFP-

. Main Feed Pump.

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. mrem'

Millirem,

MWO

_ Maintenance Work Order-

.NI

Nuclear Instrument

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,NPF

' Nuclear Power Facility

i

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NRC-

Nuclear Regulatory Commission

'

in

PM

= Planned Maintenance.

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PORV.

Power Operated Relief Valve

/

RCS

Reactor Coolant System

e

Rev:

Revision.'

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.

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'RTD

Resistance-Temperature Detector

1

1

E*

RWP

Radiological Work Permit.

h

SG

Steam Generator

SSPS

. Solid State Protection System

.

O

TDAFW'

Turbine Driven AFW Pump.

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TS.

Technical Specification

-

L

.

.TSC

. Technical Support Center

VEGP

Vogtle Electric Generating 1 Plant

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VIO-

Violation

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