05000327/LER-1981-040-03, /03L-0:on 810401,channel Check of Containment Sump Level Indicators Revealed LI-63-178 Was Reading Approx 6% High.Probably Caused by Transmitter Problem.Investigation to Be Made During Next Outage

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/03L-0:on 810401,channel Check of Containment Sump Level Indicators Revealed LI-63-178 Was Reading Approx 6% High.Probably Caused by Transmitter Problem.Investigation to Be Made During Next Outage
ML20003H263
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 04/30/1981
From: Harding M, Wilkey A
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20003H259 List:
References
LER-81-040-03L-03, LER-81-40-3L-3, NUDOCS 8105050446
Download: ML20003H263 (1)


LER-1981-040, /03L-0:on 810401,channel Check of Containment Sump Level Indicators Revealed LI-63-178 Was Reading Approx 6% High.Probably Caused by Transmitter Problem.Investigation to Be Made During Next Outage
Event date:
Report date:
3271981040R03 - NRC Website

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There'is no effect on public health or safety.

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