ML19345C198

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IE Insp Rept 50-346/80-23 on 800714-0815.Noncompliance Noted:Failure to Log Unit Tours by Operations Engineer & Failure to Keep Records of Entry & Exit to Vital Areas. Details Withheld (10CFR2.790)
ML19345C198
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 09/24/1980
From: Reyes L, Warnick R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML19345C189 List:
References
50-346-80-23, NUDOCS 8012040115
Download: ML19345C198 (15)


See also: IR 05000346/1980023

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U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

REGION III

Report No. 50-346/80-23

Docket No. 50-346

License No. NPF-3

Licensee: Toledo Edison Company

Edison Plaza, 300 Madison Avenue

Toledo,. 0H 43652

Facility Name: Davis-Besse 1

Inspection At: Oak Harbor, OH

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Inspection' Conducted: July 14-18, 21-25, 28-31, August 1, 4-8, 11-15, 1980

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Inspector:

L. A. Reyes

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Approved By:

R. F. Warnick, Chief

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Projects Section 3

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Inspection Summary

Inspection on July 14-18, 21-25, 28-31, August 1, 4-8, 11-15, 1980 (Report

No. 50-346/80-23)

pe'-Areas Inspected: Routine unannounced inspection of followup on previous

inspections' findings, monthly maintenance observation, monthly _ surveillance

observation, Licensee Event Reports followup, IE Bulletin followup, IE

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Circular followup, review of plant operations, inspection during long-term

shutdown, confirmatory order on' the Crystal River incident, implementation

of IMI lessons learned, office employees union strike, loss of shutdown

-cooling flow on July 24, 1980, NRR technical position on location of load

centers.and radiation protection. The incpection involved a total of 176

inspector-hours-onsite by the Resident Inspector including 48 inspector-

hours onsite during off-shifts.

Results: Of the thirteen. areas inspected, no items of noncompliance were

identified in twelve areas; two items of apparent noncompliance were

identified in the other area (Deficiency - Failure to log the unit tours

by the 0perations Engineer - Paragraph 9, Deficiency - Failure to keep

records of. entry and exit to vital areas - Paragraph 9, Attachment A).

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DETAILS

1.

Persons Contacted

  • T.' Murray, Station' Superintendent

B. Beyer, Assistant Station Superintendent

P. Carr, Maintenance Engineer

S. Quennoz, Technical Engineer

  • D. Huffman, Administrative Coordinator
  • D. Miller, Operations Engineer

D. Briden, Chemist and Health Physicist

J. Hickey, Training Supervisor

L. Simon, Operations Supervisor

C. Daft, Operations QA Manager

  • G. Gaime, Nuclear Security Manager
  • Denotes those present at the exit interview on July 21, 1980.

The inspectors also interviewed other licensee empl'syees, including

members of- the technical, operations, maintenance, I&C, training and

health physics staff.

2.

Previous Inspections' Findings

(Closed) Unresolved Item (50-346/80-19-01): Facility Change Request

80-181 has been completed and the Emergency Diesel Generators Sequencers

were satisfactorily tested. Portions of the testing were witnessed by

the Resident Inspector.

(Closed) Unresolved Item (50-346/80-19-02): The inspector reviewed

the calibration certificate for dewcell serial No. 641.

(Closed) Unresolved Item (50-346/80-19-04): 'The inspector reviewed

the local leak rate test results of makeup system, containment pres-

surization system and fuel transfer tubes. The penalties resulting

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from these test results added to lam at the 95% confidence level does

not exceed the maximum allowable leak rate by 10 CFR 50, Appendix J.

3.

Monthly Maintenance Observation

Station maintenance activities of safety related systems and compon-

ents listed below were observed / reviewed to ascertain that they were

conducted in accordance with approved procedures, regulatory guides

and industry codes or standards and in conformance with technical

specifications.

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The following items were considered during this review:

the limiting

conditions for operation were met while components or systems were

removed frem service; approvals were obtained prior to initiating the

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work; activities were accomplished using approved procedures and were

inspected as applicable;- functional testing and/or calibrations were

. performed. prior to returning components or systems to service; quality

control records were maintained; activities were' accomplished by

qualified personnel; parts and materials used were properly certified;

radiological controls were implemented; and, fire prevention controls

were implemented.

The following maintenance activities were observed / reviewed:

Replacement of Steam Generator 1-1 primary side manway gasket and studs.

Following completion of maintenance on the Steam Generator 1-1 primary

side manway, the inspector verified that the applicable systems had been

returned to. service properly.

No items of noncompliance or teviations were identified.

4.

Monthly Surveillance Observation

The inspector observed technical specifications required surveillance

testing on the Safety Feature Actuation System sequencers and verified

that testing was performed in accordance with adequate procedures, that

- test instrumentation was calibrated, that limiting conditions for opera-

tion were met, - that removal and restoration of .the affected components

were accomplished, that test results conformed with technical specifica-

tions and procedure require ents and were reviewed by personnel other

than the individual directing the test, and that any deficiencies

identified during the testing were properly reviewed and resolved by

appropriate management personnel.

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The inspector also witnessed portions of the following test activities:

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Auxiliary Feedwater Pump 1-2 hot aligment test, stroke of Decay Heat

Removal System isolation valves DH-Il and DH-12.

No itea of noncompliance or deviations were identified.

5.

Licensee-Event Reports Followup

Through direct observations, discussions.with licensee personnel, and

review of records, the following event reports were reviewed to deter-

mine that reportability requirements were fulfilled, immediate corrective

action was accomplished, and corrective action to prevent recurrence

had been accomplished in accordance with technical specifications.

80-05 - Boric Acid Flowpath Inoperable.

80-08 - CAP on Conduit Penetration Through Fire Wall.

80-40 - Broken Fuel Assembly Holddown Spring.

80-46 - Spent Fuel Pool Level Lower Than Technical Specification

' Requirements.

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80-47 !- Door Locked.Open on Nega;ive Pressure Boundary.

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80-49'- Momentary Loss of Decay Heat Flow.

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80-50.- Damage Bearing' Thermocouple on High Pressure Injection Pump 1-1.

80-51 - Inoperable Relays on SFAS Sequencer For. Channels 2 and 4.

No. items of noncompliance or deviations were identified.

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IE Circular Followup -

For the IE Circulars listed below, the inspector verified that the

Circular was received by the licensee management, that a review for

applicabilit.y was performed, and that if the circular were applicable

to the facility, appropriate corrective actions were taken or were

scheduled ta be taken.

79-2S - Possible Malfunction of Namco Model EA 180 Limit Switches

at Elevated Temperatures.

80-05

Vacuum Conditions Resulting in Damage to Chemical Volume

Control System (CVCS) Holdup. Tanks.

80-06 - Engineered Safety Feature (ESF) Reset Controls. During the

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review of the licensee's response, the inspector determined

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that the documentation of the testing performed was not

adequate. The licensee committed to submit an additional

response to'the bulletin and to provide adequate documenta-

tion. This is an unresolved item pending review of the

additional licensee's response to the bulletin and the

review of this document by the inspector (50-346/80-23-01).

No items of noncompliance or deviations were identified.

7.

IE Circular Followup

For the IE Circulars listed below, the inspector verified that the

Circular was received by the licensee management, that a review for

applicability was performed, and that if the circular were applicable

to the facility, appropriate corrective actions were taken or were

scheduled to be-taken.

79-02 - Failure of 120 Volt Vital AC Power Supplies.

79-04 - Loose Locking Nut on Limitorque Valve Operators.

79-05 - Moisture Leakage in Stranded Wire Conductors.

79-09 - Occurrences of Split or Punctured Regulator Diaphragms

in Certain Self-Contained Breathing Apparatus.

79-10 - Pipe Fittings Manufactured from Unacceptable Material.

79-12 - Potential Diesel Generator Turbocharger Problem.

79-13 - Replacement of Die el Fire Pump Starting Contactors.

79-15_ - Bursting of High Pressure Hose and Malfunction of Relief

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Valve "0" Ring in Certain Self-Contained Breathing Apparatus.

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79-19 -- Loose Locking Devices on Ingersoll-Rand Pumps.

79-21 - Prevention'of Unplanned Releases of Radioactivity.

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~80-02'- Nuclear: Power Plant Staff' Work Hours-

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80-05' 1 Emergency Diesel-Generator Lubricating Oil Addition and

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l80-11 - Emergency Diesel-Generator Lube Oil: Cooler Failures.

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80-13:- Grid Strap Damage.in Westinghouse. Fuel Assemblies.

80-14 - Radioactive Contamination of Plant Demineralized Water

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System and -Resultant Internal! Contamination of Personnel.

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No items:of noncompliance or deviations were identified.

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8.

Review of Plant Operations

During the period of July 14'thru August 15, 1980 the inspector re--

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viewed the following activities.

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Training-

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The-inspector attended one of the. licensee's operator requalifica-

. tion lecture series and verified that lesson plan objectives were

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met and that training was in accordance with the approved operator

requalification program schedule and objectives.

The inspector verified by direct questioning of one new, one exist-

ing, and one temporary employee .that administrative controls and

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procedures, radiological health and safety, industrial safety,

controlled access and security procedures, emergency plan, and

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quality assurance training were provided as required by the

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licensee's technical specifications; verified by direct question-

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ing of'one -craftsmen and one technician that on-the-job training,

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formal-technical training commensurate with job classification,

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and fire. fighting training were provided.

b.

Environmental Protection-

The inspector verified the installation and operability of nine

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sampling (monitoring): station (s)'and associated equipment and

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reviewed -records for completeness and accuracy. The inspector

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accompanied a licensee representative during the collection of

vegetable samples.

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-Security

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The inspector verified by the review of records that five individ-

.uals1 achieved acceptable scores during the conduct of weapons and

~ physical' fitness tests.

No items of-noncomplianceoor deviations were identified.

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'9.

Inspection During Long Term Shutdown

The inspector observed control room operations, reviewed applicable

logs and conducted discussions with control room operators during the

period of July 14 through August 15.

The inspector verified surveill-

ance tests required during the shutdown tere accomplished, reviewed

tagout records, and verified applicability of contaicment integrity.

Tours of containment, auxiliary and turbine building accessible areas,

including exterior areas were made to make independent assessments of

equipment conditions, plant conditions, radiological controls, safety,

and adherence to regulatory requirements and to verify that maintenance

requests had been initiated for equipment in need of maintenance. The

inspector observed plant housekeeping / cleanliness conditions, including

potential fire hazards, and verifi d implementation of radiation protec-

tion controls. The inspector by coscovation and direct interview verified

that the physical security plan was being implemented in accordance with

the station security plan. The inspector reviewed the licensee's jumper /

bypass controls to verify there were no conflicts with technical specifica-

tions and verified the implementation of radioactive waste system controls.

The inspector witnessed portions of the radioactive waste systems controls

associated with radwaste shipments and barreling.

While reviewing the unit log, the inspector asticed that for the period

of June 11 through June 25, 1980, there were no entries of plant tours

conducted by the Operations Engineer. This is contrary to procedure

AD1839.00 Revision 6, which requires that the Operations Engineer conduct

detailed tours of the plant at a minimum of once per week and that each

of the tours shall be documented by an entry in the unit log. This is

an item of noncompliance.

Subsequent to the inspector findings the licensee implemented corrective

action by modifying procedure AD1839.00 to allow the Operations Engineer

to designate other operations management personnel to conduct the plant

tours. The inspector will verify that operations management personnel

are conducting the plant tours in subsequent inspections. The inspector

has no further questions at this time.

J, other items of noncompliance or deviations were identified.

10.

Confirmatory Order dated April 21, 1980 on the Crystal River Incident

a.

-Background

The Order was issued as a result of the experience gained from the

Crystal River, Unit 3, incident that occurred on February 26, 1980.

During this incident a loss of power to the non-nuclear instrumenta-

tion resulted in a series of unexpected events. The actions required

by the order were mutually agreed upon by the licensee and the NRC

staff in meetings held in Bethesda, Maryland on March 4,17 and 18,

1980.

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Licensee Commitments

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-The'above mentioned meetings resulted in the following commitments:

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(11 Identify actions which will allow the operator to cope with

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various combinations of loss of instrumentation and control

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functions. This includes changes in (a) equipment and control

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systems to give clear indications of functions which are lost

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or unreliable;.(b) procedures and training to assure positive

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and safe manual response by the operator in the event that

competent -instruments are available.

(2) Determination of the effects of various combinations of loss

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of instrumentation and control functions by design review

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_ analysis and. verification by test.

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(3) Correction of electrical deficiencies which may allow the

power operated relief valve and pressurizer spray valve to

open on non-nuclear instrumentation power failures, such

as, the avent which occurred at Crystal River, Unit 3 on

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(4) Submittal of the response to IE Bulletin 79-27 by May 6,

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Actions Taken

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(1) .The licensee modified the control circuits for the Pressurizer

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Power Operated Relief Valve to ensure that the valve will not

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stay open on loss of NNI power.

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(2) The licensee modified the control circuits associated with

the pressurizer heaters to prevent the heaters from being

energized on loss of NNI power.

Items 1 and 2 were completed

by the implementation of Facility Change Request 80-058.

(3) The licensee added an additional source of AC power and DC

power to the NNI.24 VDC buses to enhance the reliability of

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the 24 VDC buses. This modification was completed by the

taplementation of Facility Change Request 80-096.

(4)

~he licensee _has initiated Facility Change ~ Request 80-100 .

to provide redundant source of AC power to the startup feed-

water control valves, the main feedwater control valves, the

tu'rbine bypass valves and to instrument strir.gs required for

cold shutdown if only one instrument'is pro iding the informa-

tion for a given parameter. Schedule of implementation for

this modification is the 1981 refueling outage.

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(5) 'The. licensee contracted with two consultants to' review the

effects of ~ loss' of power supplies in the NNI/ICS. . Report-

. SAI-OR-245-010 " Failure' Modes and Effects Analysis of the

NNI/ICS Power Supplies at the Davis-Besse Nuclear Power Station"

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has been. issued.

-(6) 'The licensee performed a test, MC 7500.30 Revision 0, " Response

. to Loss of Power in Non-Nuclear Instrumentation System," to

determine the response of the nonnuclear instrumentation to

- power failures. The results of. this test will be incorporated

in-the training'and procedures for operators to detail-the

actions to be taken for a transition to cold shutdown.

Com-

pletion of this action will hc verified by the inspector prior

to the' unit startup from the current outage.

(50-346/80-23-02)

(7) . The licensee performed a test, MC 7500.30 Revision 0, "ICS

Power Supply Failure Response," to determine the response of

the ICS to power supply failures. The results of this test

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will be incorporated in the training and procedure for operators

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to detail the actions to be taken for a transition to cold shut-

down. Completion of this item will be verified by the inspector

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prior to the unit startup from the current outage.

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(50-346/80-23-03)

-(S) The licensee submitted the response to-IE Bulletin 79- '7 on

May 6, 1980.

No items of noncompliance or deviations were identified.

11.

Implementation of TMI Lessons Learned

a.

Background

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The 3RR Lesson Learned Task Force conducted a site review of the

licensee's imp.ementation of the items in letters to the licensee

dated September 13, 1970 and October 30, 1979 and.the Show'Cause

Order dated Jan ary. 2, .1980.

The site review was made on

February 25 and 26, 1980. An evaluation report was issued on

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May 6,1980, and I&E was requested to verify final implementation

and the adequacy of procedures for various items.

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Action Taken

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Item 2.1.1 Emergency Power Supplies

The current design at. Davis-Besse provides for 126 kilowatts of

pressurizer. heater; capacity to each emergency diesel generator.

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.The heaters will be loaded to the diesels on the first step of

the sequencer (closing of the diesel breaker after the machine

has reached rated voltage and frequency). The only operator

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action required is to reset the essential pressurizer heaters

control switches (HIS-RC2-A, HIS-RC2-B) in the control room makeuo

panel.

The inspector verified that adequate guidance for energization of

the pressurizer heater during a loss of power was included in the

supplementary actions of Emergency Procedure EP 1202.02.10 " Station

Blackout." The licensee modified procedure SP 1103.05.08 " Pressurizer

Operation System Procedure" to include guidance on operating the

pressurizer heaters on a loss of power. The inspector interviewed

several reactor operators and senior reactor operators and determined

that they were knowledgeable in the actions to take for energization

of the pressurizer heaters during a loss of power.

The licensee implemented Facility Change Request 79-355 which pro-

vides the PORV block valve (RC 71) with control and motive power-

from essential motor control center F12A. The inspector reviewed

the modification package and determined that the design is adequate.

Item 2.1.3.a Direct Indication of PORV and Safety Valve Position

The licensee implemented Facility Change 79-410 which provides for direct

indication of the PORV and Safety Valve position in the control room.

Procedure SP 1105.20 " Power Operated Relief Valve Monitoring System

Operating Procedure" has been prepared to document the operation of this

position indication systen. Final acceptance of the installation and

modifications to associat.ed emergency procedures has not been completed

at this time. The inspector will verify completion of this item before

the unit startup from the current outage.

(50-346/80-23-04)

Item 2.1.3.b Instrumentation for Detection of Inadequate Core Cooling

Facility Change 79-439 was implemented to provide indication in the con-

trol room of the " Saturation Margin" fcc the existing plant _ conditions.

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A selector switch in the meter allows the operator to display the satura-

tion temperature for the given pressure or saturation pressure for the

given temperature. The revision of emergency procedures to include the

use of the saturation meter is not completed at this time but will be

verified by the inspector before the unit startup from the current outage.

(50-346/80-23-05)

Item 2.1.4 Containment Isolation

The containment isolation signals at Davis-Besse are designcd to prevent

an automatic reopen of containment isolation upon clearing of the initia-

tion signal. Reopening of the isolation valves is accomplished by manual

blocking of the isolation signal followed by further manual actuation of

each valve control switch to the open position. Testing and verification

of this feature was accomplished by Test Procedure MC 7500.34 "SFAS Sequence

Operation Test" which was performed during the current outage.

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During the testing' performed it was determined that if a SFAS is reset

prior to regaining normal power sources, a subsequent SFAS signal could

possibly lead to overloading the Emergency riesel Generator. The con-

tinued loss of. essential 4160/480v power would-then prevent follow-on

a'ctuation of specific containment isolation valves. The interim correction

to this deficiency is by means of procedural controls included in EP .1202.06

" Loss of Reactor Coolant or Reactor Coolant Pressure." The procedure in-

structs the operator not to reset SFAS until offsite power sources are.

-regained., The licensee has initiated Facility Change Request 80-182 to

correct this deficiency.

Item 2.1.5.c H, Dilution Procedures

The inspector reviewr.d procedure SP 1104.55.06 " Containment Hydrogen

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Dilution and Hydrog2n Purge" and determined that the procedure is adequate

to provide guidance'for the operation of the hydrogen purge and hydrogen

dilution systems.

Item 2.1.6.a System Integrity

The licensee has implemented a leak reduction program to reduce the pre-

sent leakage of systems outside containment that would or could contain.

highly radioactive fluids during a serious transient or accident. The

following procedures are used for the implementation of the leak reduction

program:

ST 5042.01

RCS Leakage

ST 5042.02

RCS Water Inventory Balance

_ ST 5051.03

Low Pressure Injection and Containment Spray -

PT 5164.04

-Reactor Sample System Leak Test

PT 5172.00-

Gaseous Radioactive Waste System Leak Rata Test

PT 5164.05

Reactor Coolant Drain Tank System Leak Test

ST 5051.04

ECCS Subsystem Refueling Test

The inspector reviewed the above listed procedures and determined that

they are adequate to implement a permanent leak reduction program. The

inspector.also verified that the program is being implemented at least

once per refueling cycle.

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Item 2.1.8.b High Range Effluent Monitors

The inspector reviewed procedures E? 1202.57 " Steam Generator Tube Leak"

and AD 1850.04 " Post Accident Radiological Sampling and Counting" and

. determined that the procedures are adequate to quantify high-level

effluents from the plant during accident conditions. The licensee has

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initiated Facility Change Request 80-50 to upgrade the existing instru-

mentationcapabilipf1for quantifying noble gases, lirect radiation in

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in the presence of noble gases.

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Item 2.1.8.c Inplant Iodine Instrumentation

The inspector reviewed procedures LI 4768.00 " Laboratory Instrumentation -

Stabilized Assay Meter SAM-2" and AD 1850.04 " Post Accident Radiological

Sampling and Counting" and determined that the procedures were adequate

to analyze air samples for radioiodine concentrations during an accident.

The inspector accompanied the cheuistry and health physicist en a plant

tour and verified that the necessary equipment was in place, calibrated

and properly labeled. The inspector verified by the review of records

and interview of the chemistry and health physics personnel that the

appropriate personnel had received proper training in the procedures for

analizing radioiodine from air samples. The inspector reviewed the

calibration schedule and observed that the Stabilized Assay Meters were

included for calibration every six months.

Item 2.2.1.a Shift Supervisor Responsibilities

The inspector reviewed the below listed procedures and determined that

they are adequate in identifying the shift supervisor responsibilities

during an accident, so that he can provide direct management of on going

safety related operations and not be distre:ted with administrative

assignments.

AD 1839.00

Station Operations

EI 1300.00

Station Response to Emergencies

EI 1300.01

Emergency Plan Activation

EI 1300.02

Emergency Plan Implementing Procedure - Unusual Event

EI 1300.03

Emergency Plan Implementing Procedure - Alert

EI 1300.04

Emergency Plan Implementing Procedure - Site Emergency

'I 1300.05

Emergency Plan Implementing Procedure - General Emergency

The inspector attended the Emergency Planning Training on August 1,1980,

and interviewed several shift supervisors and determined that they were

knowledgeable in their responsibilities during an emergency.

Item 2.2.1.b Shift Technical Advisor (STA)

The inspector reviewed procedure AD 1839.04 " Shift Technical Advisor

Administrative Procedure" and determined that the procedure is adequate

to delineate the duties of the shift technical advisor. The inspector

has witnessed on his routine insoections that the STA is present during

turnovers and during events such as reactor trips and loss of safety

systems functions.

Item 2.2.1.c Shif t and Relief Turnover Procedures

The inspector reviewed procedure AD 1839.00 " Station Operations" and

determined that adequate guidance was provided for a complete and system-

atic turnover between the off going and on-coming shift.

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Item 2.2.2.a Control Room Access

Thc licensee has issued Standing 0rder No. 27 which identifies the timas

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when personnel are allowed access'to the Control Room. The Standing Order

has been posted at the entrance door to the Control Room. .The inspector

reviewed Procedure AD 1839.00 " Station Operations" and determined that

adequate guidance is provided to the Shift Supervisor to control the number

of people in the Control Room. Access to the Control Room is maintained

as per the requirements of Procedure AL 1808.00 " Industrial Security Plan."

Item 2.2.2.b OnSite Technical Support Center (TSC)

The inspector reviewed Procedure EI 1300.07 " Technical Support Center

Activation" and determined that adequate guidance is provided for the

activation of the TSC to assist the operating personnel in the evaluation

of an incident. The inspector reviewed Table 5-1 of the Davis-Besse

Emergency Plan and determined that a communicator is assigned to the TSC

when it is' activated.

Item 2.2.2.c Cperational Support Center (OSC)

The inspector reviewed Procedure EI 1300.07 " Technical Support Center

Activation" and determined that adequate guidance is given fct the mann-

ing of the OSC te provide support to the Control Room and TSC.

No items of noncompliance or deviations were identified.

12.

Office Employees Union Strike

On July 30, 1980, the Office and Professional Employees International

Union, Local No.19, went on strike over contract negotiations. Picketing

was taking place on State Route 2 off the licensee's property.

The picket

was honored by other_ craft unions including company employees.

The licensee modified its shift relief procedure to assure that Operations,

Security and Health Physics manning was sufficient to comply with regulatory

requirements. The union strike ended on August 18, 1980.

No items of noncompliance or deviations were identified.

13.

Loss of Shutdown Coo!ing Flow

On July 24, 1980, tte licensee reported that a blown fuse ciused a valve

(DH-12) on the suction side of the operating decay heat removal pump to

close. Shutdown cooling flow to the reactor was lost at 9:55 a.m. EDT.

Valves in a bypass-line around DH-12 were opened,-the line was vented

and refilled and flow was re-established at 10:45 a.m. EDT. The Center

incore thermocouple (the hottest one in the core) increased from 104'

to 111*F during the time of no flow.

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At the time of the event,_the unit was in mode 5, the reactor vessel

water level was drained to approximately 16 inches above the center

line of the hot leg (7 feet above the core), the uppe r manway handhole

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was open on the primary (RCS) side of one steam generator, and reactor

coolant system maintenance work was in progress. Had it been required,

alternate sources of coolant were available (core flood tanks and

gravity flow from the horated water storage. tank).

The blown fuse was caused by electricians pulling wire (in the cabinet

containing DH-12 valve control wires) for a design change. They caused

a short while pulling wire for the pressurizer heater DH-11 and DH-12

interlock which is being installed to prevent overpressurizing the reactor

vessel [ license requirement 2.c.3.d).

Because of previous experience with

this valve closing on loss of power, the licensee has requested their

license be amended to permit deactivating the valve in the open position

while in modas 5 and 6 (cold shutdown and refueling).

License Amendment No. 28 was granted on July 25, 1980.

Final closecut of this event will be concluded in the review of Licensee

Event Report 80-58.

14.

N3R Technical Position on Lccation of Load Centers

During the Lay 10, 1980 event at Arkansas Nuclear One, Unit 1, it

became nece;sary for a person to enter the containment building to

unlock and close the breaker which provided power to the isolation

valves of the core flood tanks.

.

As a result of this event the following NRR Technical Position was

issued:

Any valve which is required by Technical Specifications to be locked

in a particular position during operation and requires entry into the

containment building to actually unlock the valve locking capability

(such as a locked open breaker) should have its locking capability

located outside the containment building where access can be provided.

The inspector verified that at Davis-Besse there are no Motor Control

Centers (MCC) inside the containment building.

No items of noncompliance or deviations were identified.

15.

Radiation Protection

The inspec..e was approached by the Health Physics coordinator for

the maintenance contractor and was questioned about the adequacy of

the monitoring equipment for the contractor personnel exit from RACA.

The inspector conducted various tours of the RACA area including the

contractor personnel exi . and interviewed several members of the

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Toledo Edison Company Health Physics Personnel. The inspector observed .

that the licensee' experienced a short supply of RM-14 meters .for several:

days but.they were~ repaired and returned to service promptly. The in-

spector discussed the-existing conditions with Region III personnel and

determined that the compensatory actions taken by the licensee satisfied

the regulatory requirements.

No items of' noncompliance or deviations'were identified.

'

16.

Unresolved Items

U1 nresolved . items are matters about which more information is reqa. red

in order to ascertain whether they are acceptable items, items of non-

compliance, or' deviations '

The unresolved items disclosed'during the

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inspection are discussed in paragraphs 6,10 and 11.

s

17.

Exit Interview

The inspector met with licensee representatives (denoted in Paragraph

,

1) on July 21-and August 7, 1980, and summar'. zed the scope and findings

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of the inspection activities.

Attachment: -Attachment A',

contains 2.790(d) Information

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