05000334/LER-1980-116-03, /03L-0:on 801217,degassifier a Recovery Heat Exchanger BR-E-12A2 Steam Leak Found to Be Cracked Weld. Cause Unknown.Exchanger Isolated & Drained.Weld Grounded Out & Temporary Mod to Seal Weld Performed

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/03L-0:on 801217,degassifier a Recovery Heat Exchanger BR-E-12A2 Steam Leak Found to Be Cracked Weld. Cause Unknown.Exchanger Isolated & Drained.Weld Grounded Out & Temporary Mod to Seal Weld Performed
ML20002D929
Person / Time
Site: Beaver Valley
Issue date: 01/15/1981
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20002D928 List:
References
LER-80-116-03L, LER-80-116-3L, NUDOCS 8101230471
Download: ML20002D929 (2)


LER-1980-116, /03L-0:on 801217,degassifier a Recovery Heat Exchanger BR-E-12A2 Steam Leak Found to Be Cracked Weld. Cause Unknown.Exchanger Isolated & Drained.Weld Grounded Out & Temporary Mod to Seal Weld Performed
Event date:
Report date:
3341980116R03 - NRC Website

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U. S. NUCLEA10 REGutATCGY COMMtSSl!N R AC FC".M 364

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40 68 OOCKET NUMSER nd 69 EVENT OATE la IS REPCRT Q ATE 80 EVENT DESCRIPTION ANO PROSA8LE CONSEQUENCES h ITTT1 I on 12/17/80, the source of a steam leak on the "A" necastrier Recovery lle.it l

ITTT1 I Eschancer (BR-E-12A21 was found to be a cracked weld. This abnormal decradation in l

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The health and l ITT71 I (BR-E-12A2] is reportable under Technical Specification 6.9.1.9.d.

101 s 1 I safety of the public was not jeopardized since ebe higher than normal background g l radiation levels in the auxiliary building Caused in part by this leak were still l

1o 171 l within the 10 CFR 20 MPC limits.

Isolating [BR-E-12A2] reduced these levels by l

l 1 o I a i I about one-third.

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44 4y 33 33 36 31 40 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lilOf1 The cause of the cracked weld is unknown. With the heat exchanger isolated and

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i building were I Q l drained. further releases of radioactive materials into the auxiliary iii2i i prevented. The weld was ground out and a temo'orary modification was made to seal l

IiI 3 I l the weld. A permanent modification is planned.

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Attachment To LER 80-Ilfs/03L Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 No further information is available or required to satisfy the reporting requirement.

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