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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029E3351994-05-10010 May 1994 LER 94-006-00:on 940415,both Trains of CREVS Declared Inoperable.Caused by Tornado Warning & Sighting of Tornado Moving Toward Plant.Tornado Warnings downgraded.W/940510 Ltr ML20029E2021994-05-0909 May 1994 LER 94-004-00:on 940408,determined That TS Pressurizer Cooldown Limit Exceeded on 930618 & Not Restored within Required Timeframe.Caused by Unanticipated Sys Interaction. SI for Check Valve Opening Tests revised.W/940509 Ltr ML20029D8151994-05-0303 May 1994 LER 94-005-00:on 940403,inadvertent Fwis Occurred.Caused by Personnel Failure to Follow Work Document Instructions. Corrective Action:Individuals Were Counseled on Requirements to Follow Work Document Instruction steps.W/940503 Ltr ML20046B8351993-07-30030 July 1993 LER 93-017-00:on 930621,discovered 24-hour Telephone Notification Had Not Been Carried Out as Required by TS LCO 3.7.11.1 Action Statement (b)(2)(a) Due to Personnel Error. NRC Informed of Missed notification.W/930730 Ltr ML20046B8501993-07-30030 July 1993 LER 93-018-00:on 930704,DG Started Due to Improper WO Planning.Restored Power to 1BB Shutdown Board & Stopped Running DGs.W/930730 Ltr ML20046A4691993-07-19019 July 1993 LER 93-016-00:on 930619,Phase A,Auxiliary Bldg & Containment Isolations Manually Initiated as Result of Fuel Assembly Failing to Remain in Upright Position After Being Released. All Fuel Movement stopped.W/930719 Ltr ML20045J0111993-07-14014 July 1993 LER 93-015-00:on 930614,1A Start Bus Alternate Feeder Breaker Tripped Upon Start of Unit 1 RCP Which Resulted in Start of DG Due to Current Transformer Wired Incorrectly. Restored Offsite Power & Secured Final DG.W/930714 Ltr ML20045H0171993-07-12012 July 1993 LER 93-014-00:on 930611,determined That Inadequate Ventilation Design Resulted in Potential Inoperability of Vital Power Equipment.Design Being modified.W/930712 Ltr ML20045B9951993-06-15015 June 1993 LER 93-004-01:on 930222,determined That Blind Flange on Elevation 734 Personnel Airlock Outer Housing Leaking.Due to Improper Installation of Blind Flange.Evaluation Performed of Other 14 Double O-ring Blind flanges.W/930615 Ltr ML20045B9311993-06-10010 June 1993 LER 93-013-00:on 930514,fire Watch Was Not Performed within Time Frame Required by Tech Specs Due to Inadequate Supervision by Fire Protection Foreman.Fire Watch Patrol reestablished.W/930610 Ltr ML20045A7261993-06-0707 June 1993 LER 93-011-00:on 930507,discovered That Fire Barrier Breached W/O Proper Compensatory Measures Established.On 930505,door Leading to Room Housing Containment Spray HX 1A Breached.Roving Fire Watch Established & LCO 3.7.12 Entered ML20044H4501993-06-0303 June 1993 LER 93-012-00:on 930504,apparent Failure to Properly Identify & Plug SG Tube Determined to Exceed TS Plugging Limit.Caused by eddy-current Coordinator Not Ensuring Task requirements.Eddy-current Procedure revised.W/930603 Ltr ML20044H1561993-05-28028 May 1993 LER 93-010-00:on 930430,Westinghouse Identified Error in Development of Calculations for Cold Overpressure Mitigation Sys Setpoints.Caused by Vendor Failure to Consider Elevation Difference.Engineering Evaluation Performed ML20044E6341993-05-17017 May 1993 LER 93-009-00:on 930417,TS Surveillance Not Performed for Three Pipe Support Snubbers Because of Omission of Snubbers from Surveillance Instruction for Visual Insp.Snubbers Visually Inspected & Functionally tested.W/930517 Ltr ML20044B6751993-02-23023 February 1993 LER 93-001-00:on 930124,Unit 1 Ice Bed Temperature Recorder in MCR Declared Inoperable.Caused by Ineffective Communication.Appropriate Personnel Involved W/Event Have Been counseled.W/930223 Ltr ML20044B6141993-01-21021 January 1993 LER 92-026-00:on 921222,determined That Several ASME Section XI Pressure Tests Not Performed Due to Section XI Program Implementation Not Being well-defined,controlled or Documented.Test Expeditiously performed.W/930121 Ltr ML20024H2441991-05-22022 May 1991 LER 91-007-00:on 910422,LCO 3.0.3 Entered When Shaft of Train a Main Control Room Air Handling Unit Failed from Fatigue & Train B Out of Svc for Maint.Caused by Shaft Misalignment.New Shaft installed.W/910522 Ltr ML20029C1761991-03-21021 March 1991 LER 91-002-00:on 910211,unit Operated in Condition Prohibited by Tech Spec 3.3.3.8 Limiting Condition for Operation.Cause Under Investigation.Night Order Issued to Personnel Re Removal of Equipment from svc.W/910321 Ltr ML20029C1231991-03-18018 March 1991 LER 90-016-01:on 901117,determined That Calibr of Nuclear Instrumentation Sys intermediate-range Channels Set Nonconservatively.Caused by Lack of Operability Control for Rod Motion.Action Plan developed.W/910318 Ltr ML20029A6711991-02-25025 February 1991 LER 91-002-00:on 910124,LCOs 3.0.5 & 3.8.1.1 Entered When Both Trains of Emergency Gas Treatment Sys Declared Inoperable.Caused by Blown Fuse & Excessive Cycling of Air Start Sys.Fuse replaced.W/910225 Ltr ML20028H0331990-09-27027 September 1990 LER 90-019-00:on 900828,failure to Update P-250 Plant Computer Constants Resulted in Axial Flux Difference.Caused by Inadequate Procedures & Inappropriate Personnel Actions. Procedure 0-PI-NXX-092-001.0 revised.W/900927 Ltr ML20028G9201990-09-26026 September 1990 LER 90-020-00:on 900829,ventilation Sys Inoperable Due to Train B Diesel Generator Out of Svc.Caused by Stuck Microswitch Contacts on Pressure Switch 0-PS-311-172. Pressure Switch Adjusted & Returned to svc.W/900926 Ltr ML20044A9361990-07-0909 July 1990 LER 90-011-00:on 900608,determined That Actual Nuclear Instrumentation Sys Power Range Detector Currents Were 20% to 31% Lower than Predicted.Caused by Calibr Values Being Incorrectly Calculated.Channels corrected.W/900709 Ltr ML20044A3241990-06-25025 June 1990 LER 90-010-00:on 900526,limiting Condition for Operation Entered Because MSIV Failed to Close When Another MSIV Inoperable for Maint.Cause Attributed to Valve Stem & Valve Guide Binding.Operations Training Ltr issued.W/900625 Ltr ML20043H5091990-06-21021 June 1990 LER 90-009-00:on 900527,automatic Start of Auxiliary Feedwater Pumps Occurred When Both Main Feedwater Pumps Placed in Tripped Condition.Caused by Personnel Error.Trip Circuitry Reset & Operators counseled.W/900621 Ltr ML20043E5401990-06-0707 June 1990 LER 90-008-00:on 900514,two Control Room Isolations Occurred as Result of Spurious Spikes.Caused by Loose Terminations on Relay Socket.Loose Connections Properly terminated.W/900607 Ltr ML20043A4211990-05-16016 May 1990 LER 90-010-00:on 900416,containment Ventilation Isolation Occurred.Caused by Allowing Gaseous Radiation Level to Increase Too Close to Alarm Setpoint.Recovery from Isolation initiated.W/900516 Ltr ML20043A2261990-05-14014 May 1990 LER 90-009-00:on 900404,lower Containment Radiation Monitor Found Inoperable & Lower Containment Atmosphere Aligned to Upper Containment Radiation Monitor During Sampling.Caused by Personnel Error.Chemistry Training revised.W/900514 Ltr ML20043A2271990-05-14014 May 1990 LER 90-006-00:on 900414,auxiliary Bldg Isolation Occurred from Spent Fuel Pit Area Radiation Monitors 0-RM-90-102 & 103.Caused by Personnel Error.Training Ltr Issued to Instrument Mechanics & Operations personnel.W/900514 Ltr ML20043A2201990-05-14014 May 1990 LER 90-007-00:on 900413,discovered That Tech Spec Surveillance Requirement Not Performed within Required Interval.Caused by Personnel Error.Surveillance Successfully Performed Since missed.W/900514 Ltr ML20042G7861990-05-0909 May 1990 LER 90-005-00:on 900409,emergency Start of Four Emergency Diesel Generators Occurred While Attempting Transfer of Power.Caused by Personnel Error.Individuals Reprimanded, Training Initiated & Procedures revised.W/900509 Ltr ML20042G7931990-05-0909 May 1990 LER 90-008-00:on 900410,reactor Trip Occurred Resulting from General Warning Alarm on Both Trains of Solid State Protection Sys.Caused by Personnel Error.Individuals Disciplined & Site Wide Message distributed.W/900509 Ltr ML20042F3741990-05-0202 May 1990 LER 90-003-00:on 900404,control Room Ventilation Sys (CRVS) Transferred to Pressurization Mode.Caused by Electrical Transient in Vital Instrument Ac Bus PY-21A.CRVS Reset & Returned to Normal Operating modes.W/900502 Ltr ML20042E4191990-04-13013 April 1990 LER 90-007-00:on 900317 & 26,containment Ventilation Isolations Occurred During Purge Activities.Caused by Inadequate Procedural Guidance for Setpoint Determination. Alarm & Trip Setpoints increased.W/900413 Ltr ML20042E2021990-04-13013 April 1990 LER 90-005-00:on 900315,inadvertent Containment Vent Isolation Occurred While Preparing to Purge Containment. Caused by Lack of Attention to Detail by Operator.Operator Counseled & Received Administrative reprimand.W/900413 Ltr ML20012F5221990-04-0505 April 1990 LER 90-006-00:on 900307,containment Ventilation Isolation Occurred.Caused by Containment Particulate Level Too Close to Setpoint.Module Replaced.Radiation Alarm Setpoint Increased from 10% to 40% of Tech Spec limit.W/900406 Ltr ML20012D8611990-03-23023 March 1990 LER 90-004-00:on 900221,handswitches Controlling Operation of Isolation Valves on Steam Supply Line to Auxiliary Feedwater Pump Found in Manual Position.Cause Undetermined. Handswitches Placed in P-auto position.W/900323 Ltr ML20012C4271990-03-12012 March 1990 LER 90-003-00:on 900211,inadvertent Containment Vent Isolation Occurred.Caused by Lack of Attention to Detail in That Operator Did Not Look Closely Enough at Switch Designations.Personnel Involved counseled.W/900312 Ltr ML20011F7191990-03-0101 March 1990 LER 89-031-01:on 891205,RHR Pumps Determined to Have Deadheading Problem Identified by NRC Bulletin 88-004.Caused by Inadequate Technical Response to Bulletin.Training Ltr Issued to 10CFR50.59 reviewers.W/900301 Ltr ML20011F7421990-02-26026 February 1990 LER 90-002-00:on 900127,control Room Isolation Occurred When Circuit Breaker Opened Supplying Power to Radiation Monitor. Caused by Failure by Personnel to Exercise Sufficient Caution.Responsible Engineers reinstructed.W/900226 Ltr ML20011F7391990-02-26026 February 1990 LER 90-002-00:on 891122,value for Distance from Floor to Ctr Line of Level Switch 2-LS-87-21 Transposed in Variable Leg Calculation.Caused by Inattention to Detail.Procedure Revised to Replace Incorrect setpoint.W/900226 Ltr ML20006E3311990-02-0909 February 1990 LER 90-001-00:on 900112,Limiting Condition for Operation 3.0.3 Entered When Three of Four Lower Compartment Cooler Fan Motors Exceeded Lubrication Frequency.Caused by Personnel Error.Personnel counseled.W/900209 Ltr ML20006D5341990-02-0707 February 1990 LER 90-001-00:on 900108,discovered That Several ERCW Valves Not Being Periodically Verified to Be Correct.Caused by Personnel Error During Procedure Revs & Workplan Reviews. Info Notice Issued to Workplan reviewers.W/900207 Ltr ML19354E1631990-01-22022 January 1990 LER 89-036-00:on 891221,discovered That Surveillance Test Results Used for Declaring Diesel Generator 1B-B Operable Deficient.Caused by Instruction Not Including 60 Minute Run Time.Event Will Be Reviewed w/supervisors.W/900122 Ltr ML19354D8941990-01-16016 January 1990 LER 89-034-00:on 891215,leak Identified from Fitting on Vol Control Tank Level Transmitter & Auxiliary Bldg Evacuated, Preventing Fire Watch Patrol from Entering Bldg for Hourly Rounds.Fitting tightened.W/900116 Ltr ML19354D9061990-01-16016 January 1990 LER 89-033-00:on 891216,refueling Water Storage Tank Level Transmitters Failed High Due to Freezing from Extremely Cold Weather & Inappropriate Use of Calculations.Engineering Procedures Revised & Heating Installed in encl.W/900116 Ltr ML20005F8851990-01-0909 January 1990 LER 89-035-00:on 891210,turbine/reactor Trip Occurred from hi-hi Feedwater Level of 75% in Steam Generator 3.Caused by Failure of Loop 3 Main Feedwater Regulating Valve to Close. Equipment Adjusted & repaired.W/900109 Ltr ML20005E0801989-12-22022 December 1989 LER 89-032-00:on 891205,RHR Pumps Determined to Have Deadheading Problem,Per NRC Bulletin 88-004,resulting in Plant Operation Outside Design Basis.On 891128,RHR Pump Exceeded Head Criteria.Pumps started.W/891222 Ltr ML20005E0831989-12-22022 December 1989 LER 89-032-00:on 891201,discovered That Tech Spec Surveillance Requirement to Verify That Valves 1-67-748 & 2-67-748 in Open Position Not Met.Caused by Personnel Error.Correct Valve Position verified.W/891222 Ltr ML20005E1161989-12-22022 December 1989 LER 89-030-00:on 891204,fire Suppression Sys Deluge Valve Isolated More than 1 H W/O Required Continuous Fire Watch Establishment.Caused by Personal Communication Breakdown. Valve Opened & Foreman in Charge counseled.W/891222 Ltr 1994-05-09
[Table view] Category:RO)
MONTHYEARML20029E3351994-05-10010 May 1994 LER 94-006-00:on 940415,both Trains of CREVS Declared Inoperable.Caused by Tornado Warning & Sighting of Tornado Moving Toward Plant.Tornado Warnings downgraded.W/940510 Ltr ML20029E2021994-05-0909 May 1994 LER 94-004-00:on 940408,determined That TS Pressurizer Cooldown Limit Exceeded on 930618 & Not Restored within Required Timeframe.Caused by Unanticipated Sys Interaction. SI for Check Valve Opening Tests revised.W/940509 Ltr ML20029D8151994-05-0303 May 1994 LER 94-005-00:on 940403,inadvertent Fwis Occurred.Caused by Personnel Failure to Follow Work Document Instructions. Corrective Action:Individuals Were Counseled on Requirements to Follow Work Document Instruction steps.W/940503 Ltr ML20046B8351993-07-30030 July 1993 LER 93-017-00:on 930621,discovered 24-hour Telephone Notification Had Not Been Carried Out as Required by TS LCO 3.7.11.1 Action Statement (b)(2)(a) Due to Personnel Error. NRC Informed of Missed notification.W/930730 Ltr ML20046B8501993-07-30030 July 1993 LER 93-018-00:on 930704,DG Started Due to Improper WO Planning.Restored Power to 1BB Shutdown Board & Stopped Running DGs.W/930730 Ltr ML20046A4691993-07-19019 July 1993 LER 93-016-00:on 930619,Phase A,Auxiliary Bldg & Containment Isolations Manually Initiated as Result of Fuel Assembly Failing to Remain in Upright Position After Being Released. All Fuel Movement stopped.W/930719 Ltr ML20045J0111993-07-14014 July 1993 LER 93-015-00:on 930614,1A Start Bus Alternate Feeder Breaker Tripped Upon Start of Unit 1 RCP Which Resulted in Start of DG Due to Current Transformer Wired Incorrectly. Restored Offsite Power & Secured Final DG.W/930714 Ltr ML20045H0171993-07-12012 July 1993 LER 93-014-00:on 930611,determined That Inadequate Ventilation Design Resulted in Potential Inoperability of Vital Power Equipment.Design Being modified.W/930712 Ltr ML20045B9951993-06-15015 June 1993 LER 93-004-01:on 930222,determined That Blind Flange on Elevation 734 Personnel Airlock Outer Housing Leaking.Due to Improper Installation of Blind Flange.Evaluation Performed of Other 14 Double O-ring Blind flanges.W/930615 Ltr ML20045B9311993-06-10010 June 1993 LER 93-013-00:on 930514,fire Watch Was Not Performed within Time Frame Required by Tech Specs Due to Inadequate Supervision by Fire Protection Foreman.Fire Watch Patrol reestablished.W/930610 Ltr ML20045A7261993-06-0707 June 1993 LER 93-011-00:on 930507,discovered That Fire Barrier Breached W/O Proper Compensatory Measures Established.On 930505,door Leading to Room Housing Containment Spray HX 1A Breached.Roving Fire Watch Established & LCO 3.7.12 Entered ML20044H4501993-06-0303 June 1993 LER 93-012-00:on 930504,apparent Failure to Properly Identify & Plug SG Tube Determined to Exceed TS Plugging Limit.Caused by eddy-current Coordinator Not Ensuring Task requirements.Eddy-current Procedure revised.W/930603 Ltr ML20044H1561993-05-28028 May 1993 LER 93-010-00:on 930430,Westinghouse Identified Error in Development of Calculations for Cold Overpressure Mitigation Sys Setpoints.Caused by Vendor Failure to Consider Elevation Difference.Engineering Evaluation Performed ML20044E6341993-05-17017 May 1993 LER 93-009-00:on 930417,TS Surveillance Not Performed for Three Pipe Support Snubbers Because of Omission of Snubbers from Surveillance Instruction for Visual Insp.Snubbers Visually Inspected & Functionally tested.W/930517 Ltr ML20044B6751993-02-23023 February 1993 LER 93-001-00:on 930124,Unit 1 Ice Bed Temperature Recorder in MCR Declared Inoperable.Caused by Ineffective Communication.Appropriate Personnel Involved W/Event Have Been counseled.W/930223 Ltr ML20044B6141993-01-21021 January 1993 LER 92-026-00:on 921222,determined That Several ASME Section XI Pressure Tests Not Performed Due to Section XI Program Implementation Not Being well-defined,controlled or Documented.Test Expeditiously performed.W/930121 Ltr ML20024H2441991-05-22022 May 1991 LER 91-007-00:on 910422,LCO 3.0.3 Entered When Shaft of Train a Main Control Room Air Handling Unit Failed from Fatigue & Train B Out of Svc for Maint.Caused by Shaft Misalignment.New Shaft installed.W/910522 Ltr ML20029C1761991-03-21021 March 1991 LER 91-002-00:on 910211,unit Operated in Condition Prohibited by Tech Spec 3.3.3.8 Limiting Condition for Operation.Cause Under Investigation.Night Order Issued to Personnel Re Removal of Equipment from svc.W/910321 Ltr ML20029C1231991-03-18018 March 1991 LER 90-016-01:on 901117,determined That Calibr of Nuclear Instrumentation Sys intermediate-range Channels Set Nonconservatively.Caused by Lack of Operability Control for Rod Motion.Action Plan developed.W/910318 Ltr ML20029A6711991-02-25025 February 1991 LER 91-002-00:on 910124,LCOs 3.0.5 & 3.8.1.1 Entered When Both Trains of Emergency Gas Treatment Sys Declared Inoperable.Caused by Blown Fuse & Excessive Cycling of Air Start Sys.Fuse replaced.W/910225 Ltr ML20028H0331990-09-27027 September 1990 LER 90-019-00:on 900828,failure to Update P-250 Plant Computer Constants Resulted in Axial Flux Difference.Caused by Inadequate Procedures & Inappropriate Personnel Actions. Procedure 0-PI-NXX-092-001.0 revised.W/900927 Ltr ML20028G9201990-09-26026 September 1990 LER 90-020-00:on 900829,ventilation Sys Inoperable Due to Train B Diesel Generator Out of Svc.Caused by Stuck Microswitch Contacts on Pressure Switch 0-PS-311-172. Pressure Switch Adjusted & Returned to svc.W/900926 Ltr ML20044A9361990-07-0909 July 1990 LER 90-011-00:on 900608,determined That Actual Nuclear Instrumentation Sys Power Range Detector Currents Were 20% to 31% Lower than Predicted.Caused by Calibr Values Being Incorrectly Calculated.Channels corrected.W/900709 Ltr ML20044A3241990-06-25025 June 1990 LER 90-010-00:on 900526,limiting Condition for Operation Entered Because MSIV Failed to Close When Another MSIV Inoperable for Maint.Cause Attributed to Valve Stem & Valve Guide Binding.Operations Training Ltr issued.W/900625 Ltr ML20043H5091990-06-21021 June 1990 LER 90-009-00:on 900527,automatic Start of Auxiliary Feedwater Pumps Occurred When Both Main Feedwater Pumps Placed in Tripped Condition.Caused by Personnel Error.Trip Circuitry Reset & Operators counseled.W/900621 Ltr ML20043E5401990-06-0707 June 1990 LER 90-008-00:on 900514,two Control Room Isolations Occurred as Result of Spurious Spikes.Caused by Loose Terminations on Relay Socket.Loose Connections Properly terminated.W/900607 Ltr ML20043A4211990-05-16016 May 1990 LER 90-010-00:on 900416,containment Ventilation Isolation Occurred.Caused by Allowing Gaseous Radiation Level to Increase Too Close to Alarm Setpoint.Recovery from Isolation initiated.W/900516 Ltr ML20043A2261990-05-14014 May 1990 LER 90-009-00:on 900404,lower Containment Radiation Monitor Found Inoperable & Lower Containment Atmosphere Aligned to Upper Containment Radiation Monitor During Sampling.Caused by Personnel Error.Chemistry Training revised.W/900514 Ltr ML20043A2271990-05-14014 May 1990 LER 90-006-00:on 900414,auxiliary Bldg Isolation Occurred from Spent Fuel Pit Area Radiation Monitors 0-RM-90-102 & 103.Caused by Personnel Error.Training Ltr Issued to Instrument Mechanics & Operations personnel.W/900514 Ltr ML20043A2201990-05-14014 May 1990 LER 90-007-00:on 900413,discovered That Tech Spec Surveillance Requirement Not Performed within Required Interval.Caused by Personnel Error.Surveillance Successfully Performed Since missed.W/900514 Ltr ML20042G7861990-05-0909 May 1990 LER 90-005-00:on 900409,emergency Start of Four Emergency Diesel Generators Occurred While Attempting Transfer of Power.Caused by Personnel Error.Individuals Reprimanded, Training Initiated & Procedures revised.W/900509 Ltr ML20042G7931990-05-0909 May 1990 LER 90-008-00:on 900410,reactor Trip Occurred Resulting from General Warning Alarm on Both Trains of Solid State Protection Sys.Caused by Personnel Error.Individuals Disciplined & Site Wide Message distributed.W/900509 Ltr ML20042F3741990-05-0202 May 1990 LER 90-003-00:on 900404,control Room Ventilation Sys (CRVS) Transferred to Pressurization Mode.Caused by Electrical Transient in Vital Instrument Ac Bus PY-21A.CRVS Reset & Returned to Normal Operating modes.W/900502 Ltr ML20042E4191990-04-13013 April 1990 LER 90-007-00:on 900317 & 26,containment Ventilation Isolations Occurred During Purge Activities.Caused by Inadequate Procedural Guidance for Setpoint Determination. Alarm & Trip Setpoints increased.W/900413 Ltr ML20042E2021990-04-13013 April 1990 LER 90-005-00:on 900315,inadvertent Containment Vent Isolation Occurred While Preparing to Purge Containment. Caused by Lack of Attention to Detail by Operator.Operator Counseled & Received Administrative reprimand.W/900413 Ltr ML20012F5221990-04-0505 April 1990 LER 90-006-00:on 900307,containment Ventilation Isolation Occurred.Caused by Containment Particulate Level Too Close to Setpoint.Module Replaced.Radiation Alarm Setpoint Increased from 10% to 40% of Tech Spec limit.W/900406 Ltr ML20012D8611990-03-23023 March 1990 LER 90-004-00:on 900221,handswitches Controlling Operation of Isolation Valves on Steam Supply Line to Auxiliary Feedwater Pump Found in Manual Position.Cause Undetermined. Handswitches Placed in P-auto position.W/900323 Ltr ML20012C4271990-03-12012 March 1990 LER 90-003-00:on 900211,inadvertent Containment Vent Isolation Occurred.Caused by Lack of Attention to Detail in That Operator Did Not Look Closely Enough at Switch Designations.Personnel Involved counseled.W/900312 Ltr ML20011F7191990-03-0101 March 1990 LER 89-031-01:on 891205,RHR Pumps Determined to Have Deadheading Problem Identified by NRC Bulletin 88-004.Caused by Inadequate Technical Response to Bulletin.Training Ltr Issued to 10CFR50.59 reviewers.W/900301 Ltr ML20011F7421990-02-26026 February 1990 LER 90-002-00:on 900127,control Room Isolation Occurred When Circuit Breaker Opened Supplying Power to Radiation Monitor. Caused by Failure by Personnel to Exercise Sufficient Caution.Responsible Engineers reinstructed.W/900226 Ltr ML20011F7391990-02-26026 February 1990 LER 90-002-00:on 891122,value for Distance from Floor to Ctr Line of Level Switch 2-LS-87-21 Transposed in Variable Leg Calculation.Caused by Inattention to Detail.Procedure Revised to Replace Incorrect setpoint.W/900226 Ltr ML20006E3311990-02-0909 February 1990 LER 90-001-00:on 900112,Limiting Condition for Operation 3.0.3 Entered When Three of Four Lower Compartment Cooler Fan Motors Exceeded Lubrication Frequency.Caused by Personnel Error.Personnel counseled.W/900209 Ltr ML20006D5341990-02-0707 February 1990 LER 90-001-00:on 900108,discovered That Several ERCW Valves Not Being Periodically Verified to Be Correct.Caused by Personnel Error During Procedure Revs & Workplan Reviews. Info Notice Issued to Workplan reviewers.W/900207 Ltr ML19354E1631990-01-22022 January 1990 LER 89-036-00:on 891221,discovered That Surveillance Test Results Used for Declaring Diesel Generator 1B-B Operable Deficient.Caused by Instruction Not Including 60 Minute Run Time.Event Will Be Reviewed w/supervisors.W/900122 Ltr ML19354D8941990-01-16016 January 1990 LER 89-034-00:on 891215,leak Identified from Fitting on Vol Control Tank Level Transmitter & Auxiliary Bldg Evacuated, Preventing Fire Watch Patrol from Entering Bldg for Hourly Rounds.Fitting tightened.W/900116 Ltr ML19354D9061990-01-16016 January 1990 LER 89-033-00:on 891216,refueling Water Storage Tank Level Transmitters Failed High Due to Freezing from Extremely Cold Weather & Inappropriate Use of Calculations.Engineering Procedures Revised & Heating Installed in encl.W/900116 Ltr ML20005F8851990-01-0909 January 1990 LER 89-035-00:on 891210,turbine/reactor Trip Occurred from hi-hi Feedwater Level of 75% in Steam Generator 3.Caused by Failure of Loop 3 Main Feedwater Regulating Valve to Close. Equipment Adjusted & repaired.W/900109 Ltr ML20005E0801989-12-22022 December 1989 LER 89-032-00:on 891205,RHR Pumps Determined to Have Deadheading Problem,Per NRC Bulletin 88-004,resulting in Plant Operation Outside Design Basis.On 891128,RHR Pump Exceeded Head Criteria.Pumps started.W/891222 Ltr ML20005E0831989-12-22022 December 1989 LER 89-032-00:on 891201,discovered That Tech Spec Surveillance Requirement to Verify That Valves 1-67-748 & 2-67-748 in Open Position Not Met.Caused by Personnel Error.Correct Valve Position verified.W/891222 Ltr ML20005E1161989-12-22022 December 1989 LER 89-030-00:on 891204,fire Suppression Sys Deluge Valve Isolated More than 1 H W/O Required Continuous Fire Watch Establishment.Caused by Personal Communication Breakdown. Valve Opened & Foreman in Charge counseled.W/891222 Ltr 1994-05-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212J6311999-10-0101 October 1999 SER Accepting Request for Relief from ASME Boiler & Pressure Vessel Code,Section Xi,Requirements for Certain Inservice Insp at Plant,Unit 1 ML20217G3721999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Sequoyah Nuclear Plant.With ML20212F0831999-09-23023 September 1999 Safety Evaluation Granting Relief from Certain Weld Insp at Sequoyah Nuclear Plant,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(ii) for Second 10-year ISI Interval ML20212F4761999-09-23023 September 1999 Safety Evaluation Supporting Amends 246 & 237 to Licenses DPR-77 & DPR-79,respectively ML20212C4761999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Sequoyah Nuclear Plant.With ML20210L4361999-08-0202 August 1999 Cycle 9 12-Month SG Insp Rept ML20216E3781999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20210L4451999-07-31031 July 1999 Unit-2 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20210G6631999-07-28028 July 1999 Cycle 9 90-Day ISI Summary Rept ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20209H3831999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Sequoyah Nuclear Plant.With ML20211F9031999-06-30030 June 1999 Cycle 9 Refueling Outage ML20196J8521999-06-28028 June 1999 Safety Evaluation Authorizing Proposed Alternative to Use Iqis for Radiography Examinations as Provided for in ASME Section III,1992 Edition with 1993 Addenda,Pursuant to 10CFR50.55a(a)(3)(i) ML20195K2951999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20206Q8951999-05-0505 May 1999 Rev 0 to L36 990415 802, COLR for Sequoyah Unit 2 Cycle 10 ML20206R5031999-04-30030 April 1999 Monthly Operating Repts for April 1999 for Sequoyah Units 1 & 2.With ML20205P9811999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20204C3111999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20205B6631999-02-28028 February 1999 Underground Storage Tank (Ust) Permanent Closure Rept, Sequoyah Nuclear Plant Security Backup DG Ust Sys ML20203H7381999-02-18018 February 1999 Safety Evaluation of Topical Rept BAW-2328, Blended U Lead Test Assembly Design Rept. Rept Acceptable Subj to Listed Conditions ML20211A2021999-01-31031 January 1999 Non-proprietary TR WCAP-15129, Depth-Based SG Tube Repair Criteria for Axial PWSCC Dented TSP Intersections ML20198S7301998-12-31031 December 1998 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept ML20199G3641998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20197J5621998-12-0303 December 1998 Unit 1 Cycle 9 90-Day ISI Summary Rept ML20197K1161998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20195F8061998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Sequoyah Nuclear Plant.With ML20154H6091998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Sequoyah Nuclear Plant,Units 1 & 2.With ML20154H6251998-09-17017 September 1998 Rev 0 to Sequoyah Nuclear Plant Unit 1 Cycle 10 Colr ML20153B0881998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Sequoyah Nuclear Plant.With ML20239A0631998-08-27027 August 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Sequoyah Nuclear Plant,Units 1 & 2 ML20236Y2091998-08-0707 August 1998 Safety Evaluation Accepting Relief Requests RP-03,RP-05, RP-07,RV-05 & RV-06 & Denying RV-07 & RV-08 ML20237B5221998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Snp ML20237A4411998-07-31031 July 1998 Blended Uranium Lead Test Assembly Design Rept ML20236P6441998-07-10010 July 1998 LER 98-S01-00:on 980610,failure of Safeguard Sys Occurred for Which Compensatory Measures Were Not Satisfied within Required Time Period.Caused by Inadequate Security Procedure.Licensee Revised Procedure MI-134 ML20236R0051998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Sequoyah Nuclear Plant ML20249A8981998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Sequoyah Nuclear Plant,Units 1 & 2 ML20247L5141998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Sequoyah Nuclear Plant ML20217K4471998-04-27027 April 1998 Safety Evaluation Supporting Requests for Relief 1-ISI-2 (Part 1),2-ISI-2 (Part 2),1-ISI-5,2-ISI-5,1-ISI-6,1-ISI-7, 2-ISI-7,ISPT-02,ISPT-04,ISPT-06,ISPT-07,ISPT-8,ISPT-01 & ISPT-05 ML20217E2221998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sequoyah Nuclear Plant ML20248L2611998-02-28028 February 1998 Monthly Operating Repts for Sequoyah Nuclear Plant,Units 1 & 2 ML20199J2571998-01-31031 January 1998 Cycle 9 Voltage-Based Repair Criteria 90-Day Rept ML20202J7911998-01-31031 January 1998 Monthly Operating Repts for Jan 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20199J2441998-01-29029 January 1998 Snp Unit 2 Cycle Refueling Outage Oct 1997 ML20199F8531998-01-13013 January 1998 ASME Section XI Inservice Insp Summary Rept for Snp Unit 2 Refueling Outage Cycle 8 ML20199A2931997-12-31031 December 1997 Revised Monthly Operating Rept for Dec 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20198M1481997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20197J1011997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Sequoyah Nuclear Plant,Units 1 & 2 ML20199C2951997-11-13013 November 1997 LER 97-S01-00:on 971017,vandalism of Electrical Cables Was Observed.Caused by Vandalism.Repaired Damaged Cables, Interviewed Personnel Having Potential for Being in Area at Time Damage Occurred & Walkdowns ML20199C7201997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Sequoyah Nuclear Plant L-97-215, SG Secondary Side Loose Object Safety Evaluation1997-10-23023 October 1997 SG Secondary Side Loose Object Safety Evaluation 1999-09-30
[Table view] |
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EVENT DESCRIPTION ANO PnCB ABLE CONSECUENCES h 4
[o ( 21 l At 1200 (c) on 11/17/80 a mode change was made from mode 3 to mode 2 with vital l gl instrument power board 2-III being powered from the maintenance power supply due to a [
1o 4 41 l f ailtrre of vital inverter 2-III. A deterriination was subsequent 1v made by the NRC ]
g I that a vital instrument board is inoperable when its vital inverter is out of service, f
[016] l Durine the oeriod of time between 11/9/80 and 11/23/80, there were a total of 9 vital l g i inverter 2-III failures. There was no effect on public health or safety. Previous l l0iAl l occurrences - 5. I SYSitu CAu$t C Au$f COv' vatvt CCCE CQct SusCODt CC88*cNENT COct Su8CCDs SueC0ct l0igj lE lD i@ W@ l A l@ l Gl El N l E l R l A l@ lF l@ g @ 19 20 2 3 9 10 13 12 IJ to
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W @lCl@ W@ l36Z l@ 10 l0 l0 l Ol l_y_j @ la2N l@ M@ lS l 3l 7l 9l JJ Jo JS 37 40 el 43 44 47 CAUSE CESCRIPr10N AND COARECTIVE ACTIONS ,
ITITl l Thd vital instrument power board had been considered coerable in sccorence with I W I Technical Specification 3.0.5. At 0935 (c) on 11/18/80, notification was received i l i F21 I from NRC that a loss of an inverter makes the corresponding vital instrument board IiiJll inoperable. For all subsequent inverter failures. the applicable' vital instrument f
, i s i n I l board has been considered inoperable until the inverter was restored.
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Name of Preparer W. T. Cottle/S. G._Ma_dd_ox Phone 615-842-8261
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Tennessee Valley Authority Sequoyah Nuclear Plant
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i LER SUPPLEMENTAL INFORMATION h
SQRO-50-327/80187 Technical Specification involved: 3.8.2.1 l
Reported Under Technical Specification 6.9.1.13.b l Dates of Occurrences: 11/09/80 Times of Occurrences: 2250 (c) 11/10/80 0325 (c) 11/10/80 1250 (c) 0246 (c) 4 11/11/80 11/16/80 2135 (c) 11/17/80 1400 (c) 11/18/80 0940 (c) 11/19/80 1000 (c) 11/23/80 1235 (c) 1 Identification and Description of Occurrences:
! During the period 11/09/80 through 11/18/80, a vital instrument power board was not considered to be inoperable upon loss of a vital inverter if the j board was immediately shifted to its alternate maintenance power supply.
The basis for this decision was Technical Specification 3.0.5 which allows
, a component or system to be considered operable if (1) the normal or emer-gency power source is operable and (2) all the redundant components or systems l.
are operable. Vital instrument power board 2-III was receiving power from the j maintenance power supply at 1200 (c) on 11/17/80, at which time a mode change
' from made 3 to made 2 was made. At 0935 (c) on 11/18/80, notification was received from NRC that Technical Specification 3.0.5 was being inappropriately appliel and that the loss of an inverter makes the associated vital instrument power beard inoperable. A commitment was made by plant management to comply with the interpretation given by NRC and all subsequent inverter failures have resulted in the applicable vital instrument power board being declared inoperable i and the appropriate Technical Specification Action Statement entered. In addition, plant management agreed to provide a Licensee Event Report detailing the failures of vital inverter 2-III.
). 1. On 11/09/80, at 2250 (c) with unit 1 in mode 4, vital inverter 2-III trip--
' ped on blower failure. Vital instrument power board 2-III was declared inoperable which resulted in entering the Action Statement of LCO 3.8.2.1.
L i
Investigation revealed a failed resistor. The resistor was repla'ed c and l
the system was declared operable on 11/10/80, at 0205 (c).
- 2. On 11/10/80, at 0325 (c)' with u nit 1 in mode 4, vital inverter 2-III trip-ped. Vital 1 atrument power board _2-III was declared inoperable which resulted in entering the Action Statement of LCO 3.8.2.1.
Investigation revealed a fuse in the clipper circuit had blown and resistor-A25R1 had failed. The fuse and resistor ~were replaced and the system was l
declared operable at 1124 (c) on 11/10/80.
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LER SUPPLEMENTAL INFORMATION (Continued) 3., On 11/10/80, at 1250 (c) with unit 1 in mode 4, vital inverter 2-III tripped. Vital instrument power board 2-III was declared inoperable
, which resulted in entering the Action Statement of LCO 3.8.2.1.
Investigation revealed that resistor A25R1 had failed. This resistor was replaced and the system was declared operable at 1730 on 11/10/80.
- 4. At 0246 (c) on 11/11/80, with onit 1 in mode 3, vital inverter 2-III
- tripped. Vital instrument power board 2-III was declared inoperable j
which resulted in entering the Action Statement of LCO 3.8.2.1.
When the inverter tripped, the vital instrument power board 2-III was immediately transferred to its maintenance supply while the vital in-verter was being repaired. Investigation revealed that the K-1 relay, RC9 temperature sensing board, and the U-9 integrated circuit located
' on the control board had failed. These parts were repladed and the 4 inverter was returned to operation at 0824 (c) on 11/11/80. At this time the vital instrument power board was still being powered from its maintenance supply and operable vital instrument power board 2-III was considered operable in accordance with the requirements of Technical Specifications 3.0.5.
On 11/12/80, at 1035 (c), vital instrument power board 2-III was removed from its maintenance supply and placed back on the vital inverter after completion of additional testing of the inverter.
- 5. At 2135 (c) on 11/16/80, vital inverter 2-III tripped. Vital instrument l power board 2-III was immediately shifted to the alternate maintenance power supply and was considered to be operable.
At 1200 (c) on 11/17/80, a mode change was made from mode 3 to mode sith the vital instrument power board 2-III being powered from the maintenance power supply.
? Investigation revealed that R147, Q12, and U9 intergrated circuit located on the control board had failed. These parts were replaced and the inverter was returned to operation at 1654 (c) on 11/17/80, supplying vital instrument power board 2-III.
- 6. At 1400 (c) on 11/17/80, vital inverter 2-III tripped. Vital instrument
> power board 2-III was immediately shifted to the alternate maintenance power supply and was considered to be operable.
Investigation revealed that the output fuses and the CR6' diode'ha'd' failed.
These components were replaced and the inverter was returned to operation at 1654 (c) on 11/17/80, supplying vital instrument power board 2-III.
1 NOTE: On 11/18/80, at 0935 (c) notification was received from NRC that the provisions of Technical Specification 3.0.5 were not appli-cable to the loss of an inverter. A loss of an inverter makes the corresponding vital instrument power board inoperable even though the vital instrument power board may be powered from its maintenance supply.
LER SUPPLEMENTAL INFORMATION (Continued) 7' . At 0940 (c) on 11/18/80, with unit 1 in made 1 at 50% RTP, vital in-verter 2-III tripped rendering vital instrument power board 2-III inoperable. This resulted in entering the Action Statement of LCO 3.8.2.1.
Investigation revealed that the RBS control board had failed. This control board was replaced and the vital instrument power board 2-III was declared operable at 1235 (c) on 11/18/80.
- 8. At 1000 (c) on 11/19/80, with unit 1 in mode 1 at 50% RTP, vital in-verter 2-III tripped rendering vital instrument power board 2-III inoperable. This resulted in entering the Action Statement of LCO 3.8.2.1.
Investigation indicated a loss of control voltage from the internal A10 power supply. The A10 power supply was replaced and control voltage was restored. The vital instrument power board was declared operable at 1150 (c) on 11/19/80.
- 9. At 1235 (c) on 11/23/80, during the performance of Startup Test 1.1, blackout at 30% RTP, vital inverter 2-III tripped rendering vital instru-ment power board 2-III inoperable. This resulted in enteri-g the Action Statement of LCO 3.8.2.1.
Investigation revealed that resistor RlB located on the A10 power supply had failed. This resistor was replaced and vital instrument power board 2-III was declared operable at 1730 (c) on 11/23/80.
NOTE: The failures of vital inverter 2-III and subsequent losses of vital instrument power board 2-III, had no adverse effect on unit 1 operations as a result of the inverter trips addresseo in this report. Although this vital instrument power board does supply control power to various separation and miscellaneous auxiliary relays associated with systems and components that are either unit 1 or shared by both units, our research has thus-far not revealed any interactions which would have a significant impact on engineered safety feature systems' performance or the capability to safely shutdown Ard cooldown unit 1.
Corrective Action:
In each instance, immediate action was taken to re-energize vital instrument power board 2-III from the alternate maintenance supply. Short term correc-tive action has been to repair vital inverter 2-III and return the inverter to service. Extensive use has been made of temporary brush recorders to attempt to determine why this particular vital inverter has experienced an unusually 1
high failure rate. This diagnostic effort is continuing.
Preparations are in progress to replace all four of the unit 2 vital inverters (2-I, 2-II, 2-III, and 2-IV) with new inverters identical to those installed in unit 1. The unit 1 inverters have demonstrated a significantly higher level of reliability since their replacement with the new units.
Studies are being made to evaluate (1) the feasibility of simplifying the
, inverter protection circuits to increase overall inverter availability and l
(2) alternate class IE instrument power supplies which might be utilized either in parallel with or in place of the inverters.
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