ML19350D207

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IE Insp Rept 50-271/80-17 on 801020-1114.No Noncompliance Noted.Major Areas Inspected:Actions Taken on Previous Insp Findings,Response to Plant Events,Plant Operations & IE Bulletin Review
ML19350D207
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 02/20/1981
From: Collins S, Foley T, Martin T, Raymond W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML19350D206 List:
References
50-271-80-17, NUDOCS 8104140021
Download: ML19350D207 (54)


See also: IR 05000271/1980017

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O.S. NUCLEAR REGULATORY COMMISSION

50271-800107

0FFICE OF INSPECTION AND ENFORCEMENT

50271-800630

50271-801017

Region I

50271-801007

50271-801013

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Report No.

80-17

50271-800908

50271-800903

Docket No.

50-271

50271-800904

50271-800114

License No.

DPR-28

Priority

Category

C

50271-800731

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50271-800815

Licensee:

Vermont Yankee Nuclear Power Corporation

50271-800417

50271-801027

1671 Worcester Road

50271-801014

50271-801014

Framingham, Massachusetts 01701

Facility Name:

Vermont Yankee

Inspection at:

Vernon, Vermont

Inspection conducted.: October 20-November 14, 1980

Inspectors:

.

M/btr

d' # # # /./ M

/ 3d

/

W. J. Raymona

enior/desicent inspector

date sighed

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INIBl

S /J. Gollins Resident Inspector

~ da te' igned

/ 3oM/

/IW

/,

M

T. F.

oley,

esid r/t Inspect 6r-

date signed

Approved by:

_ /&t4mg

g

.M

/

Section Nc'.f, Ch{pf, Reactor Projects

date ' signed

. T. Mar,ti

3, R0&NS Branch

Insoection Summary:

Inspection on October 20-November 14, 1980 (Report No. 50-271/80-17)

Areas Inspected: Routine, onsite, regular and backshift inspection by the Resident

Inspectors.

Areas inspected included: Actions Taken on Previous Inspection Findings;

Review of Plant Operations, including:

Instrumentation and Alarms, Shift Manning,

Radiation Protection Controls, Plant Housekeeping, Fire Protection / Prevention, Con-

trol of Equipment, and Shift Logs and Operating Records; System Operational Safety

Verification; Licensee Staffing; Licensee Reporting; IE Bulletin Review; Witness of

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surveillance Tests; Response to Plant' Events; Observations of Physical Security;

Plant Maintenance, Modifications, and Refueling Operations; and inspector Followup

on Regional Requests.

The inspection involved 124 inspector hours onsite by three

Resident Inspectors.

Results: No items of noncompliance were identified during this inspection.

Region I Form 12

(Rev. April 77)

8104140Q &\\

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DETAILS

1.

Persons Contacted

The below listed technical and supervisory level personnel were among those

contacted:

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Mr. L. Anson, Plant Training Supervisor

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Mr. R. Branch, Assistant Operations Supervisor

Mr. P. Donnelly, Instrument and Control Supervisor

Mr. D. Girroir, Technical Assistant

Mr. S. Jefferson, Reactor Engineering Supervisor

Mr. B. N. Leach, Chemistry and Health Physics Department

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Mr. M. Lyster, Operations Supervisor

Mr. W. Murphy, Plant Superintendent

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Mr. J. Pelletier, Assistant Plant Superintendent

Mr. D. Reid, Engineering Support Supervisor

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Mr. S. Vekasy, Technical Assistant

The inspectors also interviewed other licensee employees during the inspec-

tion, including members of the Operations, Health Physics, Instrument and

Control Maintenance, Security and General Office staffs, and Refueling

Outage contractor personnel.

2.

Action Taken on Previous Inspection Findings

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(Closed) Noncompliance (50-271/80-11-01): Manber of security force not

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qualified in one area. The inspector reviewed Licensee response to subject

item and NRC reply from Region I Safeguards Branch to Vermont Yankee Nuclear

Power Corporation, dated October 29, 1980.

Based on the content of the

above correspondence the subject item has been withdrawn. This item is

considered resolved.

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(Closed) Noncompliance (50-271/80-11-04):

Communications device not

tested at required frequency.

The inspector reviewed Licensee response

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to subject item and NRC reply from Region I Safeguards Branch to Vermont

Yankee Nuclear Power Corporation, dated October 29, 1980. Based on the

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content of the above correspondence the subject item has been withdrawn.

This item is considered resolved.

(Closed) Noncompliance (50-271/80-11-02): Security procedure not consistent

with security plan. The inspector reviewed Revision 1 to the Physical

Security Plan for Vermont Yankee Nuclear Power Station, Section 13.7,

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Records Retention and confirmed that the inconsistency between Security

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Procedure No. 0941, Revision 1, dated June 6, 1980 and the Plan has been

corrected by a revision to the security plan which states that all security

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records will be retained in accordance with Plant Procedures.

This item is

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closed.

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(Closed) Noncompliance (50-271/80-11-03):

Isolation zone not maintained

as required. The inspector reviewed Licensee response to subject item

and noted the obstructions in question were removed prior to the conclusion

of the inspection.

Discussions with Security Department Supervision and

onshift personnel indicate that an internal system of tracking security

related work items has been implemented with daily reviews of outstanding

items perfomed by supervision. The inspector toured the isolation zone

on November 11, 1980, and found the area clear and free from obstructions

as required by the Vermont Yankee Nuclear Power Station Physical Security

Plan. This item is closed.

(Closed) Noncompliance (50-271/80-11-05):

Door alarm not tested as required.

The inspector reviewed Revision 1 to the Vermont Yankee Nuclear Power Station

Physical Security Plan, Section 12.2, Alams and Annunciators and confirmed

that the Plan now addresses a revised testing program for the subject door.

Discussions with onshift security supervisory personnel indicate that testing

of the door is logged in the Intrusion Alarm Log upon completion. This item

is closed.

(Closed) Inspector Follow Item (50-271/80-02-01):

Incorporation of an ADS

accumulator air supply leak test into the licensee's periodic test program.

The inspector verified that procedure VY OP 4028, ADS Air Supply Accumulator

Surveillance, has been scheduled to be perfomed during the 1980 Refueling

Outage currently in progress.

The inspector also verified that the Licensee's

Master Surveillance Schedule has been updated per VY AP 4000, Revision 6,

Surveillance Testing Control, to provide for periodic performance of the ADS

accumulator air supply leak test. This item is considered closed.

(Closed) Inspector Follow Item (50-271/80-10-04):

Revision of AP 0503 to

incorporate requirement for a radiation work permit (RWP) in specified con-

taminated areas.

The inspector verified that Revision 6 to AP 0503,

Establishing and Posting Controlled Areas, dated October 16, 1980, has

been issued incorporating the following requirements into procedure section 6,

Contaminated Area:

If the area is not posted with any condition which re-

quires a RWP but contamination levels are greater than 10,000 dpm/100cm2

in the general area, either have the area decontaminated immediately or

post it, RWP required for entry. This item is considered closed.

(0 pen) Inspector Follow Item (50-271/80-15-07):

Environmental Qualification

of Stem Mounted Limit Switches used on Containment Isolation Valves (IEB 78-04).

The inspector reviewed Technical Specification Tables 4.7.2a and 4.7.2b in

conjunction with various plant system flow diagrams to identify the type,

location and functional requirements of containment isolatien valves subject

to PCIS control. Aside from the four inboard main steam isolation valves

(for which the licensee has documentation to establish environmental

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qualification), only one other air operated CIV was found located inside the

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drywell. Valve V2-39 is an air operated (ASCO) valve in the recirculation

loop sample line.

The inspector observed V2-39 during a drywell tour on

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October 24, 1980 and noted that it did not contain a stem mounted limit

switch for position indication.

Based on this review, the inspector identified

no discrepancies with the licensee's position that all applicable containment

isolation valves with stem mounted limit switches were environmentally

qualified. The inspector had no further comments in regard to qualification

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of components within the scope of discussions with the licensee on this item

(open NRC staff items on other environmental qualification issues are

docume.nted elsewhere). This item remains open, however, pending NRC review

of the licensee's IEB 79-01B November,1980 submittal to verify that qualifica-

tion of stem mounted limit switches is addressed in the information provided

to NRC:NRR.

(Closed) Inspector Follow Item (50-271/80-15-13):

Jet Pump Beam Replacement.

The inspector reviewed licensee procedure OP 1416, Revision 1, Replacement of

Jet Pump Hold Down Beams, October 16, 1980, which was developed by the licensec

to replace the cracked beam on jet pump No. 8

The procedure provided detailed

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instructions for jet pump beam removal; jet pump tensioning; keeper installation,

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weld qualification and welding; and, visual verification of proper placement.

The repair plan involved replacing the BWR/3 type hold down beam with a BWR/4

type which is designed for increased strength, heftier fabrication, and lower

stress levels, and is thus less susceptible to an intergrannular stress

corrosion cracking mechanism.

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The inspector reviewed licensee preparation for the jet pump beam replacement

on October 13, 1980, including the verification of selected prerequisites.

The jet pump beam was subsequently replaced, as documented in the licensee's

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followup report to the NRC, LER 80-33/1T.

The inspector reviewed LER 80-33

to verify that it was complete and accurate in the description of tile event.

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The inspector had no further questions on this item. This item is closed.

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(Closed) Inspector Follow Item (50-271/80-15-14):

Core Spray Sparger Crack

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Repair.

The following references document actions taken by the licenseeeon

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core spray (CS) sparger junction box 'C' and NRC staff review of these actions:

+ LER 80-32/1T dated October 28, 1980

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+ VY Letter WVY 80-164, Results of Core Spray Sparger Inspection

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NRC Staff Meeting Summary dated November 5, 1980, for a meeting held with

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the licensee and his consultants on October 31, 1980.

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+ NRC Region I Inspection Report 50-271/80-16

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Following a complete visual inspection of both core spray headers, no

cracks in addition to the one on junction box 'C' was identified.

NRC

Resident and Regional inspectors also reviewed video tapes of the sparger

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inspections on a sampling basis; this review identified no findings different

sfrom the licensee's (see also NRC Region I Inspection Report 50-271/80-16).

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The crack occurred on the end cap of the 'C' junction box, with visual indi-

cations for approximately 1800 on a 2.5 inch diameter circle surrounding a

1 inch plug welded in the center of the end cap. An air test of the subject

sparger showed that the crack was not through wall, as evidenced by a lack

of air bubbles with the header under pressure.

Licensee review of sparger fabrication records showed that the end caps

were fabricated from type 304 stainless steel material with a carbon content

of 0.052%. The sparger arms were fabricated with 304 stainless steel with a

0.04% carbon content. The crack occurred along the heat affected zone

created during the welding of one inch diameter inspection port plug.

It

is probable that the sensitization of the end cap material and residual

shrinkage stresses associated with the welding, together with sparger

environmental conditions, all led to the crack being formed through the

intergrannular stress corrosion mechanism. Although no other crack indi-

cations were observed on the other sparger junctions boxes, which contain

similar plugs, it must be assumed that the other junction boxes are sus-

ceptible to the came corrosion mechanism. The lack of crack indications on

the sparger arms is likely attributable to the lower carbon content of the

fabrication material. Future licensee inspections during refueling outages

of the CS spargers and junction boxes in accordance with IEB 80-13 require-

men M will serve to monitor sparger integrity.

Since the magnitude of the plug weld /end cap residual stresses could not

be accurately determined, the licensee conservatively assumed that the

observed crack could propagate and create a 2.5 inch diameter hole in the

end cap (i.e., the welded plug is assumed to detach from the end cap).

To limit leakage flow and retain the inspection port plug should the crack

propagate to failure, the licensee procurred and installed a stainless steel

clamp device on the junction box and adjacent piping.

The clamp was designed

also to minimize the potential for loose parts to enter into the reactor

coolant system. The inspector observed that the clamp was installed on the

'C' junction box on November 2, 1980.

Further licensee evaluations of crack repair and core spray sparger integrity

also included considerations for loose parts generation, the potential for

sparger blockage and core spray /ECCS performance.

These matters were dis-

cussed with the NRC staff during a meeting in NRC:HQ on October 31, 1980.

Based on the results of this meeting and supported by the licensee's

December 1, 1980 submittal to the staff, the NRC staff concluded that

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resumption of reactor operation with the clamp in place would be acceptable.

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The inspector also reviewed LER 80-32 and found that it was complete and

accurately described the event.

The inspector had no further comments in

regard to core spray sparger repair.

This item is closed.

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(0 pen) Unresolved Item (50-271/80-16-02):

Loose Parts Analysis for Core

Spray Sparger Clamp. The integrity and acceptability of the tac welds

on the core spray sparger clamp locking cups was evaluated by the

licensee. The results of the licensee's evaluation were presented to

the NRC staff during a meeting on October 31, 1980, and are documented

in the licensee's December 1,1980 submittal to the NRC.

Additionally,

a loose parts analysis was performed for the parts in question and, as

reported in the December 1, 1980 submittal, no unacceptable consequences

were identified.

This item will remain open, however, pending inspector

review of the analysis on a subsequent inspection.

(Closed) Unresolved Item (50-271/80-15-02):

Penetration Box Closure.

During an inspection tour inside the drywell on November 5, 1980, the

inspector noted that the covers for the penetration boxes in question

had been returned to a configuration in agreement with Ebasco Drawing

G-191377, including installation of all cover screws, proper mating of

gaskets at box corners and proper gasket sealing.

This item is closed.

(0 pen) Unresolved Item (50-271/80-15-06):

Broken Flexible Conduit.

During

an inspection tour on November 5,1980, the inspector noted that the

flexible conduit on M0-10-17 had been repaired.

Disucssions with the

plant Maintenance Supervisor indicate that untennirated wires in penetra-

tion connection boxes X101D and X105A had been secured.

However, the

inspector noted that flexible conduit on valve M0-23-15 had not been

repaired.

This item remains unresolved pending completion of licensee

action on M0-23-15.

(0 pen) Inspector Follow Item (50-271/80-15-14):

Revised Plant Emergency

Procedures, IAL 80-34. The inspector was informed that, subsequent to his

previous review in this area (see NRC Region I Inspection Report 50-271/

80-15, paragraph 14), the emergency operating proceduces had undergone

additional VY staff review and further revision.

Th3 procedures were

still in draft form awaiting final PORC reviu and approval prior to

issuance. The inspector reviewed the new procedure drafts (see paragraph

14 of IR 80-15 for listing) to verify that:

procedure "Immediate Action" and " Followup Action" sections directed

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the operator to the emergency plan implementing procedures;

the emergency plan implementing procedures referenced by each E0P

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was appropriate, based on a review of FSAR Section 14.5 and 14.6,

with considerations given to projected offsite and site boundary

doses; and,

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all E0Ps concerning events with the potential for offsite radiological

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effects were included in the listing of procedures addressed under

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IAL 80-34 requirements.

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The inspector noted that one procedure, OP 3101, Loss of Normal Power,

was initially revised into the emergency plan implementing procedure

format, and then left unchanged from the original format in the second

draft. The reasons for these changes were discussed with a licensee

representative; the inspector acknowledged that revision of OP 3101 to

incorporate the emergency plan implementing format did not appear to

be necessary.

Inspector comments on procedures OP 3115 and 3124 were

discussed with the licensee and addressed in the final E0P drafts.

The inspector stated at the exit interview that the procedures, if approved

as written in the second draft, would meet the IAL 80-34 requirements.

The

licensee stated that the procedures would be issued and operator traiaing

on the revised procedures would occur during the week of November 17, 1980.

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This item remains open pending issuance of approved procedures and completion

of operator training.

Additional inspector review in the emergency planning

area is discussed in paragraph 13 of this report.

3.

Review of Plant Operations - Plant Inspection

The inspector reviewed plant operations through direct inspection and

observation throughout the reporting period. Activities in progress

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consisted of refueling operations,

a.

Instrumentation

Control Room process instruments were observed for correlation between

channels and for conformance with Technical Specification requirements.

No unacceptable canditions were identified.

b.

Annunciator Alarms

The inspector observed various alarm conditions which had been received

and acknowledged. These conditions were discussed with shift personnel

who were knowledgeable of the alarms and actions required.

During plant

inspections, the inspector observed the condition of equipment associated

with various alarms. No unacceptable conditions were identified andr

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except as noted below the inspector had no further comments in this area.

c.

Shift Manning

The operating shifts were observed to be staffed to meet the refuelie.g

operations requirements of Technical Specifications, Section 6, both

to the number and type of licenses.

Control room and shift manning

were observed to be in conformance with Technical Specifications and

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site administrative procedures.

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d.

Radiation Prcr.ection Controls

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Radiation p.otection control areas were inspected.

Radiation Work

Permits in use were reviewed, and compliance with those documents,

as to protectivs clothing and required monitoring instruments, was

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inspected.

Proper posting of radiation and high radiation areas was

reviewed in addition to verifying requirements for wearing of

appropriate personal monitoring devices.

Except as noted below, the inspector had no further comments in this

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area.

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Storage of Solid Radioactive Waste

On November 4,1980, the inspector interviewed Vermont Yankee Health

Physics supervisory personnel in response to a questionnaire concerning

the licensee's storage of radioactive waste,

The following information

was forwarded to Region I personnel at the request of the Division

of Fuel Facilities and Material Safety Inspection:

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Vermont Yankee presently ships the majority of its low-level

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waste to Barnwe11, S. C. for disposal.

In the past, they have

shipped to Beatty, NV and Richland, WAs, but very infrequently

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If the above low-level waste sites were closed the licensee

estimates it would take approximately 12 months to reach the

full capacity of existing onsite storage

The difference in rate of accumulation of low-level solid

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radioactive waste between " normal operation" and " shutdown"

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condition is minimal.

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The inspector had no further questions in this area.

Equipment Removal / Decontamination

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The inspector observed work in progress on November 13, 1980, near

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the Southeast corner of the reactor building 252 foot elevation to

remove / decontaminate equipment from the torus area.

Controls esta-

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blished for equipment separation, surveying and removal were observed

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and discussed with HP personnel directing the work.

Confinnatory

radiation survey measurements were made by the inspector.

No items of noncompliance were identified.

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e.

Plant Housekeeping Controls

Storage of material and components was observed with respect to

prevention of fire and safety hazards.

Plant housekeeping was

evaluated with respect to controlling the spread of surface and

airborne contamination. There were no unacceptable conditions

identified,

f.

Fire Protection / Prevention

The inspector examined the conditon of selected pieces of fire

fighting equipment. Combustible materials were being controlled

and were not found near vital areas.

g.

Control of Equipment

During plant inspections, selected equipment under safety tag

control was examined.

Equipment conditions were consistent with

information in plant control logs.

h.

Shift Logs and Operating Records

During the inspection period, the inspector reviewed on a sampling

basis the following logs and records for the period of Octobe r 20-

November 14, 1980:

Shift Supervisor's Log

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Shutdown Control Operator's Round Shees

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Auxiliary Operator's Round Sheet

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Shutdown Shift Turnover Data and Checklist

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Night Order Book

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The logs and records were reviewed to verify that entries are pro-

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perly made; entries involving abnonnal conditions provide sufficient

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detail to communicate equipment status, deficiencies, corrective

action, restoration and testing; records are being reviewed by manage-

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ment; operating orders do not conflict with the Technical Specifications;

logs and incident reports detail no violations of Technical Specifica-

tions or reporting requirements; logs and records are maintained in

accordance with Technical Specification and Administrative Control

Procedure requirements.

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1.

Switching and Tagging Order File Review

The Switching and Tagging Order File was periodically reviewed for

a determination of the types of equipment affected, duration of

temporary system alteration and impact on Technical Specification

LC0 requirements,

None of the tagging orders reviewed were deemed

to constitute a LC0 degradation nor an item requiring a 10 CFR 50.59

review.

No items of noncompliance were identified.

4.

System Operational Safety Verification

a.

SLC System Return to Operation

A detailed review was conducted of the Standby Liquid Control System

(SLC) following completion of system maintenance to verify the system

was properly aligned and fully operational in the standby mode.

Review

of the above system included the following:

(1) Verification that plant valve lineup procedures were consistent

with plant system drawings.

Plant procedure OP 2114 and drawing

G-191171 were used to verify proper lineups for the SLC system.

(2) Walkdown of system by inspector to verify positions of accessible

valves in the flow path were correct by visual observation of the

valve or its remote position indication.

(3) Visual inspection of major components for leakage, proper lubrica-

tion, general condition and other conditions that might prevent

fulfillment of their functional requirements.

(4) Verification by observation that instrumentation essential to

system actuation and performance was operational.

No items of noncompliance were identified.

b.

Torus Closecut Inspection

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The inspector accompanied a licensee inspection team during a torus

closecut inspection on November 13, 1980, to review torus work com-

pleted during the outage and to ascertain torus readiness for a return

to operation.

Items reviewed on a sampling basis included the four

T-Quenchers installed on the safety relief valve discharge; installed

vent header deflectors; installed downcomer ties; rerouted RHR return

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lines; and, thermocouple and differential pressure instrumentation

installed in torus bay No.' 10 in preparation for future torus /SRV

testing. The inspector noted that housekeeping and cleanliness in

tha torus interior was exceptionally good. The inspector also

noted that grating on the torus interior catwalk had been removed.

No inadequacies were identified. The inspector had no further

comments in this area.

5.

Licensee Staffing

The following change,s in licensee personnel were made:

T. Watson was hired as the Operations Training Assistant.

6.

In-Office Review of Licensee Event Reports

The licensee event reports (LERs) listed below were reviewed in the NRC

Resident / Regional Office.

The reports were reviewed to detemine whether:

the information provided was clear in the description of the event and

identification of safety significance; the event cause was identified and

corrective actions taken (or planned) were appropriate; the report satis-

fied requirements with respect to information provided and timeliness of

submittal; and, on-site followup was warranted. Those reports annotated

with an asterisk (*) concern events that occurred when the inspector was

onsite and inspector review / evaluation of the event is documented elsewhere,

in this or other inspection reports.

LERs 80-03, 80-21, 80-36, 80-35, 80-34, 80-28, 80-26, and *80-27.

No items of noncompliance were identified.

7.

Review of Periodic and Special Reports

Upon receipt, periodic and special reports submitted by the licensee

pursuant to Technical Specification 6.7 and Environmental Technical Specification 5.4 were reviewed by the inspector to verify that reporting

requirements had been met. The following reports were reviewed:

Monthly Operating Reports for the months of September and October, 1980.

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No unacceptable conditions were identified,

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8.

IE Bulletin Review and Followup

Licensee responses and actions taken for the IE Bulletins listed below

were reviewed to verify that:

the bulletins were received onsite and reviewed for applicability

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to the facility;

bulletin action items, if applicable, and-identified problems were

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appropriately dispositioned;

corrective actions taken, or planned, were appropriate; and,

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responses to the NRC were accurate and within the time period

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specified in the bulletin.

Inspector followup on selected bulletins is summarized below. The

inspector had no further comment on the subject bulletins, except

as indicated below.

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a.

IEB 80-01, Operability of ADS Valve Pneumatic Supply, dated

January 14, 1980

References:

(1) VY Inspection Report 50-271/80-02, dated

April 2,1980

IEB 80-01 required actions be taken by licensees to verify continued

operability of the ADS valve pneumatic supply. A previous inspection

documented by reference (1) verified licensee actions complete with

the exception of an outstanding inspector follow item to verify

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incorporation of an ADS accumulator air supply leak test into the

licensee's periodic test program. This follow item is complete ac

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noted in section 2 of this report.

b.

IEB 80-20, Failures of Westinshouse Type W-2 Spring Return to Neutral

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Control Switches, dated July 11, 1980

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The inspector reviewed licensee response dated August 22, 1980, which

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provided all information requested by the bulletin in that Vermont

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Yankee does not utilize the Westinghouse Type W-2 Spring Return to

Neutral Control Switch in any safety related system.

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No items of noncompliance with bulletin requirements were identified,

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c.

IEB 80-19, Failure of Mercury-Wetted Matrix Relays in Reactor

Protective Systems of Operating Nuclear Power Plants, dated

August 15. 1980

The' inspector reviewed licensee response WVY 80-119 dated

August 22, 1980. The inspector verified that subject IEB

requirements have been completed in that the licensee reported

that Vermont Yankee does not utilize Mercury-Wetted Matrix

relays in its reactor protection system.

No itens of noncompliance with bulletin requirements were

identified.

c.

IEB 80-09, Hydramotor Actuator Deficiencies, dated April 17, 1980

The inspector reviewed licensee response WVY 80-89 dated June 30, 1980.

The inspe-tor verified that subject IEB requirements have been completed

in that tha licensee reported that Vermont Yankee does not presently

utilize or plan to use the hydramotor actuators in any system.

No items of noncompliance with bull.etin requirements were identified.

9.

Observations of Physical Security

The inspector made observations, witnessed and/or verified during regular

and offshift hours that selected aspects of plant physical security were

in accordance with regulatory requirements, the physical security plan

and approved procedures.

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a.

Physical Protection Security Organization

observations indicated that a full time member of the security

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organization with authority to direct physical security actions

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was present as required.

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manning of all shifts on various days was observed to be as

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required.

b.

Access Control

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Observations of the following items were made:

-

identification, authorization and badging

--

access control searches, including the use of compensatory

i

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measures during periods when equipment was inoperable

j

escorting.

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c,.

hsicalBarriers

_

selected barriers in the protected area and vital area were

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!

observed and random monitoring or isolation zones was per-

formed. Observation of vehicle searches were made.

No iteras of noncompliance were identified.

10. Response to Plant Events

The inspectors responded to events and Prompt Reportable occurrences that

occurred during the inspection to observe / review the licensee's response to

the events and to verify continued safe operation of the reactor in accordance

with the Technical Specifications and regulatory requirements. Some or all of

the following items, as applicable, were considered during the inspector's

review of operational events:

observations of plant parameters and systems important to safety

--

to confirm operation within nonnal operational limits;

description of event, including cause, systems involved, safety

--

significance, facility status and status of engineered safety

features equipment;

verification of conformance to Technical Specification LC0 require-

--

ments;

determination that root causal factors were identified and that

--

corrective actions, taken or planned, were appropriate to correct

the cause;

verification that corrective action taken was appropriate to

--

prevent recurrence;

determination whether the event involved operation of the facility

--

in a manner which constituted an unreviewed safety question as

defined in 10 CFR 50.59 (a) (2), or in such a manner as to repre-

sent an unusual hazard to health and safety of the public and

environment;

determination whether the event involved continued operation of the

--

facility in violation of regulatory requirements or license

conditions; and,

evaluation of whether applicable reporting requirements were met.

--

4

Items reviewed during this inspection are summarized below.

--

_

.

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15

l

a.

Reactor Water Cleunup System Leakage and Repair

Licenseeinspection of reactor water cleanup system piping inside the

drywell was performed during the 1980 refueling outage as part of the

routine inservice inspection (ISI) program.

During the ISI inspection,

certain defects in excess of code allowable were identified. The

defects initially identified were located in 4 inch diameter, schedule

80 stainless steel piping downstream of the inboard containment isolation

valve V12-15 and were not through wall.

Details of these initial findings,

as well as NRC review in the area, are documented in NRC Region I Inspec-

tion Report 50-271/80-16.

As a result of the initial findings, the licensee extended the scope

of piping examinations to include sections upstream of valve V12-15

to the RWCU system tap off point from the 20 inch diameter shutdown

cooling suction drop line. On November 2, 1960, the licensee reported

to the NRC Resident Office that additional, through wall leaks were

identified in the upstream piping. The through wall defects were

located on the RHR to RWCU system sweepolet and at the sweepolet to

RWCU pipe weld interface. The leaks were located upstream of manual

isolation valve V12-46 and were thus non-isolable.

Leakage from the

sweepolet was characterized as minimal to the extent that immediate

corrective action was not necessary. Based on these findings, the

licensee extended the scope of RWCU system pipe replacement to include

the schedule 120 piping and the sweepolet. Additional NRC review of

the RWCU pipe replacement work was performed during a special inspec-

tion by NRC Region I personnel and is documented in NRC Region I

Inspection Report 50-271/80-20.

Independent observations were made by the inspector and discussions

were held with licensee personnel to review the operational considera-

tions of the RWCU system leaks.

Inspector findings in this review

are summarized in the following areas.

(1) RWCU System Leakage

The inspector observed the sweepolet defects during a drywell

entry on November 5, 1980. With the piping under about 35 psi

pressure (due to reactor vessel level elevation head), the

inspector noted that one defect (sweepolet body) was dry and

the second defect (sweepolet to pipe interface) was weeping

slightly. The weeping could be characterized as moisture that

could be wiped away with a cloth, and then several seconds

would elaspe before new moisture would appear.

The defect on

the sweepolet body, although dry, showed signs of previous

leakage /weepage, assumed to occur under higher system pressures.

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The location of the defect on the sweepolet was in a high

stress area. The defect on the sweepolet to pipe interface

was located in the pipe side of the weld in the heat affected

zone. This defect is characterized as a pinhole sized exterior-

flaw about 1 mm in diameter. The inspector noted that the amount

of leakage with the reactor system shutdown did not constitute

an immediate safety concern prior to development and implementa-

tion of a repair plan.

'

The inspector also considered what the pre-shutdown leakage

from the defects could have been with the reactor system under

pressure. Although this leakage could not be quantified by the

,

inspector, the inspector noted through daily review of drywell

leakage monitoring systems that no appreciable unidentified

j

leakage was recorded during pre-shutdown operations (reference:

NRC Region I Inspection Reports 50-271/80-08,80-10,80-13).

-

'

4

The inspector also noted the location of the sweepolet with

'

respect to the adjacent drywell wall and drywell to torus vents

located on the 238 foot elevation. The inspector concluded that

the probability for sweepolet leakage to flow into the drywell/

3

torus vents, and thereby(bypass the drywell leakage monitoring

'

systems, was negligible reference:

NRC Region I Inspection

Report 50-271/80-08).

Based on the above, the inspector con-

cluded that pre-shutdown leakage from the RWCU system was very

small.

The inspector had no further comments on this item.

(2)

Reactor Vessel Cleanup and Core Discharge

'

Upon discovery of the RWCU leakage, the licensee isolated the

3

RWCU system to the extent possible prior to offloading the

core and draining the reactor vessel and affected piping. A

temporary suction line was installed to the RWCU pumps to pro-

vide for continued reactor vessel cleaning during the repairs

and to maintain refueling pool clarity for fuel movement opera-

tions. The inspector observed fuel pool conditions during sub-

sequent operations and noted that pool clarity was very good.

The licensee considered alternate methods for repair of the

!

non-isolable portions of the RWCU line, including the use of

inflatable dams to be installed on the reactor vessel side of

.

the leak; and, total core off load and draining 'of the reactor

i

vessel and attached piping to below the repair area.

The latter

approach was chosen and procedure OP 1121.01, Preparation of the

,

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. , - - . _ . . , , _ _ , _ ~ , .

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.,,--

, ,-., , _ ~ - ,

,~

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17

Reactor Yessel for the RWCU System Repair, was prepared to

govern the evolution.

The inspector discussed the overall

aspects of the draining operation with licer.see personnel and

noted that a temporary level measuring system would be employed

to provide inner-shroud level indications.

Removal of all fuel from the reactor vessel started on

November 6,1980 and was completed on November 11, 1980.

Paragraph 12 of this report discusses inspector review of

core discharge operations.

Subsequent draining of the reactor

vessel was periodically observed by the inspectors.

The inspector had no further comments on.this item.

(3) Radiological Considerations

Radiological aspects of the core discharge / vessel drain evolution

were discussed with licensee personnel.

Licensee review of the

job included considerations for:

+

the need for special controls at the Reactor Building

345 foot elevation to restridt personnel access and to

minimize / monitor airborne activity levels with the reactor

vessel drained;

+

identification of the stellite balls on control rods nearest

the cleanup repair site (East side of reactor) as presenting

the highest source term with the reactor vessel drained.

Several peripheral control rods near the "A" recirculation

nozzle outlet were moved to the fully inserted position to

reduce gamma streaming through the recirculation nozzle and

to move the stellite balls out of the verticle plane of the

work area; and,

+

use of lead blanket shielding between the reactor vessel

and the repair area to reduce background radiation levels.

Independent radiation surveys of the work site made by the

inspector prior to draining the vessel showed general area

l

radiation levels ranging from 0.5 to 1.0 R/hr, with " hot

j

l

spots" on contact with nearby piping up to 1.5 R/hr.

Inspector surveys of the work site after installation of

lead shielding (vessel drained) showed the radiation levels

had been reduced to 0.2-0.3 R/hr.

1

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,.

.

The inspector had no further comment on this item at the

present.

Review of personnel exposure control for RWCU system

repairs will be conducted as part of the routine inspection

program on subsequent inspections.

(4) Metallurgical Analyses / Reporting

'

i

The licensee submitted LER 80-37/1T in accordance with

Technical Specification 6.7.B.1 to document his ISI inspection

'

findings and describe planned corrective actions. The report

i

was reviewed by the inspector and was found to accurately re-

flect the event circumstances.

Part of the licensee's correc-

,

tive plan, as described in the November 10, 1980, LER letter,

was to replace the existing RWCU piping with conforming

material per NUREG 0313, Revision 1, from the RHR branch

connection to the outboard isolation valve. Material con-

fonning to NUREG 0313 contains controlled quantities of carbon

and is less susceptible to stress corrosion cracking mechanisms.

Inspector review of the ISI findings, with consultation from

NRC Regional and HQ staff, concluded that the VY actions were

appropriate, in that the nature, location and service environ-

ment of the identified defects presented strong evidence in

support of intergrannular stress corrosion cracking as the

cause mechanism for the majority of the cracks.

However,

ultimate determination of the cause for the identified cracks

rests on the results of metallurgical analysis of crack

specimens.

The licensee's November 10, 1980 letter to the NRC

committed to reporting the results of the metallurgical

analyses in an LER supplement. The results are expected to

be available around the first of February,1981.

This item is open pending NRC review of the metallurgical

analyses report, and a determination of what further corrective

actions, if any, are considered necessary (IFI 50-271/80-17-01).

The inspector had no further comments in this area at the present.

Inspector review of subsequent licensee actions to evaluate / repair

RWCU system cracks will be followed on subsequent inspections.

,

,

b.

Penetration Fire Barriers

i

On November 11, 1980, the NRC Region I Office received a letter

(dated November 3, 1980) from Chemtrol Corporation of Texas which

questioned whether penetration fire barrier seals installed at the

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~ _ , , . . - . . - _ . _ _ _ _ - . _ . - . . , , , - -

.-.

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__

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19

VY plant conformed to applicable industry standards.

The inspector

reviewed the information presented by the Chemtrol letter dated

November 3, 1980, interviewed licensee personnel and reviewed

facility records and penetration seal installation drawings to

determine whether the concerns raised were applicable to the

facility and if so, their significance.- Findings are sumarized

below.

l

(1) References

'

(a) Chemtrol Corporation letter to NRC Region I dated

November 3, 1980

(b) Chemtrol Corporation letter to NRC Region I dated

November 14, 1980

.

(c) ANI Penetration Seal Acceptance letter dated July 2,1979

(d) Chemtrol Corporation letter to GE Company dated

,

February 27, 1980

j

(e) Chemtrol Test Procedure CTP-0203 dated October 22, 1979

(f) ANI letter to Chemtrol Corporation dated January 31, 1980

!

,

'

(g) Portland Cement Association Test Report for CTP-0205

dated October 27, 1980

(h) Chemtrol Corporation Drawing No. A-114, Revision 1,

dated January 22, 1980

,

.

(1) Chemtrol Test Procedure CTP-0205 dated January 23, 1980

4-

l

(j) NRC Staff letter to VYNPC dated October 24, 1980

(2) Background

'

!

Fire barrier seals are used to seal electrical penetrations between

vital plant areas to stop/ impede the spread of a fire from one

l

!

area to the next.

Industry / regulatory standards for fire barrier

seals require that the barriers be rated for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />; that is,

.

the barrier must remain intact for 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> when subjected to a

fire of specified intensity. The fire barrier seals act in

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20

conjunction with other fire suppression systems (such as

water sprinkler, CO2 deluge) to provide protection against

loss of safety system function caused by fire.

Following the

Browns Ferry fire in 1975, all nuclear power plants were re-

quired to upgrade fire prevention / detection / suppression

capabilities, to include the installation of penetration

fire barrier seals.

The Chemtrol Corporation was contracted by VYNPC to install

fire barrier seals at the VY plar.t in the Fall of 1979. Fire

barrier seals were installed in a number of " configuration

types" using either of two types of silicone elastomer

_GE RTV 6428 and GE 850 RTV). All installation types at VY,

(.except one, received acceptance notifications by American

Nuclear Insurers as approved 3-hour fire rating configurations.

One configuration, labeled " Typical H", did not have the ANI

approval at the time of installation but was scheduled for

acceptance testing. Submittal of information on the Typical

H configuration to the NRC for review was recognized as an out-

standing item in an NRC:NRR October 24, 1980 letter to VY.

Chemtrol Corporation scheduled the perfomance of three

separate test with an independent laboratory in October, 1980.

Testing of materials CT-19/GE 850 RTV Silicone Foam and

CT-800/GE 6428 RTV Silicone Elastomer were to be tested under

configurations specified in test procedures CTP-0204, CTP-0205

and Typical Drawing "H".

Testing completed on October 20, 1980,

under CTP-0204 using the 850 RTV Silicone Foam was completed

satisfactorily. Testing of th e 6428 RTV Silicone Elastomer

was done on October 27, 1980, with unacceptable results.

The

test was terminated as a failure after one hour and thrity-one

minutes.

Based on the performance of the 6428 RTV Silicone

Elastomer in the CTP-0205 configuration, Chemtrol decided not

to test the Typical H configuration.

In that the Chemtrol

test results were at odds with previous tests which were

successful to qualify the 6428 material, Chemtrol initiated

steps to analyze samples of tested material to detemine

whether a change in chemical formulation had occurred.

The

results from this analysis were not yet available as of

November 30, 1980.

The October 27, 1980 test results prompted concern within the

(

Chemtrol Corporation over the use of the 6428 RTV Silicone

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21

Elastomer in the VY installations.

In a letter dated

November 3,1980, Chemtrol estimated that 75% of the penetra-

tion seals at VY use the 6428 RTV Silicone Elastomer.

This

estimated value was lowered to 27% in a November 14, 1980

letter to the NRC.

(3) Findings

,

Through discussions with licensee personnel and tours of the

facility, the inspector noted that the 6428 RTV Silicone

Elastomer was installed at the plant and, for the most part,

associated with cable penetrations in one area. Most 6428 RTV

Silicone Elastomer in use at VY is installed on two banks of

cable tray penetrations that run between the cable vault / switch-

gear room and the Reactor Building NW corner; these penetrations

are of the configuration type called Typical H.

The licensee

estimated that the use of the 6428 RTV Silicone Elastomer con-

stituted 20% of all fire seals installed at the plant, and 80%

of this amount was associated with the aforementioned penetra-

tions. The inspector noted the fire loading conditions on both

sides of the penetration barriers. The cable vault /switchgear

room are routinely monitored by the . inspector during inspection

tours and have been found free of transient combustible materials.

The inspector also noted that the RB side of the penetrations were

clear of combustibles, although this area had been used as ar HP

control point for torus work crews prior to the completion of the

torus modifications.

Licensee review and evaluation of the Chemtrol findings were

in progress, but incomplete.

Further information from Chantrol

regarding the specifics of the testt completed on October 27 and

October 28, 1980, was required.

The licensee did state that

based on preliminary evaluations, the October 27th test performed

by Chemtrol may not be applicable to the VY installation. The

principle factor in support of this assumption was based on the

physical differences between the CTP 0205 test configuration and

the Typical H configuration installed at the plant.

The inspector

noted through review of engineering drawings for both configuration

types that the CTP 0205 configuration employed a greater total

area of silicone elastomer fill than did the Typical H configuration.

The licensee stated further that previous analyses and acceptance

testing using 6428 RTV Silicone material in configurations similar

to the VY installations had successfully demonstrated the 3-hour

fire rating capability.

However, the licensee stated that this

matter would be pursued with the Chemtrol Corporation to resolve

outstanding questions raised by the October 27th testing.

~

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The inspector had no further questions on this item for the

present. The item is considered open pending:

completion

of licensee actions to evaluate the applicability of the

October 27, 1980 Chemtrol test results to VY installations;

1

and, further NRC staff review of licensee actions and findings

(IFI 50-271/80-17-02). A special inspection of this area by

NRC Region I Specialist was conducted; see NRC Region I

Inspection Report 50-271/80-18.

1

11.

Surveillance Testing

The inspector reviewed licensee actions related to (i) the completion

of core shutdown margin surveillance testing for the beginning of cycle 8

operation; and (ii) procedures and preparations for the conduct of a

Primary Containment Type A leak rate test (LRT).

Findings are

summarized below,

a.

Shutdown Margin Test

Core shutdown margin testing was completed on October 31, 1980, in

accordance with Technical Specification 4.3.A.1

equirements for the

beginning of cycle 8 operations. Testing was conducted in accordance

.

with procedure OP 4426, Shutdown Margin Check, Revision 7, dated

September 14, 1979, with tne reactor at 640F and the vessel head

removed. Control rod 30 '3 was used as the object rod, with

diagonally adjacent rod 34-27 selected as the margin rod. A calculated

integral worth for rod 34-27 supplied by the NSSS vendor was used.

The following completed data sheets were reviewed:

+

VYOPF 4426-01, Revision 7, Shutdown Margin Data Sheet

+

VYOPF 4450.02, Revision C, Rod Worth Minimizer Check

Post test review of data sheets indicated that test prerequisites

had been met. The value chosen for R1, the expected increase in

excess reactivity over the cycle due to gadolinium burnup, was 0.5%

delta k/k.

The value for R2 was 0.07% delta k/k, which is a penalty

taken to account for potential shutdown margin loss due to boron

carbide settling. An overall rodworth uncertainity of 10% was

assumed.

Inverse multiplication plots wet e maintained as both rods

were withdrawn from the core. The test demonstrated that the reactor

remained subcritical with both rods withdrawn. Adding the calculated

worth of rod 34-27 to the. core k-effective (at 80oF with the worst

rod, 30-23, withdrawn) and applying a moderator temperature

coefficient correction, the minimum shutdown margin was determined

to be at least 0.524% delta K.

Based on the calculated inteoral worth rod

_

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.

23

34-27, the minimum shutdown margin was femonstrated with rod 34-27

at position 16. The Technical Specification requirement that mini-

mum shutdown margin be greater than R+ 0.57%, or 0.82% delta k,

was satisfied.

The inspector had no further comments on this item.

No items of noncompliance were identified,

b.

Preparations for Containment Integrated Leak Rate Test

Plans and preparations for the conduct of a containment Type A leak

rate test were discussed with licensee personnel during the inspection

period.

During these discussions, the licensee asked what the NRL

staff position was for the conduct of a reduced length Type A test.

This matter was discussed with NRC Regional and Headquarters

personnel in a conference call on November 3,1980.

The NRC staff

has accepted reduced duration Type A tests in the past, when conducted

precisely in accordance with topical report BN-TOP-1, Revision 1.

Under the BN-TOP-1 Methodology, the leak rate test interval is taken

at 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> instead of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Licensee personnel compared the VY test instrumentation and capabilities

with the requirements of BN-TOP-1 and concluded the requirements could

be satisfied with the exception of the following:

+

repeatability for drybulb temperature measurements

+

a lack of data to demonstrate repcatability for exactel and dew

point sensor measurements.

The licensee concluded, however, that repeatability for the above

instruments could be demonstrated based on data from previous Type A

tests.

During the conference call on November 3,1980, the NRC staff

stated that the VY proposal would have to be submitted in writing for

review before approval could be given for the proposed VY test

methodology. Due to the shortness of time before the Type A test

was scheduled for conduct and NRC staff limitations for providing a

quick response to a VY submittal, the licensee decided to not seek

approval for a rec'uced length Type A test for this outage. A 24-hour

test would be conducted.

The inspector had no further comments in this area. VY Type A leak

rate testing will be followed on subsequent inspections.

.

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24

12.

Plant Modifications and Refueling Operations

Licensee activities in the areas of maintenance, facility modifications

and refueling operations were reviewed during the inspection period.

Refueling and reactor vessel work during the inspection period included

a variety of activities and followed the following general sequence:

(1) fuel shuffle and core verification complete - 10/24; shutdown

margin test complete - 10/31;

installation of core spray sparger "C"

junction box clamp - 11/1;

initial ISI findings of non-isolable leak

on RWCU system - 11/1; TS change request submitted to allow core off load

without 3 cps on SRMs to support RWCU repair - 11/6; core off load for

RWCU repair started - 11/6; core off load complete - 11/11; and, refuel

cavity and reactor vessel drained to level of recirculation nozzle - 11/14.

Inspector review and findings in this area are summarized below,

a.

Refueling Operations

(1) Fuel Handling Activities

Fuel movement activities were periodically monitored by the

inspectors throughout the reporting period.

Related records

were reviewed and activities were observed to varify that:

prior to handling of fuel in the core, all surveillance

--

testing was completed.

--

during the refueling outage, periodic testing of refueling

related equipment was performed.

inspector observance of fuel handling operations for

--

verification of conformance to Technical Specification

and approved procedure requirements.

containment integrity was maintained.

--

observation of licensee housekeeping in the refuel area.

--

review of licensee staffing during fuel handling operations

--

to verify minimum crew and type on license requirements

were met.

No unacceptable conditions were identified and, except as noted

below, the inspector had no further comments in this area.

,

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.

25

During the fuel movement period of October 22 through

October 24 periodic inspections were conducted to ascertain

whether licensee fuel handling operations were being conducted

as required by Technical Specifications and approved procedures.

The following references were used to evaluate licensee actions:

OP 1100, Revision 9, issued August 23, 1979, Refueling

--

Platfonn Operation

OP 1410 Revision 9, issued June 30, 1980, Fuel Loading

--

AP 1000, Revision 5, issued September 18, 1979, Refueling

--

Vennont Yankee Technical Specifications, Section 3.12 and

'

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4.12, Refueling and Spent Fuel Handling

During the review of licensee procedures the inspector noted

conflicting requirements pertaining to the inspection of the

refueling platform grapples and cables, and subsequent logging

of the completed action.

The inspector noted that:

OP 1410, Fuel Loading, Precautions step 9, requires that:

-

--

grapples and cables shall be inspected daily and checked

to insure correct operation. Verification of this check

shall be logged in the Refueling Log.

AP 1000, Refueling, step B.7, requires that:

the refueling

--

platform grapples and cables shall be visually inspected

daily and checked to insure correct operation. Verification

!

of this check shall be logged in Control Room Operations Log.

AP 1000, Refueling, Page 6, step 11, requires that:

the

--

Senior Licensed Operator on the refueling floor visually

inspect grapples and cables each shift to insure correct

operation, and insure this is logged.

The inspector verified by review of the shift supervisor's log

>

that inspections of the refueling platform grapples and cables

were being conducted and logged at least daily. The inspector

,

interviewed selected Senior Licensed Operators on the Refueling

Floor and determined that each visually inspected grapples and

cables on a shift basis, although this action was not always

logged.

A review of the Refueling Log revealed no entries con-

cerning inspection of the refueling platform grapples and cables.

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26

Following discussion with Operations Department personnel, it

was determined that a daily verification of the refueling plat-

form grapples and cables was required by the licensee in an attempt

to minimize fuel handling problems.

The licensee noted the

inspectors comments and will issue changes to the above refer-

'

enced procedures to provide consistent inspection and logging

requirements. The results of the licensee's actions will be

reviewed during a subsequent inspection (IFI 50-271/80-17-03).

(2) Technical Specification Change

Repair of the non-isolable portion of the RWCU system required

a complete off load of the reactor core.

Licensee review of the

off load evolution identified that minimum source range count

rate requirements (defined as 3 cps per Technical Specification 3.12.B.2) could not be maintained with no fuel in the reactor.

Further, the minimum count rate could not be achieved prior to

reinsertior, of the first fuel assembly following RWCU repairs.

A scheme to optimize SRM count rates with a partially loaded

core was developed. The scheme defueled the reactor in a

modified spiral pattern.

Core reload would occur in the

exact opposite sequence. The licensee submitted to NRC:NRR

a proposed Technical Specification change, along with an

accompaning safety evaluation, to allow for using the spiral

unload scheme and core reload with less than 3 cps on i.he

SRMs.

NRC:NRR approved the proposed changes to Technical Specifi-

cation 3.12 on November 10, 1980.

The inspector had no further comment on this item.

(3) CORE Loading Verification Procedures

VY procedures for core load verification were reviewed in

accordance with special review instructions contained in

TI 2515/40, BWR Core Loading and Verification Procedures

dated October 1, 1980.

References for this review included

the following:

OP 1411, Core Verification, Revision 4, September 14, 1979

--

AP 1000, Refueling, Revision 6, September 26, 1980

--

OP 1140, Fuel Loading, Revision 9, August 23, 1979

--

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27

Administrative controls established by the above procedure

were reviewed to verify the following were included:

(a) videotaping of the loaded core with camera equipment

mounted on the fuel handling mast;

(b) a minimum of two staff members involved in the observation

and recording of core load information;

(c)

requirements that infonnation verified for core load

verification included core location, fuel assembly serial

number, bail orientation, fuel channel clip position

and cell orientation;

(d)

requirements for QA verification of bundle orientation.

During this review, the inspector noted that sufficient procedural

guidance was given to adequately verify the items specified under

paragraph (c) above, but that no information was presented in the

procedures to show the proper orientation for 12 peripheral fuel

bundles that are not part of a complete cell.

The Reactor Engineer

stated that such an item was assumed to be general knowledge through

staff training.

Inspector discussions with RE personnel found this

to be the case.

The inspector stated, however, that the appropriate

procedures should be changed to incorporate the required positions

of the 12 peripheral fuel bundles.

The inspector also noted during review of the referenced procedures

that no requirement existed to provide for second level /QA review

of the loaded core. The inspector noted during discussions with

RE personnel that in spite of the lack of administrative require-

ments, third and fourth levels of review are provided for core load

verification on a routine basis. Aside from the two RE staff

members that record the core verification data and videotape the

core, an 0QAD staff member is present during the verification.

Beyond this, one or more members of the RE staff, including the

Reactor Engineer, reviews the completed videotapes as a final

check of core load orientation. The inspector adknowledged the

above, but stated that the appropriate procedures should be

changed to require, at a minimum, second level /QA verification

of core loading.

The required procedure changes were discussed with the Reactor

Engineer, who stated that the appropriate changes would be made

during the next procedure review cycle.

This item is unresolved

pending incorporation of the requirements (URI 50-271/80-17-04).

!

!

.

.

28

The inspector also conducted an independent review / verification

of the completed core on Octcber 27, 1980 and noted proper FA

-

positioning by core location, serial number, cell orientation,

clip position and bundle orientation.

This review was completed

subsequent to licensee verification checks.

The inspector had

no further comments on this item.

b.

Plant Modifications

Preparations for and modifications in progress during the inspection

period were reviewed to verify activities were completed in accordance with

administrative requirements and licensee committments. Areas reviewed

and inspector findings are summarized below.

(1) Drywell Leakage Deflectors, EDCR 80-36

EDCR 80-36, Primary Coolant System Leakage Deflectors, dated

October 6, 1980, was written to uddress concerns raised in

LER 80-18.

The licensee evaluated the sources of leakage inside

the drywell from main steam, HPCI, RCIC, RHR and feedwater lines

to determine the potential for leakage to bypass the drywell floor

and equipment drain sumps.

Leakage from the main steam, HPCI and

the drywell continuous air monitor

RCIC systems can be detected by(fan cooler collectors) due to the

and the equipment drain system

high temperature and radioactivity of the steam associated with

the systems. Only leakage from the feedwater and RHR supply / return

lines has the remote potential to go unmonitored.

The EDCR adds

deflector plates, made of'no, 11 guage galvanized sheet steel

cut to dimensions of 72"L X 48"W, under the appropiate feedwater

and RHR lines. The deflector plates are to be installed above

four drywell to torus vent pipes, in the vicinity of drywell pene-

trations X-9B, X-9A, X-13A, X-12, and X-138. The intent of the

deflector plate is to deflect leakage from the line protected,

rather than protect the entire vent pipe opening.

The deflector

plates are to be tac welded to the I-beam and grating structure

on the drywell 252 foot elevation, with an epoxy seal to the dry-

well skin.

The licensee also considered the effects of the deflectors

on LOCA blowdown capability and concluded that the functioning of

the vent headers would not be affected (i.e., no reduction in

vent area) due to the four foot seperation between the deflectors

and the vent opening.

Installation of the deflectors is scheduled to be completed during

the 1980 refueling outage. This item will be examined by the

inspector on a subsequent inspection, following installation of

the deflectors.

-

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29

4

(2)

Recirculation Pump / Analog Trip System, EDCR 79-02

Installation of the RPT/ Analog Trip System continued during the

outage. Activities in progress were observed periodically by

the inspector to verify work was done in accordance with the

governing procedures.

The RPT system will provide an ATWAS

trip function on high reactor pressure (at 1150 psig) and low-low

vessel level (-44.5 inches with 10 second time delay).

The

'

recirculation pump generator field breakers are automatically

opened if the trip setpoints are reached.

Installation of the

Analog Trip system will replace certain YARWAY level trans-

mitters and Barksdale pressure switches mounted on the 25-5

and 25-6 racks with Rosemont Pressure and Level transmitto s.

Change-out of the YARWAY/Barksdale transmitters is intendea to

enhance the reliability of the RPS by providing a more accurate

monitoring of reactor vessel pressure and level, and initiate

protective functions through RPT and alternate rod insertion.

The inspector noted through discussions with licensee staff

that installation of the alternate rod insertion feature, although

the outage due to the

part of the EDCR, will not occur during(valves).

non-availability of certain components

The inspector

also noted that the NRC's confirmatory order to VY dated

,

February 21, 1980, addressed installation of the RPT only.

On November 2, 1980, the inspector used the Installation Procodure

for EDCR 79-02, dated October 11, 1980 to perform a partial

verification of field run wiring between analog system cabinets

and instruments mounted on racks 25-5 and 25-6.

Installation

of the following circuits was verified:

CABINET RPS-CP-25-6A, Subassembly A2,B2

Conduits: A2-1101PRA2, 18550RA2, 1855 ARA 2, 18592

B2-1856DRB2, 11103PRB2, 1851ARB1

Cables / Wires

Terminals

C1806P-RA2

AA1, AA2, AA3, AA4

C1855A-RA2

AAS, AA6

C1855B-RA2

AA7, AA8, AA9

C18590

BB4, BBS

C11103P-RB2

KK6, KK7

C18568-RB2

JJ10, JJ11, JJ12

._

.

.

30

CABINET ECCS-CP-25-6B

Conduits:

1865DS1, 1867DS1, 1865FS1, 11293, 1865ASI

Cables / Wires

Terminals

C1866ASII

CC1, CC2, CC3

C1867BSI

CC7, CC8, CC9, CC10

C11451VSI

KK4, KK5

CABINET ECCS-CP-25-5A, Subassembly A1, B1

Conduits: Al-1850 ERA 1,1803QRA1,1850DRA1,1850 ARA 1,1855 ARA 2

B1-1851 ERB 1, 1810QRB1, 1851ARB1, 1851DRB1, 1859C, 1859F

Cables / Wires

Terminals

C1803Z-RAL

AA1, AA2, AA3, AA4

C1850A-RA1

AA5, AA6

C1850C-RA1

AA10, AAll, AA12

C11100Z-RA1

BB8, BB9

CABINET ECCS-CP-25-5B

Conduits:

1860FSII, 1129A, 1862ESII, 1860ASII, 1862ASII, 1860GSII

Cables / Wires

Terminals

C1862CSII

DDI, DD2

C1862BSII

CC7, CC8, CC9

CC10, CC11, CC12

C112500-SII

EE3, EE4, EES, EE6

C1861ASII

CC1, CC2, CC3

No inadequacies were identified during the above review. The

inspector had no further comments on this item at the present;

however, NRC review of the RPT installation and testing will con-

tinue on subsequent inspections.

(3) Drywell High Range Radiation Monitors, EDCR 80-02

The inspector reviewed the design pacPage for EDCR 80-02, Contain-

ment High Range Radiation Monitor, dated September 24, 1980. . Work

completed under the design change will satisfy Item II.F.1.2.c of

NUREG 0737.

Work in progress this outage will install two

__

o

.

31

Victoreen Model 877 ion chamber detectors above the equipment

hatch inside the drywell. The detectors will provide _ gamma _

field dose rate measurements over the range of.1E+0 to 1E+7

R/hr, with control room readout consisting of two panel indica-

tors on CRP 9-2, two sigma indicators on CRP 0-3 and alarm

only annunciator on CRP 9-3 (D/W RAD LEVEL HijiQUIP FAIL).

The inspector had no further comment on this item at the present.

This item will be reviewed further on subsequent inspections.

13.

Inspector Followup on Rdgional Request

The inspectors conducted special inspections of specific areas during

the inspection period at the request of the NRC Regional and/or HQ

staffs. Areas reviewed during this inspection included:

+

susceptibility of the VY containment to the Indian Point 2 type

flooding event;

further followup of licensee actions taken in response to IEB 80-17

+

requirements, BWR Failure to Scram;

+

adequacy of certain emergency plan implementing procedures for per-

forming postulated off-site dose projections; and,

+

completion status of VY actions taken in response to the Category A,

TMI Short Term Lessons Learned items of NUREG 0578.

Inspection findings in these areas are summarized below,

a.

Susceptibility of Flooding Events

During the period of November 3 and 4, 1980, the inspector conducted

an inspection to determine Vermont Yankee's susceptibility to the Indian

Point No. 2 type of flooding event. As a result of the inspection, the

following information was forwarded to Region I personnel at the request

of the Division of Reactor Operations Inspection:

Vermont Yankee is equipped with both a Drywell Equipment Drain Sump and

a Drywell Floor Drain Sump. The Equipment Drains are provided for

varicus components in the drywell, including valve and pump seal leak-offs.

The Drywell Floor Drain system collects and disposes what is considered

to be " unidentified" leakage.

In addition, the reactor cavity drains

to the floor drain sump.

.

,

.

32

The Drywell Equipment and Floor Drain Sumps are equipped with

level switches used for a leakage rate alarm system.

Leakage

rate measurement is accomplished by measuring the time interval

between activation of two different level switches in the sump

as the sump fills with water. Whenever the time interval de-

creases to a prescribed point (indicating an increase in leakage

rate), or if a sump pump runs longer than a preset time interval,

,

an alarm annunciates on Control Room Panel (CRP) 9-4 indicating.either

Drfwell Equip ~m~ent Drain ~ SumpJeillage"High_(A-4/A-9)~or Diywel_1_Elo.or

~

DrainSumpLeakageHigh(A-4/C-8).~Eachsumpisequippedwith

-

two 50 GPM aumps. A sump pump will start automatically upon the

liquid reacting a preset high level and will stop upon the liquid

being lowered to a preset low level.

A second pump starts and

an alarm sounds in the Control Room if the liquid reaches a

high-high level.

Pump)run indication is provided in the control room by operating

(red or secured (green) status lights on CRP 9-4 horizontal

section; in addition, a flow recorder (2 pen) and integrating

flowmeters are provided on CRP 9-4 for detennining leakage rate

over a period of time.

Components inside containment utilize a closed cooling water system

RBCCW, whose surge tank level is monitored by weekly surveillance.

The following documents were reviewed during the inspection:

OP 4152, Revision 8. July 11, 1980, Drywell Equipment and

-

Floor Drains Surveillance

OP 2152, Revision 7. July 11, 1980, Drywell Equipment and

-

Floor Drains

Dwg 191177 Revision 6, Flow Diagram - Radwaste System

-

OP 3140, Revision 4, April 16, 1980, Alarm Response

-

RP 2182, Revision 8, August 14, 1980, Reactor Building Closed

-

Cooling Water System

The inspector had no further questions in this area.

b.

Scram on Scram Discharge Header Low Pressure:

IEB 80-17

NRC staff review of the VY response to IEB 80-17, Supplement 3,

Item 1.a noted that the licensee had incorporated changes to

'

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.

.

33

procedures (DI 80-45, Revision 1 to OP 2111) that instructed the

.

'

control room operator (CRO) to initiate an immediate manual scram

of the reactor whenever scram pilot air pressure decreases to

65 psi (a value at least 10 psi above the scram outlet valve opening

pressure), based on local indications from PI-3-229.

The use of local

(outside the control room) pressure indication as a basis to initiate

CR0 action was discussed with the licensee. The NRC staff position

presented was that the use of local position indication was unacceptable

in this case, due to the following considerations:

+

PI-3-229 is mounted near the backup scram valves on the 252-foot

elevation of the Reactor Building.

Upon receipt of the CRP 9-5

annunciator, SCRAM PILOT HDR PRESS HI/LO (panel A-8, window D-4),

the information immediately available to the CR0 is that scram

pilot air pressure is either_above 75 psig or below 70 psig. To

determine whether the air header pressure was below 70 psig would

require that an auxiliary operator be dispatched to PI -3-229 for

a reading and then report back to the control room.

This

determination could take 3 to 5 minutes to accomplish under ideal

conditions.

.

+

NRC staff evaluation of various scram discharge system failure

mechanisms 4dicated for a certain postulated failure, the scram

discharge headers could fill in as fast as 2 to 3 minutes without

attendant rod-in motion.

Under this scenario, immediate manual

action by the CR0 is necessary to assure the scram function occurs

before loss of the scram discharge system.

Based on the above, the inspector stated that the licensee's

response to Item 1.a was unacceptable and that either (i) a control

room indication of scram pilot air pressure must be provided; (ii) pro-

cedures must be revised to require a manual scram based on receipt of

the annuncistor alarm; or, (iii) other compensatory measures be taken

to address the concerns discussed above.

Actions to address the NRC

staff position must be completed prior to startup from the 1980 refueling

outage.

The licensee acknowledged the inspector's comments and stated that

the staff position would be reviewed and actions taken as appropiate.

This item is unresolved pending completion of licensee action in this

area and subsequent review by the NRC (URI 50-271/80-17-05).

,

c

EPIP Review - Offsite Dose Projections

During the inspector's review of VY emergency operating procedures

(EOPs) and emergency plan implementing procedures (EPIPs),

.

.

34

particular attention was given to OP 3013, Initial Evaluation of

Offsite Radiological conditions. This procedure provides instructions

for the offsite and EOF response members to assess the type and

magnitude of postulated radioactive releases, Appendix A and Table I

requirements - see paragraph 2 above) y the E0Ps (per IAL 80-34

to this procedure are now referenced band would be used by the

shift supervisor, acting as the emergency director, to determine

an initial, rough estimate of offsite radiological conditions upon

which to base recommended protective actions.

The instructions,

dose projections and information provided by Appendix A to OP 3013

were reviewed to verify the procedure was technically adequate and

capable of accomplishing the desired function when implemented.

Appendix A of OP 3013 provides a tabulation of plant area radiation

monitom (ARM) with corresponding projected dose rates at the site

boundary, assuming a full scale reading on the ARM.

Information

tabulated includes type of release (elevated or ground); ARM;

panel location; ARM full scale reading; and, the 1/50 and 1/100

boundary valve cloud concentration and dose rate..For Appendix A

purposes, the site boundary is divided into two sectors:

one

900 sector pointing West from the site; and, one 2700 sector for

all other directions. A plume travelling _toward_the_ West would

constitute _the.most.. restrictive releas_e_ direction,_f_ or_ the_ assumed ___

meteorology, and a dilution factor from the point of emission of

1/50 is applied.

For a release path in any other direction, a 1/100

dilution factor is applied for conditions at the boundary. The

inspector compared these assumptions with the DBA dose calculations

provided by FSAR Section 14 and found them in agreement with the

computer based dilution projections.

The inspector reviewed the Appendix A - Table I information to

verify:

all ARMS useful for dose projection were incorporated;

listings for ARM full scale readings and conversions to source

terms were accurate; and, projected boundary dose rates were

accurate.

Findings are as follows:

(1) Table I values for dose projections at the 1/50 and 1/100

boundaries provide conservative dose estimates. Using the

Stack Gas I/II monitors as an example, the full scale reading

of IE+6 cpm was found to represent a source term of 0.75 ci/sec

release rate at the stack, based on a empirically derived

correlation of monitor efficiency. The full scale reading

represents a concentration of 1E-2 uci/cc ive a 156,000 cfm

-

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35

ventilation air flow and assuming a mix of isotopes provided

by EPA-520/1-75-001. A Chi-over-Q calculation based on this

source term, assuming Class E stability and a 5 m/sec wind

speed, yields 50 mR/hr and 25 mR/hr at the 1/50 and 1/100

boundaries, respectively. The Table I values of less than

60 mR/hr and less than 30 mR/hr, respectively, are then

conservative.

(2) ARMS listed in Table I cover three levels of the Turbine Building,

two levels of the Reactor Building and the A0G Building. The

listing provides most of the ARMS available that would be useful

for initial dose assessments.

The instructions _provided

in Table I were sufficient to get the dose assessment completed.

The inspector noted, however, a few discrepancies in the tabulated

infonnation, related to designated ARM number and full scale

readings. Turbine Building ARMS were listed as instrument numbers

20, 22, 26 and 27, whereas the appropiate designators are 13, 21

and 24, for the moisture seperator, main steam valve and T/G inlet

area monitors, respectively.

Full scale readings for the monitors

were listed as 1000 mR/hr, whereas the actual value is 10,000 mR/hr.

The insoector also noted that ARM #14, located on the West Refuel

Floor and has a full scale reading of lE+6 mR/hr, should also be

included in Table I.

>

(3) The inspector noted Appendix A Table I also contains references

for Iodine dose determinations and accident level classification

limits based on radiciodines.

No information immediately available

in the control room provides radioiodine concentration or dose

information and thus, a recommendation for protective actions

based on radiciodines could r.ot be made during the initial assessment.

As such, references / instructions to conduct an iodine dose assessment,

which could be a cause for confusion, should be deleted in the

instructions to control room personnel.

The inspector had no further comment on this item at the present.

Dis-

i

crepancies noted in paragraphs (2) and (3) above will be corrected in

<

a subsequent update of OP 3013. This item is open pending completion

of licensee action in the area and subsequent review by the inspector

(IFI 50-271/80-17-06).

d.

Review of NUREG 0578 Short Term Lessons Learned Category A Items

Implementation

During the inspection period the inspectors completed a review

of licensee implementation of NUREG 0578 Short Term Lessons Learned

. _ _ - -

,

.

36

Category A Items. The review consisted of establishing licensee

committments to fulfill the Category A requirements and a followup

inspection to detennine the status of licensee implementation. The

following references were used during the course of this inspection:

(1)

NUREG 0578, Published July 1979, TMI-2 Lessons Learned Task

Force Status Report and Short Term Recommendations

(ii)

NUREG 0660, Published May 1980, Revised August 1980, NRC

Action Plan Developed as a Result of the TMI-2 Accident

(iii) WVY 80-135, September 29, 1980, Shift Technical Advisor

Implementation Schedule

(iv)

WVY 80-7, January 8, 1980, Vermont Yankee Responses to NUREG 0578 Recommendations

(v)

WVY 79-130, November 20, 1979, Followup Actions Resulting from

the NRC Staff Review Regarding the TMI-2 Accident

(vi)

NRC (DENTON) letter, October 30, 1979, to ALL OPERATING NUCLEAR

POWER PLANTS, Discussion of Lessons Learned Short Term

Requirements

(vii) WVY 79-135, November 15, 1979, Long Term Questions for B&O

Task Force

(viii) NRC letter, April 1,1980, Staff Evaluation of VY Actions

on Category A Items of NUREG 0578

(ix)

WVY 80-131, September 12, 1980, Proposed Technical Specification

Change

(x)

WVY 80-141, October 7, 1980, Proposed Technical Specification

Change

(xi)

WVY 80-151, October 23, 1980, Interim Criteria for Shift Staffing

(xii) NRC letter, July 31, 1980, Interim Criteria for Shift Staffing

(xiii) WVY 80-069, April 29,1980, Containment Hydrogen Monitoring

(xiv) WVY 80-052, April 1, 1980, Containment Hydrogen Monitoring

Note that in the listings that follow, the NUREG 0578 item number is

given followed by the NUREG 0660 TAP number in parentheses.

.

.

.

37

(1)

Item 2.2.1.b (I.A.1.1) Shift Technical Advisor

Requirements:

Reference (i)and(vi)

+

STA on Duty by January 1, 1980.

+

STA shall have a bachelor's degree or equivalent and receive

plant specific training in the response and analysis of the

plant for transients and accidents.

Licensee Commitment:

Reference (iv)

+

An STA will be available at the plant at all times starting

January 1, 1980, and assigned to shift duty.

+

A pool of 15 graduate engineers from the VY staff is to

fill the position on an interim oasis.

Inspection Findings

An interim group of STA's have been assigned to shift duty since

January 1, 1980. Members of the STA group are staff engineers

who have received STA specific training.

Sleeping accommmodations

have been provided at the site such that the STA is at all times

available to the control room within 10 minutes.

VY procedure

AP 0150, Revision 13, issued July 11, 1980, defines the duties,

responsibilities and authorities of the STA.

.

Licensee letter dated September 29, 1980, (WVY 80-135) to NRC

notes that the schedule for having fully trained STA's in place

by January 1, 1981, will not be met.

The estimated completion

date for having fully trained STAS is June 1, 1981.

By letters

dated September 12, 1980 andOctober7,1980(referencesixandx),

proposed Technical Specification changes were submitted to the

NRC to incorporate the assi " ment of SYAs.

The inspector had no further comments on this item.

(2)

Item 2.2.1.a (I. A.1.2) Shift Supervisor Responsibilities

Requirements:

Reference (i)and(vi)

Shift supervisor responsibilities and authority defined to

+

maintain broad perspective.

.

.

38

+

Comand function delineated and transfer of comand defined.

+

Non-safety related duties delegated.

Licensee Comitments:

Reference (iv)

'

VY agreed with NRC position and issued a management directive

+

before January 1, 1980, to clearly define shift supervisor

responsibilities and authorities.

Inspection Finding

VY procedure AP 0150, Revision 13, dated July 11, 1980, was re-

viewed and found to implement the requirements defined by the

staff position.

The inspector had no further coment on this item.

(3)

Item - - -

(I.A.1.3) Shift Manning-Overtime Limits

Requirements:

Reference (ii) and(xii)

'

+

Specified minimum number of operations personnel on shift

and defined availability of personnel to man shifts.

Licensee Comitment:

Reference (xi)

+

VY intends to comply with the requirements of this item as

specified in a letter dated October 23, 1980, to the NRC.

Inspection Finding

By letter dated October 23, 1980, the licensee stated that the

interim staffing criteria were evaluated. VY found that all

adjunct requirements except d and e of reference (xii) were

met. Plans in progress for additional licensed operator

training will bring VY into compliance with all the revised

criteria by July 1, 1982.

VY is reviewing the shift overtime limits defined by reference (xii)

and IEC 80-02 and intends to comply with the criteria. VY formal

response to the NRC on this item is expected by November 20, 1980.

The inspector had no further coment on this item.

.

.

39

(4)

Item - - -

(I.C.1) Small Break LOCA Procedures

Requirements: Reference (i)and(ii)

+

Develope guidelines and procedures for coping with small

break LOCAs.

+

Retrain operations staff under new procedures.

Licensee Commitments:

Reference (v)

+

VY agreed to the NRC Staff position and worked with the

BWR Owners Group to develope accident procedure guidelines.

Inspection Findings

NRC Region I Inspection Report 50-271/80-04 documents inspector

review of procedures developed pursuant to the NRC staff approved

BWR guidelines, and review of operator training on the revised

procedures. No inadequacies were identified in regard to

procedures and training.

It should be noted that Inspection Report 50-271/80-04 identified

one unresolved item (80-04-02) concerning the power supplies for

torus and CST level instruments, and the availability of this

level information assuming the loss of the single most limiting

instrument bus. The subject item is still open.

The inspector had no further comment on this item.

(5)

Item 2.2.1.c (I.C.2) Shift and Relief Turnover

Requirements: Reference (i)and(vi)

+

Checklists to be provided to assure adequate shift turnover

of plant status information.

+

Checklists / logs to be provided to note equipment either out

of service and/or degraded.

+

System established to monitor effectiveness of shift turnover

procedure.

,

l

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.

.

40

Licensee Comitment:

Reference (iv)

+

By letter dated January 8, 1980, VY stated that operating

procedures were reviewed and revised as required to meet

the requirements of this item.

Inspection Findings

Inspector review of procedures AP 0150 dated July 11, 1980, and

AP 0152 dated December 31, 1979, found the applicable requirements

had been implemented.

The inspector had no further comment on this item.

(6)

Item 2.2.1.a (I.C.3) Shift Supervisor Responsibilities

Requirements: References (i)and(vi)

+

Shift supervisor responsibilities and authority specified.

+

Comand function delineated.

'

+

Non-safety related duties delegated.

Licensee Comitment:

Reference (iv)

+

VY stated their intent to comply with these requirements

by letter dated January 8, 1980.

Inspection Finding

VY procedure AP 0150, Revision 13, dated July 11, 1980, was re-

viewed and found to implement the requirements defined by the

staff position.

'

The inspector had no further coment on this item.

(7)

Item 2.2.2.a (I.C.4) Control Room Access

Requirements:

Reference (1), (ii) and (vi)

+

Develope administrative policy to establish that person having

control room comand function has authority to limit access.

+

Establish line of succession of control room command function

and chain of comunication.

)

. .

.

.

_

_

-

_

_

.

.

i

,

i

41

l

Licensee Connitment: Reference (iv)

+

By letter dated January 8,1980, VY stated that the authority

,

of the shift supervisor to limit control room access had been

re-affirmed and procedures were modified to establish control

'

room access policy.

Inspection Finding

!

VY procedure AP 0150, Revision 13, dated July 11, 1980, was found

to implement the requirements on control room access, lines of

authority and transfer of command functions.

l

The inspector noted that NRC ldtter of September 11, 1980 to VY,

t

-

j

reference (viii), states that a change to AP 0152 satisfies this

requirement. AP 0150 is the applicable reference.

The inspector had no further comment on this item.

(8)

Item 2.1.8 a (II.B.3) Post-Accident Sampling

Requirements:

Reference (i),(ii)and(vi)

t

+

Conduct design review and implement interim measures to allow

'

capability to promptly obtain an RCS and containment air

sample under accident conditions without exceeding 10 CFR 20

!

exposure limits assuming a RG 1.3 or 1.4 release of fission'

[

products; install additional shielding as required.

,

+

Conduct design / operational review and implement interim

,

measures to allow conduct of radiological spectrum analyses

i

I

for indicators of core damage following an accident; include

assessment for the effects of direct and airborne radiation

!

levels.

+

Provide procedures that allow the prompt performance of a

f

boron and chloride chemical analyses assuming a RG 1.3 or 1.4

l

source tenn.

j

Licensee Commitment:

Reference (iv), (v), (xiii) and (xiv)

+

By letter dated January 8, 1980, the licensee stated that the

[

piant sampling capability had been reviewed in light of the

i

new criteria.

Capability for containment air sampling and

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42

hydrogen analysis is provided by the containment air

dilution (CAD) system, which has a sample connection

available outside the reactor building.

Insotopic

analysis of the gas sample can also be performed.

+

A tap for RCS samples is located in'.the Reactor

Building, which may not be habitable under 10CFR 20

restrictions assuming a RG 1.3/1.4 source term.

Procedures were revised and measures were taken to make

it possible to obtain an RCS sampie containing several

mci /ml activity, convey it to a laboratory and analyze

it without exceeding 10 CFR 20 limits.

+

Modifications have been proposed (EDCR 79-51) that would

allow analysis of samples with existing laboratory equip-

ment as well as on-line analytical equipment.

Selection

of the most suitable equipment and methods is expected to

meet the Category B requirements of NUREG 0578

(January 1, 1980).

Inspection Findings ,

Procedure OP 3530, Post Accident Sampling, Revision 0, inclusive

of DI 80-21 dated September 24, 1980, was reviewed and found to

address licensee commitments in this area.

Through discussions

with the Chemistry and Health Physics Supervisor, review of OP 3530

and other operating procedures, and review of facility records,

the following was determined.

OP 3530 was developed as a result of the licensee's design / opera-

tional review of containment and RCS sample and analysis capabili-

ties.

Protective measures instituted oer OP 3530 are based on an

RCS sample activity of several mei/ml.' Results of the licensee's

preliminary evaluation of post accident radiation shielding surveys

were documented in a February 2, 1980, internal memorandum (TMI

TECH FILE).

Sample bomb dose calculations for 10 cc and 40 cc

bombs using 1 inch and 1.5 inch lead shielding were documented in

internal . memoranda dated April 2,1980 and August 11, 1980.

Containment gas sampling and hydrogen analysis capability is pro-

vida by the CAD system in conjunction with the MSA and Delphi

monitoring systems. The MSA system, which is mounted outside the

Reactor Building, provides hydrogen analysis capability over the

range of 0 to 4 volume percent. The MSA unit is a backup for the

Delphi Unit. The Delphi unit located in the Reactor Building on

l

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43

the 280 foot elevation, provides hydrogen analysis capability

over the range of 0 to 10 volume percent. Obtaining drywell

samples under pressurized containment atmosphere conditions

is available under nonnal operation of the CAD system. The

CAD system also provides for containment air sampling under

negative pressure conditions up to several inches of mercury.

OP 3530 contains instructions to obtain and analyze containment

gas samples.

Instructions for RCS sampling and analyses for activity levels

up to 3 mei/ml are also provided by OP 3530.

Capabilities for

sampling and analysis of higher activity samples will be provided

by design modifications completed under EDCR 79-51. For isotopic

analysis of RCS sampics once collected per OP 3530, a serial

dilution on a 1 ml volume is performed to reduce radiation levels

to the point where standard counting techniques can be employed

using OP 0631. The sample dilution will produce a sample with

activity levels within the capability of the onsite multi-channel

analyzer.

Within the capabilities of existing equipment, unpressurized RCS

samples can be taken and analyzed for baron, chloride, total

dissolved gas and oxygen. The capability does not currently

exist for taking pressurized RCS samples or for performing a

dissolved hydrogen analysis. Analysis sensitivity was specified

as falling within the range of 1.0 micro ci/gm up to the high

range limit. Licensee evaluation of sample analysis capability

assumed releases from the fuel at equilibrium core inventories,

consisting of 100% noble gas, 25% iodine and 1% particulates.

Other measures accounted for and/or incorporated in OP 3530 include

considerations for: personnel exposures for conducting the sample

operations, including a requirement for calculating a dose commit-

ment prior to undertaking the operation; personnel monitoring and

the use of TLDs and high range survey instruments; use of shielding

around the interim stack gas monitor, RM-16 detector; use of

shielding in the transport of samples; use of sample shielding and

ventilation (hood) systems to reduce background levels during sample

analysis; and, purging of sample lines to reduce plate-out and

accumulated buildup of contaminants.

In that the licensea imple-

mented measures for sample taking and analyses for activities up

to only 3 mci /ml, no otherportable shielding was used nor deemed

necessary, based on expected direct radiation and airborne dose

rates for the assumed source term.

\\

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44

.

Licensee action to demonstrate sample and analysis capability

under the assumed high activity conditions was limited to sample

dose rate calculations.

The inspector had no further questions on this item.

(9)

Item 2.1.3.a(II.D.3)SV/SRVPositionIndication

Requirement: Reference (i)and@i)

+

Positive indication of SV/SRV open status.

+

Safety grade, unambiguous indication in the control room

with annunciator / alarm functions.

+

Seismic qualification provided or schedule for qualifying.

Licensee Commitment:

Reference (iv) and (v)

+

By letter dated January 8, 1980, VY stated that modifications

had been completed to meet the above requirements.

Pressure

switches were installed in the SRV discharge piping and

accoustic accelerometers were installed on the SV discharge

manifolds.

Both position indication systems have control

room readout and alarm functions.

+

Pressure switches used on the SRVs are not seismically

qualified. The licensee committed to qualify the switches

by participation in a vendor program or replace the switches

with a qualified indicator by January 1, 1981.

Inspection Findings

NRC Region I Inspection Report 50-271/80-02 provides the results

of previous NRC inspection of the position indication for the

safety values.

No inadequacies were identified in regard to the

design and installation of the SV position indication system.

However, one item left open during that review concerned the

seismic qualification certain components in the system. Discussions

with licensee personnel indicated that the seismic qualification

i

for the subject components had not been completed and further,

j

that completion of the qualification may not occur by January 1,1981.

This item is addressed further below.

..

_ _

.

_ - - -

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45

The inspector reviewed the design package and the physical

installation of position indicators for the safety relief

valves. The modification was completed under PDCR 79-22,

Safety Relief Valve Open-Close Monitor.

The installation

and test procedures for the pressure switches were completed

,

on December 31, 1979. A two-out-of-three logic is used for

the valve open inidcation and power for the circuit is pro-

vided from a vital AC bus. An open-close indication for each

SRV is mounted on CRP 9-3 and a system annunciator / alarm

function is provided on CRP 9-3.

Except for the environmental

qualification of the pressure switches, the inspector had no

further comment on this item.

The inspector stated that if delays are expected beyond

January 1, 1981, to complete environmental qualification for

either the SV accoustic accelerometers or the SRV pressure

switches, the qualification program status and schedule should

be documented in a letter to the NRC.

This item is considered

open and will be followed on subsequent inspections

(IFI 50-271/80-17-07).

(10) Item 2.1.7.a (II.E.1.2) Auxiliary Feed System

Requirement

This item is specific to PWR plants and does not apply to VY.

(11) Item 2.1.1(II.E.3.1)PressurizerHeaterPowerSupply

Requirement

This item is specific to PWR plants and does not apply to VY.

(12) Item 2.1.5.c ( - - - ) Recombiner Procedure Review and Upgrade

Requirement

,

This item is specific to plants that have hydrogen recombiners

and does not apply to VY.

(13) Item 2.1.4 (II.E.4.2) Isolation Dependability

Requirements:

References (1),(ii)and(vi)

+

PCIS design shall comply with SRP 6.2.4 in diversity of

parameters needed for isolation.

>

_

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46

+

Identify all essential and non-essential process lines

penetrating the drywell and modify PCIS logic as required

to ensure proper isolation.

+

Ensure all non-essential lines are automatically isolated.

+

Ensure the PCIS reset feature would not result in inadvertent

loss of containment isolation.

Licensee Commitment: References (iv) and (v)

+

By letter dated January 8,1980, VY reported the results

of reviews in regard to diversity of parameters, non-essential /

essential system identification and isolation of non-essential

systems. VY concluded that sufficient PCIS initiation diversity

existed in accordance with SRP 6.2.4; and, all essential /

non-essential systems were found to respond appropriately

under PCIS actuation.

+

During VY review of the PCIS logic, several valves were found

that would automatically reopen when the PCIS logic was reset.

Interim administrative controls were instituted to require

the operator to place the control switch for the subject

valves in the " CLOSED" position prior to resetting the PCIS.

A design change would be installed on a subsequent plant

shutdown to inhibit automatic opening of the valves following

PCIS reset.

Inspection Findings

Licensee conclusions under the first three items above were re-

viewed by the inspector.

No inadequacies were identified.

Modifications to the PCIS logic were completed during a February,

1980, plant shutdown.

Inspector review and findings of the

modifications completed under EDCR 79-35 are documented in

NRC Region I Inspection Report 50-271/80-02.

No inadequacies

were identified.

The inspector had no further comment on this item.

(14) Item 2.1.3.b (II.F.2) Instrumentation for Inadequate Core Cooling

Requirement:

References (ii) and (vi)

+

Use of a subcooling meter.

i

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47

+

Design / analyze / install instrumentation to provide

unambiguous indications of inadequate core cooling.

Licensee Commitment:

Reference (.iv).,(v)and(vii)

+

Use of a subcooling meter is a PWR specific item and

does not apply to VY.

+

VY evaluations and actions in response to the staff positions

will be forwarded through the BWR Owners Group for evaluating

by the Bulletins and Orders Task Force.

+

Potential reactor vessel level instrumentation problems

identified by GE SIL 299 have been incorporated into VY

Operating Procedures and the operator training program.

NRC review of this item is documented in NRC Region I

Inspection Report 50-271/80-04.

No inadequacies were

identified.

The inspector had no further comment on this item.

(15) Item 2.1.1 (II.G.1) PRV Power Supplies

Requirements

This item is specific to PWR plants and does not apply to VY.

(16) Item 2.2.2.L (III.A.1.2.) Emergency Support Facilities

Requirements:

References (1), (ii) and (vi)

+

Establish interim Technical Support Center (TSC).

+

Upgrade to pemanent status per Category B schedule.

+

Develope procedure to describe TSC.

+

Designate individual responsible for activating TSC.

+

Incorporate references to TSC in emergency procedures.

Licensee Commitment:

References (iv)and(v)

.

By letter dated January 8, 1980, VY agreed to meet the requirements

of the staff position, provided descriptions of existing and planned

facilities and established schedule dates.

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48

.

Inspection Findings

The inspector toured the TSC and reviewed related implementing

procedures. The inspector found that emergency procedures

OP 3001, 3002 and 3003 were revised to delineate actions to

activate the TSC and define how its function will integrate

with other emergency response centers.

Procedure AP 3014

dated December 31, 1979, defines the administrative require-

ments for the TSC, its set up and maintenance. OP 3006, Revision

9, dated November 7, 1979, provides for the periodic calibration

of TSC equipment. No inadequacies were identified.

The inspector had no further comments on this item.

(17) Item 2.2.2.C (III.A.1.2) Operational Support Center

Requirements:

References (i), (ii) and (vi)

+

Interim Operations Support Center (OSC) established.

Licensee Commitment:

References (iv) and (v)

+

By letter dated January 8, 1980, VY stated that an interim

OSC had been established. The area designated for the OSC

was the ground floor of the Service / Administration Building,

with the HP control point used as the communications center.

Inspection Findings

The inspector reviewed applicable plant procedures that established

the OSC and integrated its function with other emergency response

centers. AP 3015 dated December 31, 1979, established the OSC

and defined its functions and designated responsibilities for its

activation. Functions of the OSC were incorporated in procedures

OP 3001, OP 3002, OP 3003 and AP 3014

No inadequacies were

identified.

The inspector had no further comment on this item.

(18) Item 2.1.6.a (III.D.1.1) Primary Coolant Outside Containment

,

Requirements:

References (i),(iv),(vi)and(viii)

+

Implement program to reduce leakage from plants systems

outside of containment to as-low-as practical levels, for

j

those systems that could contain highly radioactive fluids

following an accident.

.

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49

+

For immediate leak reduction, implement leakage reduction

measures and measure actual leakage rates with systems in

operation and report the results to the NRC.

+

Establish and implement a program of preventive maintenance

to maintain leakage to as-low-as-practical levels; program

should include periodic integrated leak tests.

+

Include considerations for a North Anna type release path.

Licensee Comitment: References (iv) and (v)

+

Systems outside containment that could contain high levels of

radioactivity following an accident were identified and

examined for leakage under operating conditions.

Systems

excluded from the program were also identified.

For those

systems included in the program, steam and water systems

were visually inspected and gasious systems were leak tested

with helium while operating under positive pressures.

Results

of these inspections and a listing of systems in each category

were reported in a January 8, 1980, letter to the NRC.

+

" Benchmark" samples of airborne activity were taken in plant

areas not rcutinely visited by plant operators. The " Benchmark"

activity levels will be used for comparison whenever increases

in leakage are suspected.

+

A leakage reduction program was instituted which will result

'

in the visual inspection (and repair as necessary) of selected

systems each month in conjunction with the Technical Specifica-

tion Surveillance operability tests.

Systems included in this

<

program include:

the RHR, HPCI, RWCU, CS, RCIC systems; and,

the RHR, RWCU and recirculation sample systems.

+

Based upon a review of the North Anna event, VY detennined

that all tanks containing radioactivity vent into filtered

ventilation systems prior to release to the environment,

and thus, no modifications were required.

Inspection Findings

The inspector reviewed the results of the base line leakage measure-

ments performed on the standby gas treatment system (SGTS) as re-

ported in a December 17, 1979, Test Report to the Operations

,

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50

Supervisor. Testing was conducted under special test procedures

STP-79-05, Helium Leak Testing, dated December 10, 1979.

The

HPCI gland seal exhauster was also tested.

No leakage was found.

The inspector also reviewed the results of baseline leakage

measurements completed on systems that contain radioactive materials.

The measurements were made by visual examination of piping with

the plant operating at full power, during a walkdown of the systems

over the period of November 27-December 31, 1979.

No leakage was

found other than the flange leak on the RWCU system.

Flange' leakage on the suction side of the RWCU pumps, identified

during the base line leakage program, was repaired under

MR-79-1139 on January 9, 1980.

The " Benchmark" air activity sample results for areas not

routinely visited by the operator were also reviewed. These

areas include the steam tunnel (3.3E-0 uci/cc), the RWCU heat

exchanger room (7.6E-10 uci/cc), and the Holdup Pump Room in the

Radwaste Building (2.3E-9 uci/cc).

Implementation of the monthly leakage monitoring and reduction

program was confirmed by rsview of completed data sheets, for the

procedures listed below, for the period of February, 1980 to

September, 1980. The system covered by each procedure is also

listed.

HPCI

OP 4120.01

--

RCIC

OP 4121.05

--

CS

OP 4123.01

--

RHR

OP 4124.04

--

RHR Sample

AP 0150.02

--

,

RWCU Sample

AP 0150-02

L

--

The AP 0150-02 data sheets are the auxiliary operator #2 round sheets

and are completed once per shift.

Instructions to the auxiliary

operator, in general, require that observations for leakage be made

,

in all areas toured. Additionally, specific entries on the round

l

shcet require that certain areas be specifically examined as part of

the leakage reduction program.

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i

Based on review of the AP 0150.02 forms and discussions with the

Operations Supervisor, the inspector noted that no provisions

existed to record the results of leakage monitoring on the

recirculation sample system. Additionally, although portions

of the RWCU system were specifically covered by the form, no

provisions existed to ensure that all portions of the RWCU

system ware examined during the shift rounds. The licensee

stated that AP 0150.02 would be changed by November 30, 1980,

to incorporate documentation of the recirculation sample system

and the RWCU system leakage monitoring results.

This item is unresolved pending completion of licensee action

on this item and subsequent review by the NRC (URI 50-271/80-17-08).

(19) Item 2.1.8.b (III.D.3.3) Inplant Radiation Moriitoring

Requirement:: References (i),(ii),(vi)and(viii)

r

Provide interim method for quantifying high level releases

+

of up to 10'+ ci/sec for noble gases from all potential

release points.

Capability for effluent monitorin'g of radiciodines shall

+

be provided with sampling conducted by absorption on

charcoal, followed by onsite laboratory analysis.

+

If control room read-out of high range monitors is not

practical for implementation of interim measures, in-situ

reading by a individual with verbal communications with the

control room is acceptable. Measures shall also then include

procedures to minimize personnel exposures and the capability

to obtain radiation readings at least every 15 minutes.

Licensee Commitments:

References (iv) and (v)

By letter dated January 8, 1980, the licensee stated interim

+

procedures and equipment were provided to quantify high level

releases. A dedicated RM-16 installed at the base of the stack,

used in conjunction with stack flow rates, can be converted

to a release rate. Techniques for taking measurements, per-

forming analyses and minimizing personnel exposures are incor-

porated in newly developed procedures. Analysis can be per-

formed in the plant counting laboratory, with backup capability

at Yankee Rowe and the Westborough facility.

.

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Inspection Findings

Modifications in progress to meet the long term requirements

for augmented radiation monitoring are being done in accordance

W.th EDCR 80-28, Gaseous Radiation Monitor, dated September 25,

1980. The new system will provide monitoring for stack gas

effluents over the range of 1E-7 uci/cc to 1E+5 uci/cc. A new

ion chamber will be installed in the existing stack gas effluent

monitor line, upstream of the existing lower range monitor, in the

stack house at the base of the stack.

One decade overlap with

existing monitors will be provided, with control room readout

in the range of 0.1 mR/hr to IE+7 mR/hr.

Discussions with

licensee personnel indicate that current schedules for completing

this item by January 1, 1981, may not be met.

Procedure OP 3530, Post Accident Sampling, Revision 0, dated

December 31, 1979, contains the necessary instructions for

obtaining samples with the interim equipment. The capability

for measuring radiciodines using portable instrumentation

(SAM II) is described in section 4 of OP 3530, as well as in

OP 3013, for use by the offsite monitoring teams.

Fe310 wing review of plant systems and structures, the only release

point considered for the source of high level releases was the

plant stack. A dedicated RM-16 was installed in the stack house

with the HP 210 probe of the monitor positioned to measure the

dose rate along a 1 foot section of the existing gas effluent

monitor sample return line. The detector probe and portions of

the effluent monitor return line are shielded by eight inches of

lead bricks. The RM-16 is powered normally by connection to

panel LP1AE which is powered from MCC 8A. MCC 8A is powered from

4160V bus No. 3 through station service transformer T-8 and 480V

bus No. 8.

Bus No. 3 is carried by the B Diesel generator on

loss of normal power. The RM-16 monitor also has battery power

as a backup supply.

Two batteries are supplied with each battery

capable of supplying power for two days.

The read-out range of the RM-16 was verified as 0.2 mR/hr to 2000

mR/hr, corresponding to a stack release rate in the range of

26 ci/sec to 147,000 ci/sec.

Comparison with the existing stack

gas monitors shows that a gap exists in the ranges of the

instruments, between 0.75 ci/sec to 26 ci/sec.

(Themonitors

installed under EDCR 80-28 will eliminate this discrepancy).

Instructions and curves

in OP 3530 also allow conversion of

RM-16 readings to effluent release concentrations (uci/cc), with

considerations for isotopic mix and time after reactor shutdown

accounted for. The inspector reviewed the bases for the RM-16

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release conceritration conversions curvesInich Wire ~ derived

~

--

~

,

.

from shielding calEuiitions o5 Fi~ foot section of staihEss

steel sample line.

'

The inspector noted that a Gai-tronics unit is available at

the stack house to allow direct comunication with the control

room.

Backup means of comunications is also available through

the use of walkie-talkies.

Calibration of the RM-16 is provided for by OP 4560, Calibration

of RM-16, Revision 2, dated April 16, 1980.

Check sources are

used to verify check points of 1 mR/hr, 10 mR/hr and 100 mR/hr

along the detector range.

Calibration frequency for the RM-16

is specified as semi-annual by 0P 4540.

'

During inspector review of the stack facilities on November 4, 1980,

water was noted dripping through a stack house wall penetration

onto the top of the RM-16 electronics unit. This information

was imediately reported to plant personnel for corrective

action.

No inadequacies were identified. The inspector had no further

coment on this item.

(20) Item 2.1.8.c (III.D.3.3) Iodine Measurements

Requirements: References (i),(ii),(vi)and(vii)

+

Provide interim method for measuring radiciodines following

an accident using portable sampling equipment with a single

'

channel analyzer.

Licensee Comitment:

References (iv) and (v)

+

By letter dated January 8, 1980, VY stated equipment and

procedures exist to measure radiciodines in the concentrations

of interest following an accident. MCAs are available to

monitor a charcoal sampling medium.

The analyzers can detect

,

iodine in the presence of noble gases.

Plant procedures

!

describe methods in the presence of gross activity levels,

which involve clearing the samples of noble gases by purging

with clean air.

Inspection Findings

The inspector found that instructions for obtaining and analyzing

radioiodine samples were provided in procedures OP 3530, OP 3013,

!

.

. .

.

_

.

. _

+

v

54

OP 3010 and OP 2511,

In addition to use of the onsite MCA

and counting facilities, instructions were provided in OP 3530

for the use of portable single channel analyzers (SAM II) units.

Set-up, calibration and use of the SAM II detectors were discussed

with licensee personnel.

No inadequacies were identified.

Instructions and precautions for limiting personnel exposures

were given in the referenced procedures.

Previous inspector review of this item is documented in NRC

Region I Inspection Reports 50-271/80-09 and 50-271/80-13.

The inspector had no further comment on this item.

14. , Unresolved Items

Unresolved items are items about which more information is required to

ascertain whether thev are acceptable items, items! of noncompliance, or

deviations. Unresolved items are discussed in paragraph 12ea, 13.b and

13.d of this inspection report.

15. Management Meetings

During the period of the inspection, licensee management was periodically

notified of the preliminary findings by the resident inspectors. A summary

was also provided at the conclusion of the inspection and prior to report

issuance. Additionally, the resident inspectors attended the exit interview

on October 31, 1980, conducted by a region-based inspector in regard to an

inspection of the licensee's inservice inspectior, and outage modification

programs,

l

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