05000327/LER-1981-024-03, /03L-0:on 810314,problems Were Experienced W/Steam Supply Controls to steam-driven Auxiliary Feedwater Pump 1A-S.Probably Caused by Initial Pressure Spike & Bias Error Due to Clog in Sense Lines Causing Steam Supply Isolatio

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/03L-0:on 810314,problems Were Experienced W/Steam Supply Controls to steam-driven Auxiliary Feedwater Pump 1A-S.Probably Caused by Initial Pressure Spike & Bias Error Due to Clog in Sense Lines Causing Steam Supply Isolation
ML20003E903
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 04/10/1981
From: Harding M, Wilkey A
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20003E897 List:
References
LER-81-024-03L-03, LER-81-24-3L-3, NUDOCS 8104170468
Download: ML20003E903 (2)


LER-1981-024, /03L-0:on 810314,problems Were Experienced W/Steam Supply Controls to steam-driven Auxiliary Feedwater Pump 1A-S.Probably Caused by Initial Pressure Spike & Bias Error Due to Clog in Sense Lines Causing Steam Supply Isolation
Event date:
Report date:
3271981024R03 - NRC Website

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' EVEidT DESCRIPTION AND PROS ASLE CONSECUENCES h Q l At 1204 CST with unit in cride 3 af ter a reactor trin, the steam-driven auxiliary feed-1' 1A-S was declared ineperable when the operator experienced problems with the g l water pir p [o 14 j l steam.sunniv controls. The plant entered action statement "a" of I.CO'3.7.1.2.

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g l pump was automatically isolated bv PDIS-1-17 and~18.

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9 Wrdin2/A. M. Wilkev.

Phone (615) 342-8317 8104170468

Tcon:ccee Valley Authority Sequoyah Nuclear Plant LER SUPPLEMENTAL INFORMATION SQRO-50-327/81024 Technical Specification Involved:

3.7.1.2.b Reported Under Technical Specification:

6.9.1.13.b Date of Occurrence: 3/14/81 Time of Occurrence: 1204 CST Identification and Description of Occurrence:

Operator experienced difficulty with oceam supply controls to steam-driven 4

l auxiliary feedwater pump 1A-S.

Pump was declared inoperable.

i Conditions Prior to Occurrence:

Unit in mode 3 following reactor trip Apparent Cause of Occurrence:

An initial pressure spike (over 50-feet WC) in additior. to a bias error caused by a clog in the sense lines to PDIS-1-17 and 18 (approximately 5-feet WC) caused PDIS-1-17 and 18 to isolate the steam supply to the i

AFW pump turbine.

Corrective Action

The setpoints for PDIS-1-17 and 18 were temporarily modified with engineering design's concurrence from 55.68 f t. WC to 95 f t. WC to prevent recurrence of this event in the future. A permanent setpoint change will be implemented by a design change request now being prepared and expected to be submitted by May 1, 1981.

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