05000327/LER-1981-063-03, /03L-0:on 810525,w/unit at 99% Power,Containment Hydrogen Analyzer 1-43-210 Was Found Out of Tolerance During Performance of Scheduled Surveillance Test.Reagent Flow Readjusted to Bring Analyzer Into Tolerance

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/03L-0:on 810525,w/unit at 99% Power,Containment Hydrogen Analyzer 1-43-210 Was Found Out of Tolerance During Performance of Scheduled Surveillance Test.Reagent Flow Readjusted to Bring Analyzer Into Tolerance
ML20005A531
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 06/23/1981
From: Harding M, Wilkey A
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20005A524 List:
References
LER-81-063-03L, LER-81-63-3L, NUDOCS 8106300430
Download: ML20005A531 (1)


LER-1981-063, /03L-0:on 810525,w/unit at 99% Power,Containment Hydrogen Analyzer 1-43-210 Was Found Out of Tolerance During Performance of Scheduled Surveillance Test.Reagent Flow Readjusted to Bring Analyzer Into Tolerance
Event date:
Report date:
3271981063R03 - NRC Website

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el DI)GettT NUVOEM 08 69 EVENT OATE F4 il RtPOmfDATE to tVENT DESCRIPTION AND PROSAOLE CONSEQUENCES O'o o 2 l With unit 1 at 99% at 1420 CDT on 5/25/81, containreent hydrogen analyzer 1-43-210 was l found out of tolerance during performance of its scheduled surveillance test. The gl blant; entered the action statement of LCO 3.6.4.1.

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