05000324/LER-1980-108-03, /03L-0:on 801202,drywell Equipment Drain Leakage Integrator Indicating Five Gpm W/No Pumps Running.Caused by Drywell Equipment Drain Square Root Converter Being Out of Calibr.Converter Recalibr

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/03L-0:on 801202,drywell Equipment Drain Leakage Integrator Indicating Five Gpm W/No Pumps Running.Caused by Drywell Equipment Drain Square Root Converter Being Out of Calibr.Converter Recalibr
ML20002B990
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 12/31/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20002B988 List:
References
LER-80-108-03L, LER-80-108-3L, NUDOCS 8101070493
Download: ML20002B990 (1)


LER-1980-108, /03L-0:on 801202,drywell Equipment Drain Leakage Integrator Indicating Five Gpm W/No Pumps Running.Caused by Drywell Equipment Drain Square Root Converter Being Out of Calibr.Converter Recalibr
Event date:
Report date:
3241980108R03 - NRC Website

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S EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h the drvwell i

f5 TT1 i During normal plant surveillance, the control operator noticed that l

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The health and safety of the public was not affected by this event.

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33 converter was found to be out of calibration. [

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