LER-1981-050, /03L-0:on 810504,w/unit at 60% Rated Thermal Power,Pressurizer Level Pressure Channel Declared Inoperable When Indicator Read Higher than Redundant Channels.Caused by Error in Senseline Tubing to Condensate Pot |
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- 4 69 EVE NT DATE 74 76 REPORT DAT E to EvfNT DESCRIPTION AND PROD A8LE CONSEQUENCES h 10 l 2 l l With Unit I at 60% RTP. pressurizer level oressure channel 1-L-68-339 was declared I
inoperable at 0340 CST when the associated indicator was 3bserved to be reading higher [
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At 1505 CST, auxiliary control room channels 1-L-68-325C and 3260 were l
Io is l l also declared inoperable for the same reason, and action statement "a" of LCO 3.3.3.5 l
lo j il l was entered. There was no effect on public health or safety. Reference: SORO-50-327/[
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Durine a subsequent inn i t outane. Instrn-not ~ocMnicn dincovernd gl an error in the sense line tubing to the condensate pot which accounted for the errors li13l l exnerienced with the instrument loops. The error was corrected and the loops have been.
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LSequoyah Nucis r Plant LER SUPPLEMENTAI. INFORMATION SQRO-50-327/31050 In February 1981, DCR-P1036 was submitted to modify the tubing to the condensate pot in the sense lines for pressurizer level loops 1-L-68-325C, 326C, and 339. -Tubing from'the condensate pot to the pressurizer vapor sample line was to be added to allcw noncondensable gases to escape from the pot so that the pot could function properly to maintain the required reference leg for the three level loops. This request was implemented by ECN L5392.
During a channel check performed on March 23, 1981, pressurizer level loop 1-L-68-339 was discovered to be indicating approximately 15% lower than redundant citannels. The loop was declared inoperable and the associated reactor protection bistable was tripped in accordance with action 7 of LCO 3.3.1.1.
Since auxiliary control room loops 1-L-68-325C and 1-L-68-326C shared a common sensing line with 1-L-68-339, they were also checked. After verifying that the two auxiliary control loops were also indicating approx-tmately 15% low, the plant entered action statement "a" of LCO 3.3.3.5.
The error was diagnosed as an increased static head in the common reference leg for the loop transmitters. The 15% orror was attributed to an accumulation of water in the tubing added by ECN L5392.
To compensate for the in crease'd sqatic head, the pressurizer high level trip bintable setpcint was shifted f, rom 92% to 76%. In addition, temporary scales were installed on main control r~oom indicators to enable operatois to obtain direct readings. Ute auxiliary control room loops were recubed to the sensing line for 1-L-68-335, which did not have the sense line modification (ECN L5392).
On April 2, 1981, a channel check of 1-L-68-339 revealed that loop to be indi-cating approximately 8% high. Since this indicated that previous corrective action was not adequate, the loop was declared inoperable and the associated bistable tripped in accordance~with action statement 7 of LCO 3.3.1.1.
A return to the premodification configuration was planned for the next unit outage.
On April 17, 1981, auxiliary control room loops 1-L-68-325C and 1-L-68-326C were observed to be reading approximately 15% high. The pltnt again entered action statement "a" of LCO 3.3.3.5.
During the subsequent unit outage, the sense lines for 1-L-68-339, 1-L-68-325C, and 1-L-68-326C were returned to their premodification configuration. Since this configuration was susceptible to variations in the reference leg static head, the loops were monitored closely and refilled as necessary. Since losses of condensate in the reference leg resulted in higher (than actual) pressurizer level signals, the limiting safety system setting off 93% was not compromised.
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.. LER SUPPLEMENTAL INFORMATION (Continued)
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On'May 4, 1981, pressurizer level channels.1-L-68-339, 325C, and 326C were again d : lared low when they were observed ' to be reading higher than redun-dant channels. The reference legs were backfilled, calibration verified, and' the loops were returned to service that same day.
During a subsequent unit outage, instrument mechanics discovered that sense
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line tubing to the condensate pot for the instrument loops had been revarsed
- - inside a wall-penetration. The line from the bottom of the condensate pet
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- - was tubed to.the vent line and the line from the top.of the pot was tubed to the instrument loop transmitters. The tubing error had prevented proper opcration of the condensate pot which had resulted si erroneous-level indi-Cations.
1 The tubing error was corrected on May 13-14, 1981, and the loops were returned to'scrvice. A modification on the condensate pots has been requested (DCR-1120) to-improve their operation. A similar modification to the Unit 2 pressurizer loopu.was perforced and verified during-Unit 2 hot functional testing.
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| 05000327/LER-1981-001-03, /03L-0:on 810102,condensate Storage Tank Level Channel 0-L-2-230 Declared Inoperable When Control Room Indicator Failed Low.Caused by Disconnected Instrument Sense Line Due to Improperly Tightened Compression Fitting | /03L-0:on 810102,condensate Storage Tank Level Channel 0-L-2-230 Declared Inoperable When Control Room Indicator Failed Low.Caused by Disconnected Instrument Sense Line Due to Improperly Tightened Compression Fitting | | | 05000327/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000327/LER-1981-002-03, /03L-0:on 810109,two Intermediate Deck Doors in Ice Condenser Found Frozen Closed.Caused by Water Leaking from AHU-3A Defrost Drain Line Flange Due to Loose Flange Bolts.Bolts Retightened | /03L-0:on 810109,two Intermediate Deck Doors in Ice Condenser Found Frozen Closed.Caused by Water Leaking from AHU-3A Defrost Drain Line Flange Due to Loose Flange Bolts.Bolts Retightened | | | 05000327/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000327/LER-1981-003-03, /03L-0:on 810105,main Feedwater Flow Channel F-3-35B Failed Low.On 810112 Feedwater Channel F-3-35B & F-3-90B Failed.Caused by Freezing of Inadequately Protected Instrument Sense Lines.Lines Thawed | /03L-0:on 810105,main Feedwater Flow Channel F-3-35B Failed Low.On 810112 Feedwater Channel F-3-35B & F-3-90B Failed.Caused by Freezing of Inadequately Protected Instrument Sense Lines.Lines Thawed | | | 05000327/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000327/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000327/LER-1981-004-03, /03L-0:on 810112,RWST Instrument Channel L-63-54 Failed.Caused by Sense Lines Freezing Due to Insufficient Insulation Around Lines & on Sides of Cabinet Housing Level Transmitter.Heaters in Use Until Insulation Can Be Added | /03L-0:on 810112,RWST Instrument Channel L-63-54 Failed.Caused by Sense Lines Freezing Due to Insufficient Insulation Around Lines & on Sides of Cabinet Housing Level Transmitter.Heaters in Use Until Insulation Can Be Added | | | 05000327/LER-1981-005-03, /03L-0:on 810114,capacitor C1A in A10 Power Supply & Control Card RB-8 Failed While in Svc.Caused by Failure of Vital Inverter 2-II.Components Replaced & Inverter Returned to Svc on 810114 | /03L-0:on 810114,capacitor C1A in A10 Power Supply & Control Card RB-8 Failed While in Svc.Caused by Failure of Vital Inverter 2-II.Components Replaced & Inverter Returned to Svc on 810114 | | | 05000327/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000327/LER-1981-006-03, /03L-0:on 810114,stroke Test Not Performed Following 800929 Repair of Leaking Valve 1-FCV-63-38.Caused by Inadequate Procedure.Procedure Being Revised | /03L-0:on 810114,stroke Test Not Performed Following 800929 Repair of Leaking Valve 1-FCV-63-38.Caused by Inadequate Procedure.Procedure Being Revised | | | 05000327/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000327/LER-1981-007-03, /03L-0:on 810116,level Channel for Steam Generator 3 (L-3-97) Declared Inoperable.Caused by Failure of Trip Bistable 1-LS-3-97F to de-energize.Module Replaced,Calibr & Returned to Svc | /03L-0:on 810116,level Channel for Steam Generator 3 (L-3-97) Declared Inoperable.Caused by Failure of Trip Bistable 1-LS-3-97F to de-energize.Module Replaced,Calibr & Returned to Svc | | | 05000327/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000327/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000327/LER-1981-008-03, /03L-0:on 810116,three Intermediate Deck Doors to Ice Condenser,Under Air Handling Units 6A,8A & 8B,found Frozen Closed.Caused by Frozen Water in Drain Lines Due to Fuse Failure in Heat Tape Controller.Ice Removed | /03L-0:on 810116,three Intermediate Deck Doors to Ice Condenser,Under Air Handling Units 6A,8A & 8B,found Frozen Closed.Caused by Frozen Water in Drain Lines Due to Fuse Failure in Heat Tape Controller.Ice Removed | | | 05000327/LER-1981-009-03, /03L-0:on 810127,containment Sump Level Loop L-63-177 Declared Inoperable.Caused by Calibr Drift Due to Problem W/Level Transmitter.Transmitter Replaced | /03L-0:on 810127,containment Sump Level Loop L-63-177 Declared Inoperable.Caused by Calibr Drift Due to Problem W/Level Transmitter.Transmitter Replaced | | | 05000327/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000327/LER-1981-010-03, /03L-0:on 810128,notification Received That During Ieb 79-14 review,180-1b (Light) Weight Discrepancy Discovered,Altering Support Design Requirements.Caused by Incorrect Weights Being Used in Computer Analysis | /03L-0:on 810128,notification Received That During Ieb 79-14 review,180-1b (Light) Weight Discrepancy Discovered,Altering Support Design Requirements.Caused by Incorrect Weights Being Used in Computer Analysis | | | 05000327/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000327/LER-1981-011-03, /03L-0:on 810130,vital Inverter & Vital Instrument Power Board 1-I Declared Inoperative.Caused by Severance of Conduit & Cable B30I Supplying Power to Inverter.Cable & Conduit Replaced | /03L-0:on 810130,vital Inverter & Vital Instrument Power Board 1-I Declared Inoperative.Caused by Severance of Conduit & Cable B30I Supplying Power to Inverter.Cable & Conduit Replaced | | | 05000327/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000327/LER-1981-012-03, /03L-0:on 810126,RCS Tave Decreased Below Limits. Caused by Operator Failure to Coordinate Turbine Loading Rate.Turbine Load Reduced & RCS Tave Increased | /03L-0:on 810126,RCS Tave Decreased Below Limits. Caused by Operator Failure to Coordinate Turbine Loading Rate.Turbine Load Reduced & RCS Tave Increased | | | 05000327/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000327/LER-1981-013-03, /03L-0:on 810203,liquid Radwaste Monitor, 0-RE-90-122,declared Inoperable.Caused by High Background Count Reading Due to Leak in Brooks Rotameter.Rotameter Seals Replaced,Sample Chamber Cleaned & Monitor Flushed Out | /03L-0:on 810203,liquid Radwaste Monitor, 0-RE-90-122,declared Inoperable.Caused by High Background Count Reading Due to Leak in Brooks Rotameter.Rotameter Seals Replaced,Sample Chamber Cleaned & Monitor Flushed Out | | | 05000327/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000327/LER-1981-014-03, /03L-0:on 810123,testing Procedure SI-158 for Containment Isolation Valves 1-FCV-62-72,73 & 74 Was Determined to Be Inadequate.Caused by Failure to Take Into Account back-pressure in Line.Procedure Changed | /03L-0:on 810123,testing Procedure SI-158 for Containment Isolation Valves 1-FCV-62-72,73 & 74 Was Determined to Be Inadequate.Caused by Failure to Take Into Account back-pressure in Line.Procedure Changed | | | 05000327/LER-1981-014, Forwards LER 81-014/03L-0 | Forwards LER 81-014/03L-0 | | | 05000327/LER-1981-015-03, /03L-0:on 810216,during Surveillance Testing,Ice Condenser Basket Bays 1,18 & 24 Were Found Below Limits for Average Basket Weight.Caused by Sublimation.Ice Added Throughout Ice Condenser | /03L-0:on 810216,during Surveillance Testing,Ice Condenser Basket Bays 1,18 & 24 Were Found Below Limits for Average Basket Weight.Caused by Sublimation.Ice Added Throughout Ice Condenser | | | 05000327/LER-1981-015, Forwards LER 81-015/03L-0 | Forwards LER 81-015/03L-0 | | | 05000327/LER-1981-016-03, /03L-0:on 810206,diesel Generator 2B-B Breaker Tripped Twice While Attempting to Synchronize W/Tva Power Grid for Surveillance Test SI-7.Caused by Overcurrent During Paralleling Operation.Target Reset & Parallel Repeated | /03L-0:on 810206,diesel Generator 2B-B Breaker Tripped Twice While Attempting to Synchronize W/Tva Power Grid for Surveillance Test SI-7.Caused by Overcurrent During Paralleling Operation.Target Reset & Parallel Repeated | | | 05000327/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000327/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000327/LER-1981-017-03, /03L-0:on 810212,welder Accidentally Blew Pin Hole in Pipe Sleeve,Releasing Low Level Activity Xe-133.Caused by Thin Wall Pipe & Restricted Access.Pin Hole Repaired | /03L-0:on 810212,welder Accidentally Blew Pin Hole in Pipe Sleeve,Releasing Low Level Activity Xe-133.Caused by Thin Wall Pipe & Restricted Access.Pin Hole Repaired | | | 05000327/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000327/LER-1981-018-03, /03L-0:on 810205,discovered That SI-137.2,RCS Water Inventory,Not Performed within 72-h Per Surveillance Requirements.Caused by Steady State Conditions Not Being Established Long Enough for Performance Before Reactor Trip | /03L-0:on 810205,discovered That SI-137.2,RCS Water Inventory,Not Performed within 72-h Per Surveillance Requirements.Caused by Steady State Conditions Not Being Established Long Enough for Performance Before Reactor Trip | | | 05000327/LER-1981-019-03, /03L-0:on 810211,inside Containment Isolation Valve 1-33-704 on Svc Air Header Discovered Omitted from Drawing.Valve Added | /03L-0:on 810211,inside Containment Isolation Valve 1-33-704 on Svc Air Header Discovered Omitted from Drawing.Valve Added | | | 05000327/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000327/LER-1981-020, Forwards LER 81-020/03X-1 | Forwards LER 81-020/03X-1 | | | 05000327/LER-1981-020-03, /03X-1:on 810207,w/unit in Mode 5 & Auxiliary Bldg Gas Treatment Sys Train B Fan Discharging Through Shield Bldg Exhaust Vent,Radiation Monitor for Exhaust Path 2-RM-90-100 Discovered Inoperable.Cause Not Stated | /03X-1:on 810207,w/unit in Mode 5 & Auxiliary Bldg Gas Treatment Sys Train B Fan Discharging Through Shield Bldg Exhaust Vent,Radiation Monitor for Exhaust Path 2-RM-90-100 Discovered Inoperable.Cause Not Stated | | | 05000327/LER-1981-021-03, /03L-0:on 810211,reactor Coolant Pumps 1 & 2 Were Stopped.Caused by RCS Pressure Going to Zero After RHR Containment Spray Isolation Valve Inadvertently Opened.Pumps Returned to Operable Status in Approx 1-h | /03L-0:on 810211,reactor Coolant Pumps 1 & 2 Were Stopped.Caused by RCS Pressure Going to Zero After RHR Containment Spray Isolation Valve Inadvertently Opened.Pumps Returned to Operable Status in Approx 1-h | | | 05000327/LER-1981-021, Forwards LER 81-021/03L-0 | Forwards LER 81-021/03L-0 | | | 05000327/LER-1981-022, Forwards LER 81-022/03L-0 | Forwards LER 81-022/03L-0 | | | 05000327/LER-1981-022-03, /03L-0:on 810219,w/unit in Mode 5,chlorine Detector O-CLAN-43-205A Declared Inoperable.Caused by Electrolyte Used to Drip Onto Sensor Becoming Stopped Up in Felt Filter.Filter Replaced & Detector Returned to Svc | /03L-0:on 810219,w/unit in Mode 5,chlorine Detector O-CLAN-43-205A Declared Inoperable.Caused by Electrolyte Used to Drip Onto Sensor Becoming Stopped Up in Felt Filter.Filter Replaced & Detector Returned to Svc | | | 05000327/LER-1981-023-03, /03L-1:on 810303,four Undersized Pipe Sleeves Associated W/Seal Injection Water Lines to Reactor Coolant Pumps Identified.Caused by Incorrect Installation.Workplan 9073 Issued to Reshape Subj Piping Sleeves | /03L-1:on 810303,four Undersized Pipe Sleeves Associated W/Seal Injection Water Lines to Reactor Coolant Pumps Identified.Caused by Incorrect Installation.Workplan 9073 Issued to Reshape Subj Piping Sleeves | | | 05000327/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000327/LER-1981-024, Forwards LER 81-024/03L-0 | Forwards LER 81-024/03L-0 | | | 05000327/LER-1981-024-03, /03L-0:on 810314,problems Were Experienced W/Steam Supply Controls to steam-driven Auxiliary Feedwater Pump 1A-S.Probably Caused by Initial Pressure Spike & Bias Error Due to Clog in Sense Lines Causing Steam Supply Isolatio | /03L-0:on 810314,problems Were Experienced W/Steam Supply Controls to steam-driven Auxiliary Feedwater Pump 1A-S.Probably Caused by Initial Pressure Spike & Bias Error Due to Clog in Sense Lines Causing Steam Supply Isolation | | | 05000327/LER-1981-025, Forwards LER 81-025/03L-0 | Forwards LER 81-025/03L-0 | | | 05000327/LER-1981-025-03, /03L-0:on 810217,during Surveillance Instruction SI-7,diesel Generator 1B-B Failed to Load Properly.Caused by Blown Fuse in Governor Potentiometer Circuit.Fuse Replaced | /03L-0:on 810217,during Surveillance Instruction SI-7,diesel Generator 1B-B Failed to Load Properly.Caused by Blown Fuse in Governor Potentiometer Circuit.Fuse Replaced | |
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