05000327/LER-1981-018-03, /03L-0:on 810205,discovered That SI-137.2,RCS Water Inventory,Not Performed within 72-h Per Surveillance Requirements.Caused by Steady State Conditions Not Being Established Long Enough for Performance Before Reactor Trip

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/03L-0:on 810205,discovered That SI-137.2,RCS Water Inventory,Not Performed within 72-h Per Surveillance Requirements.Caused by Steady State Conditions Not Being Established Long Enough for Performance Before Reactor Trip
ML19347D240
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 03/04/1981
From: Kirk G, Mcgriff J
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19347D239 List:
References
LER-81-018-03L, LER-81-18-3L, NUDOCS 8103110535
Download: ML19347D240 (1)


LER-1981-018, /03L-0:on 810205,discovered That SI-137.2,RCS Water Inventory,Not Performed within 72-h Per Surveillance Requirements.Caused by Steady State Conditions Not Being Established Long Enough for Performance Before Reactor Trip
Event date:
Report date:
3271981018R03 - NRC Website

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O 2 l On 02-05-81. review of survefil mnce' inst uce f nna discovered ehne ST-137.2. Rr"i weer Q l Inventory. Vas not perforiced i thin 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />'as recuired by surveillance requirement

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SI-137.'2 was performed on 01-23-81 at 0510 (c) and not perYormed anain until

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