Similar Documents at Hatch |
|---|
|
LER-1981-016, /03L-0:on 810305,steam Flow Indicator for Main Steamline a Did Not Show Flow in Line While Increasing Reactor Power.Caused by Valve Stem Separated from Inner Disc of Valve.Valve Stem,Inner & Main Discs & Cylinder Replaced |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3661981016R03 - NRC Website |
|
text
NHC F OHM N G U. S. fJUCL E AH HF GL L M ORY COMMISslON LICENSEE EVENT REPORT f
conTHololocel l
l l
l l
l@
(PLEASE PRUM OR TYPE ALL Hf OUIRED INFORMATIOfD v
[o W l C l A l E II lH l 2 l@l0 l0 l-10 l0 l0 l010 l-10 l0 l@l 41 IL11 ll llGI I IQ s 9 sctNste coat i4 is uco.st reutn a
2o umtwo nPL u si uAi w lolil
'$,$ l l-j@l 0 l 5 l 0 l 0 l0 l 3 l 6 l 6 l@l 0 13 10 j 5 l 8 l1 l@l 01 3 ] 2 l 7 l 8 l 1 l@
s l
8 60 61 DO A 6 7 *.UYu t ti bd 0')
tvtNT DATE 14 15 P[FJt T DAT E BJ EVENT DESCRIPTION AND PROBABLE CONSECUENCES h I o 12 ] l On llarch 5,1931, while increasinq reactor power, the Steam Flow Incica+w I
[o i3 i l for the "A' flain Steamline was not indicating a flow in the line. When j
10141 I an attempt was made to' close the Inboard Isolation Valve on the "A"
l l O l sj l Steamline, a full closed indication could not be received.
The Outboard l
la lo l L Isolation Valve was closed per Tech Spec 3.6.3, Action a.2. This was j
jol7l l a non-repetitive event.
There was no effects to public health and l
l o ja l l safety due to this event.
83 j
7 8 9 SYSTEM CAU!E
CAUSE
COYP.
VALVE CODE COOE SUBCODE COYPONENT CODE SU8 CODE SUCCODE lol9l l C l D l@ [E j@ U@ l V l Al L l V l E l X l@ y@ y @
7 8
9 10 11 12 IJ 18 19 20 SEQUENTI AL OCCU R R E N CE REPORT DEVISION
, p.RO EVENT YE AR REPOHT NO.
CODE TYPE NO.
@;Ugi lBl1l l-l l 01 Il 6l y
l0l3l U
[--J l0l E
_2%
22 23 24 26 21 28 29 30 31 32
[
AK N A T ON ON PLANT T
140VR S S B ITT D FOR I B.
PP LI MAN F PCH J
lAl@l_Jj@
l_zj@
[j@
l 010l 0101 Lt]@
I ri l@
I r4 l@
lal31414l@
33 34 35 30 31 40 41 42 43 44 47 CAUSE oESCRIPTioN AND CORRECTIVE ACTIONS h li lo l l When the valve was disassembled it was discovered that the valve sten had I
L separated from the inner disc of the valve.
The valve stem, inner disc.
I i i iii,;
disc cylinder and main disc were replaced and the valve reassembled.
I i3 l
The Main Steam Isolation Valve Trip Test was then performed and the l
Ii14l 1 valve returned to service on March 14, 1981.
7 8 9 60 ST JS
% POW E n OTHER STATUS sCOV Y DISCOVERY DESCRIPTION li 151 l F l@ l 0l S l 5l@l f1A
,j l Al @l Operator Observation l
ACTIVITY CONTENT RE LE ASE D OF RE LE ASE AYOUNT OF ACTtVITY LOCATION OF RELEASE li lo l LZ l@ l zi@l tiA I
I flA l
7 8 9_
10 11 44 45 Su PEH50NNEL EJtPOSURES NUVaER TYPE JE SCntPTION 1010l01@lzl@l ftA l
i 7
,E nSONNJ',NJu',2,ES oESCni.1 ION @
Nuvu n 10l0l0l@l flA l
i s G 9 11 12 80 1 OSS OF OR D AVACE TO FACalliY 43)
TYPE DESC9sPflON I
LZ_l@l itA I
J B 9 10 30 isSutf@OL HipisON UL l
fA I
! ! I I I I I I I I I ! 15 2 o 7
8 9 in 68 69 ra ;
- - 8104030 D
PW E OF PHEPAHEH E. I. Ili X. SUDt. OfL Qint-FHONE: Obh7-7781 t
s-LER No.: 50-366/1981-016 Licensee: Georgia Power Company Facility: Edwin I. Hatch Docket No.: 50-366
Narrative
Report for LER 50-366/1981-016.
On thrch 5, 1981, with the reactor in the run mode at 55% Mut, there was no flow in the "A" Main Steamline as evidenced by the Steam flow Indicator. When an attempt was made to slow close the Inboard Main Steam Isolation Valve on the "A" Steamline, to check for an increase in the other steamline flows, the valve did
...t give a full closed indication.
As the Inboard Isolation Valve was incapable of meeting the requirements of Tech Specs Table 3.6.3-1, the Outboard Isolation Valve was closed per Tech Specs 3.6.3 Action A.2.
This was not a repetitive event.
~When the valve.as disassembled, after the reactor was shutdown for other activi tie, it was discovered that the valve stem had separated from the inner disc of the valve.
Although the valve did not receive a closed indication it was closed, as the valve disc closes in the direction of the flow.
The valve stem then hit against the top of the disc preventing the stem from traveling enough to actuate the limit switches for a full closed indication.
The. valve stem, inner disc, disc cylinder and main disc were replaced and the valve reassembled.
A leak rate -test was then performed and no leakage was found. The Main Steam ~ Line Isolation Valve Trip Test was performed satisfactorily and the valve returned to service on March 14, 1981.
The Steam Flow Indicators were checked on'.the other three steam lines to insure that this was a singular incident.
Isolation Valves for Unit I and Unit II are manufactured by different companies. Unit II valves are manufactured by -Rockwell and Unit I valves are manufactured by Atwood and Morrill...
Neither public health' and safety nor safe plant, 6
6 g:
m
- ll --..--
L-
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000366/LER-1981-001-03, /03L-0:on 810102,during Refueling,Drywell Isolation Valve 2T48/F209 Found Leaking When LLRT Performed on Drywell to Torus Dp Sys.Caused by Scratches on Valve Seat Due to Valve Closing on Debris | /03L-0:on 810102,during Refueling,Drywell Isolation Valve 2T48/F209 Found Leaking When LLRT Performed on Drywell to Torus Dp Sys.Caused by Scratches on Valve Seat Due to Valve Closing on Debris | | | 05000366/LER-1981-001, Forwards LER 81-001/03L-0.Detailed Event Analysis Encl | Forwards LER 81-001/03L-0.Detailed Event Analysis Encl | | | 05000321/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000321/LER-1981-001-01, /01T-0:on 801228,HPCI Steam Line Pressure Switches 1E41-N001a,c,d Actuated Outside Tech Specs.Caused by Switch Setpoint Drift.Switches Recalibr | /01T-0:on 801228,HPCI Steam Line Pressure Switches 1E41-N001a,c,d Actuated Outside Tech Specs.Caused by Switch Setpoint Drift.Switches Recalibr | | | 05000366/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000366/LER-1981-002-03, /03L-0:on 810106,reactor Core Isolation Cooling Steamline Pressure Switches 2E51-NO19A & C Were Found to Actuate Below Tech Spec Limits.Caused by Setpoint Drift. Switches Recalibr | /03L-0:on 810106,reactor Core Isolation Cooling Steamline Pressure Switches 2E51-NO19A & C Were Found to Actuate Below Tech Spec Limits.Caused by Setpoint Drift. Switches Recalibr | | | 05000321/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000321/LER-1981-002-03, /03L-0:on 810101,more than 5 Gpm Leaked Into Drywell W/Reactor at 401 Mwe.Caused by Mechanical Seal Leaking Water from Reactor Recirculation pump,1B31-C001A. Seal Replaced | /03L-0:on 810101,more than 5 Gpm Leaked Into Drywell W/Reactor at 401 Mwe.Caused by Mechanical Seal Leaking Water from Reactor Recirculation pump,1B31-C001A. Seal Replaced | | | 05000366/LER-1981-003-03, /03L-0:on 810223,core Max Fraction of Limiting Power Density Found to Be Greater than Frtp During Startup. Caused by Time Delays for Adjusting Rods,Running Transient Incore Probe Scans & Processing Time for Computer | /03L-0:on 810223,core Max Fraction of Limiting Power Density Found to Be Greater than Frtp During Startup. Caused by Time Delays for Adjusting Rods,Running Transient Incore Probe Scans & Processing Time for Computer | | | 05000321/LER-1981-003-03, /03L-0:on 810130,HPCI Governor Valve Stuck Open. Caused by Lift Rod Being Bent & Galled Due to Interference Between Lift Rod Fork Connector & Valve Lever.Damaged Rod Replaced,Upper Guide Bushing Honed & Fork Modified | /03L-0:on 810130,HPCI Governor Valve Stuck Open. Caused by Lift Rod Being Bent & Galled Due to Interference Between Lift Rod Fork Connector & Valve Lever.Damaged Rod Replaced,Upper Guide Bushing Honed & Fork Modified | | | 05000366/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000321/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000366/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000366/LER-1981-004-03, /03L-0:on 810122,nozzle Loads Found Exceeding Vendor Allowables for Reactor Core Isolation Cooling Steam Turbine During Reanalysis of Piping & Hangers Per IE Bulletin 79-14.Caused by Ae Error in Sys Design | /03L-0:on 810122,nozzle Loads Found Exceeding Vendor Allowables for Reactor Core Isolation Cooling Steam Turbine During Reanalysis of Piping & Hangers Per IE Bulletin 79-14.Caused by Ae Error in Sys Design | | | 05000321/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000321/LER-1981-004-03, /03L-0:on 810106,w/unit in Steady State Power Operation,Qa Audit Showed That Temporary Procedure Change HNP-818 Was Not Approved by Plant Manager within 14 Days of Implementation.Caused by Deletion of Requirement | /03L-0:on 810106,w/unit in Steady State Power Operation,Qa Audit Showed That Temporary Procedure Change HNP-818 Was Not Approved by Plant Manager within 14 Days of Implementation.Caused by Deletion of Requirement | | | 05000366/LER-1981-005-01, /01T-0:on 810126,reactor Pressure Vessel Core Spray Loops Discovered Inoperable.Caused by Procedure HNP-2-1230 Being Performed,Closing Manual Injection Valves 2E21-F007A & B.Valves Reopened & Procedure Changed | /01T-0:on 810126,reactor Pressure Vessel Core Spray Loops Discovered Inoperable.Caused by Procedure HNP-2-1230 Being Performed,Closing Manual Injection Valves 2E21-F007A & B.Valves Reopened & Procedure Changed | | | 05000366/LER-1981-005, Forwards LER 81-005/01T-0 | Forwards LER 81-005/01T-0 | | | 05000321/LER-1981-005-03, /03L-0:on 810113,during Steady State Operation, Drywell Temp Recorder IT47-R612 Found to Be Inoperative. Caused by Misalignment of Cam Follower Contact W/Main Programming Cam.Follower Adjusted to Maintain Contact W/Cam | /03L-0:on 810113,during Steady State Operation, Drywell Temp Recorder IT47-R612 Found to Be Inoperative. Caused by Misalignment of Cam Follower Contact W/Main Programming Cam.Follower Adjusted to Maintain Contact W/Cam | | | 05000321/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000366/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000366/LER-1981-006-03, /03L-0:on 810123,standby Gas Treatment Sys Filter train,2T46-D001A,removed Less Halogenated Hydrocarbon Refrigerant Gas than Required by Tech Specs During Testing by Vendor.Caused by Defective Charcoal in Filter Bed | /03L-0:on 810123,standby Gas Treatment Sys Filter train,2T46-D001A,removed Less Halogenated Hydrocarbon Refrigerant Gas than Required by Tech Specs During Testing by Vendor.Caused by Defective Charcoal in Filter Bed | | | 05000321/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000321/LER-1981-006-03, /03L-0:on 810119,standby Liquid Control Pump a Discharge Relief Valve 1C41-F029A Operated Outside Tech Spec.Caused by Setpoint Drift.Valve Reset | /03L-0:on 810119,standby Liquid Control Pump a Discharge Relief Valve 1C41-F029A Operated Outside Tech Spec.Caused by Setpoint Drift.Valve Reset | | | 05000321/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000321/LER-1981-007-03, /03L-0:on 810203 & 19,unit 1 Cable Spread Room Sprinkler Sys Was Inoperable for Period Greater than 14 Days & Special Repts Were Not Issued.Caused by Personnel Error. Personnel Reinstructed | /03L-0:on 810203 & 19,unit 1 Cable Spread Room Sprinkler Sys Was Inoperable for Period Greater than 14 Days & Special Repts Were Not Issued.Caused by Personnel Error. Personnel Reinstructed | | | 05000366/LER-1981-007-03, /03L-0:on 810126,discovered That on 810124 & 25 Reactor Coolant Sampled from Wrong Sample Line.Caused by Lack of Communication Among Personnel Who Collect & Analyze Reactor Coolant.Personnel Instructed & Coolant Sampled | /03L-0:on 810126,discovered That on 810124 & 25 Reactor Coolant Sampled from Wrong Sample Line.Caused by Lack of Communication Among Personnel Who Collect & Analyze Reactor Coolant.Personnel Instructed & Coolant Sampled | | | 05000366/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000321/LER-1981-008-03, /03L-0:on 810216,in Normal Operations at 309 Mwt, 1E51-N012A,B,C & D Actuated at 10.2,11.3,11.2 & 10.7 Psig, Respectively.Caused by Switch Setpoint Drift.Barksdale Switches Recalibr | /03L-0:on 810216,in Normal Operations at 309 Mwt, 1E51-N012A,B,C & D Actuated at 10.2,11.3,11.2 & 10.7 Psig, Respectively.Caused by Switch Setpoint Drift.Barksdale Switches Recalibr | | | 05000321/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000366/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000366/LER-1981-008-03, /03L-0:on 810119,pressure Switches Were Found Out of Tolerance.Caused by Setpoint Drift.Pressure Switches Recalibr & Returned to Svc | /03L-0:on 810119,pressure Switches Were Found Out of Tolerance.Caused by Setpoint Drift.Pressure Switches Recalibr & Returned to Svc | | | 05000366/LER-1981-009-03, /03L-0:on 810212,reactor Coolant Not Analyzed Once Per 24-h as Required by Tech Spec.Caused by Reactor Vessel Hydro During Time Period When Next Conductivity Measurement Was to Be Taken | /03L-0:on 810212,reactor Coolant Not Analyzed Once Per 24-h as Required by Tech Spec.Caused by Reactor Vessel Hydro During Time Period When Next Conductivity Measurement Was to Be Taken | | | 05000366/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000321/LER-1981-009-03, /03L-0:on 810206,nitrogen Storage Tank Inventory Went Below 2000 Gallon Tech Spec Requirement.Caused by Supplier Delaying Shipment.Shipment Received.Supplier Instructed Not to Delay Shipments | /03L-0:on 810206,nitrogen Storage Tank Inventory Went Below 2000 Gallon Tech Spec Requirement.Caused by Supplier Delaying Shipment.Shipment Received.Supplier Instructed Not to Delay Shipments | | | 05000321/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000366/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000366/LER-1981-010-03, /03L-0:on 810222,reactor Core Isolation Cooling Auto Flow Controller Did Not Control Turbine Properly While in Auto Position During Quickstart Test.Caused by Loose Ribbon Connector on Flow Control M-4 Station | /03L-0:on 810222,reactor Core Isolation Cooling Auto Flow Controller Did Not Control Turbine Properly While in Auto Position During Quickstart Test.Caused by Loose Ribbon Connector on Flow Control M-4 Station | | | 05000321/LER-1981-010, Forwards LER 81-010/01T-0 | Forwards LER 81-010/01T-0 | | | 05000321/LER-1981-010-01, /01T-0:on 810211,AE Reported That Diesel Generator 1A,1C,2A,2B & 1B Outlet Svc Water Piping & Associated Seismic Supports Exceeded Tech Spec.Caused by Design Omission.Design Mods Made | /01T-0:on 810211,AE Reported That Diesel Generator 1A,1C,2A,2B & 1B Outlet Svc Water Piping & Associated Seismic Supports Exceeded Tech Spec.Caused by Design Omission.Design Mods Made | | | 05000321/LER-1981-011-03, /03L-0:on 810214,liquid Radwaste Sample Tank, WSTB1,discharged Prior to Analysis,Contrary to Ets.Caused by Technician Error in Collecting Unit 2 Radwaste Sample in Prelabeled Unit 1 WSTB-1 Bottle | /03L-0:on 810214,liquid Radwaste Sample Tank, WSTB1,discharged Prior to Analysis,Contrary to Ets.Caused by Technician Error in Collecting Unit 2 Radwaste Sample in Prelabeled Unit 1 WSTB-1 Bottle | | | 05000321/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000366/LER-1981-011-03, /03L-0:on 810204,nonrated Window Discovered in 3-h Rated Fire Wall.Caused by Design,Mfg & Const/Installation Error.Direct Conversion Reactor Study 81-48 Submitted & Fire Watch Established | /03L-0:on 810204,nonrated Window Discovered in 3-h Rated Fire Wall.Caused by Design,Mfg & Const/Installation Error.Direct Conversion Reactor Study 81-48 Submitted & Fire Watch Established | | | 05000366/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000321/LER-1981-012-03, /03L-0:on 810228,turbine Failed to Trip on Overspeed.Caused by Dried Lubrication Around Overspeed Tripping Mechanisms Causing Binding.Mechanism Disassembled, Cleaned,Relubricated & Reassembled | /03L-0:on 810228,turbine Failed to Trip on Overspeed.Caused by Dried Lubrication Around Overspeed Tripping Mechanisms Causing Binding.Mechanism Disassembled, Cleaned,Relubricated & Reassembled | | | 05000321/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000366/LER-1981-012-02, /02L-0:on 810224,during Surveillance Testing, Standby Liquid Control Pump B Failed to Start,Losing Squibb Valve B Continuity.Caused by Failure of Control Fuse in Circuit Breaker.Fuse Replaced | /02L-0:on 810224,during Surveillance Testing, Standby Liquid Control Pump B Failed to Start,Losing Squibb Valve B Continuity.Caused by Failure of Control Fuse in Circuit Breaker.Fuse Replaced | | | 05000366/LER-1981-012, Forwards LER 81-012/02L-0 | Forwards LER 81-012/02L-0 | | | 05000366/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000321/LER-1981-013-03, /03L-0:on 810228,HPCI Sys Was Declared Inoperable When Oil Line Near Rear Bearing Broke.Caused by Person Stepping on Oil Line & Turbine Vibration Finishing Separation.Line Repaired | /03L-0:on 810228,HPCI Sys Was Declared Inoperable When Oil Line Near Rear Bearing Broke.Caused by Person Stepping on Oil Line & Turbine Vibration Finishing Separation.Line Repaired | |
|