ML19345C089

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Forwards IE Info Notice 80-40, Excessive Nitrogen Supply Pressure Actuates Safety Relief Valve Operation to Cause Reactor Depressurization. No Written Response Required
ML19345C089
Person / Time
Site: Perkins, Cherokee  
Issue date: 11/07/1980
From: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Dail L
DUKE POWER CO.
References
NUDOCS 8012030862
Download: ML19345C089 (1)


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UNITED STATES i

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NOV 7 1980 a

In Reply Refer To:

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ATTN:

L. C. Dail, Vice President EJ vt Design Engineering P. O. Box 33189 Charlotte, NC 28242 Gentlemen:

This Information Notice is provided as an early notification of a possibly significant matter..It is expected that recipients will review the information for possible applicability to their facilities. No specific action or response

-is requested at this time..If further - NRC evaluations so indicate, an IE Circular or Bulletin will be issued to recommend or request specific licensee actions.

If you have questions regarding this matter, please contact the Director of the appropriate NRC Regional Office.

Sincerely,

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James P. O'Reilly Director

Enclosures:

1.

IE Information Notice No. 80-40 2.

List of Recently Issued IE Information Notices cc w/ enc 1:

J. T. Moore, Project Manager M

8012030 9

l SSINS No.: 6835 Accession No.:

8008220269 UNITED STATES NUCI. EAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINJTON, D.C. 20555 4hqD nyO a[

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_G November 7, 1980 IE Information Notice No.: 80-40:

EXCESSIVE NIROGEN SUrPLY PRESSURE ACTUATES SAFETY-RELIEF VALVE OPERATION TO CAUSE REACTOR DEPRESSURIZATION Description of Circumstances:

On October 7 and 31, 1980, the reactor coolant system was spuriously depres-surized at Boston Edison Company's Pilgrim Nuclear Power Station Unit No.

1.

The Pilgrim Station Unit I uses a GE BWR. The depressurizations resulted when excessive pressure in the nitrogen supply system caused the "A" Target Rock (TR) safety-relief valve to open and remain open until the excessive supply pressure could be isolated, pneumatic operator pressure vented and the main steam system depressurized sufficiently to allow the main disk to reseat.

These two events involved a failure in the pressure regulation of the supply nitrogen and not a failure of the TR safety-relief valve to function as designed.

The safety-relief valves at Pilgrim are designed to be supplied, with other drywell instrumentation, from either the compressed air system or containment atmosphere control system (CACS).

The CACS uses nitrogen for containment inerting. The supply for the safety-relief valves is provided from the CACS through an ambient air vaporizer and then through one of two parallel pressure regulators or a parallel bypass line.

Shortly before the time of each event a new supply of liquid nitrogen had been added to the storage tanks.

At the time of the events the two pressure regulators were in service with the bypass closed. Nitrogen pressure supplying the valves increased to 160 - 165 psi.

This may have been caused by liquid nitrogen reaching the pressure regulators

.y a failure in a pressure regulator. The result was excessive pressure or which was sufficient to leak through the solenoid actuator and initiate the pneumatic operator of the safety-relief valve.

The design normal operating pressure of the compressed air or nitrogen systems supplying the safety-relief valves is90-110 psi. At a pressure of 145 psi the solenoid valve may begin to leak since excessive pressure acts to unseat the disk.

The supply pressure must then decrease to 135 psi or less for the solenoid disk to reseat.

In addition, the design of the safety-relief valve is such that as the main steam pressure increases, less instrument pressure is necessary to initiate the pneumatic operator. Approximately 3 to 5 psi at the pneumatic operator in sufficient to initiate the safety-relief valve opening.

Such a pressure begins to build with leakage through the solenoid actuator and was reached in the "A" valve at 160 psi supply pressure.

According to information from GE and TRC, approximately 180 psi pressure is necessary for all of the safety-relief valves to open as result of supply overpressure.

It would appear that under such conditions of overpressure that safety-relief valve openings would be sequential rather than simultaneous.

The particular solenoid actuator valves used with these two-stage safetyrelief valves are manufactured by TRC. Their des,ign is such that excessive control pressure tends to unseat the solenoid valve disk. The three-stage TR safety-relief valves use either AVC0 (Automatic Valve Company) or ASCO (Automatic Switch Company) solenoid valves according to information from GE.

The AVCo solenoid

IN 80-40 Nsv cb2r 7, 1980 v

Pega 2 of 2 valve has been tested to 300 psi and found not to leak and the ASCo solenoid valve tends to seat with increasing supply pressure. Therefore, the NRC

' believes that the tendency for solenoid leakage and hence safety-relief valve opening is confined to the tvo-stage safety-relief valve installations.

This information is provided as a notification of a possibly significant matter which is still under review by the NRC staff.

It is anticipated that the results of continuing NRC review will culminate in issuance of an IE Bulletin which will recommend or require specific licensee action.

In the interim, we expect that recipiente will review the information for possible applicability to their facilities, particularly those with installations of the TR two-stage safety-relief valves.

If you have questions regarding this matter, please contact the Director of the appropriate NRC Regional Office.

l IN 80-40 November 7, 1980 RECENTLY ISSUED IE INFORMATION NOTICES Information Date of Notice No.

Subject Issue Issued to 80-40 Excessive Nitrogen Supply 11/07/80 All nuclear power reactor Pressure Actuates Safety-facilities with an OL Relief Valve Operation to or CP Cause Reactor Depressuri-zation 80-39 Malfunctions Of Solenoid 10/31/80 All light water reactor Valves Manufactured By facilities holding Valcor Engineering Corporation power reactor OLs or cps 80-38 Cracking In Charging Pump 10/30/80 All PWR facilities Casing Cladding with an OL or CP 80-37 Containment cooler leaks 10/24/80 All nuclear power and reactor cavity.

facilities holding flooding at Indian Point Unit 2 power reactor OLs or cps 80-36 Failure of Steam 10/10/80 All nuclear power Generator Support Bolting reactor facilities holding power reactor OLs or cps 80-35 Leaking and dislodged 10/10/80 All categories G and Iodine-124 implant seeds-G1 medical licensees 80-34 Boron dilution of reactor 9/26/80 All pressurized water coolant during steam reactor facilities generator decontamination tolding power reactor OLs 80-33 Determination of teletherapy 9/15/80 All teletherapy timer accuracy (G3) licensees 80-32 Clarification of certain 8/12/80 All NRC and agreement requirements for Exclu-state licensees sive-use shipments of radioactive materials-80-31 Maloperation of Gould-8/27/80 All light water reactor Brown Boveri Type 480 volt type K-600S and facilities holding OLs or cps K-DON 600S circuit breakers O Operating Licenses or Construction Permits

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