05000324/LER-1980-103-03, /03L-0:on 801118,during Reactor Startup While Investigating Cause of Speed Indication Problems W/Reactor Recirculation Pump 2A,pump Motor Generator Unit Tripped. Caused by Technician Inadvertently Shorting Electrical Lead

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/03L-0:on 801118,during Reactor Startup While Investigating Cause of Speed Indication Problems W/Reactor Recirculation Pump 2A,pump Motor Generator Unit Tripped. Caused by Technician Inadvertently Shorting Electrical Lead
ML19345E170
Person / Time
Site: Brunswick 
Issue date: 12/18/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19345E165 List:
References
LER-80-103-03L, LER-80-103-3L, NUDOCS 8012230373
Download: ML19345E170 (1)


LER-1980-103, /03L-0:on 801118,during Reactor Startup While Investigating Cause of Speed Indication Problems W/Reactor Recirculation Pump 2A,pump Motor Generator Unit Tripped. Caused by Technician Inadvertently Shorting Electrical Lead
Event date:
Report date:
3241980103R03 - NRC Website

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U.S. NUCLEAR REGULATORY COW.13SSION NRC FOHM 366 (7 771 LICENSEE EVENT REPORT A

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[ Reactor Recirculation Pump 2A, in order to determine the cause of speed indication i

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. CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS h li l o l l This event occurred because a maintenance technician inadvertent 1v shorted an elec-I trical lead in the pump control loop circuitry which tripped the motor generator unit.g g

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