05000282/LER-1980-033-03, /03L-0:on 801028,steam Flow Transmitter 1FT-464 Observed Reading Low.Caused by Zero Adjustment Shift in Barton Model 384 Differential Pressure Transmitter.Device Recalibr

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/03L-0:on 801028,steam Flow Transmitter 1FT-464 Observed Reading Low.Caused by Zero Adjustment Shift in Barton Model 384 Differential Pressure Transmitter.Device Recalibr
ML19345B527
Person / Time
Site: Prairie Island 
Issue date: 11/26/1980
From: Hunstad A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19345B524 List:
References
LER-80-033-03L, LER-80-33-3L, NUDOCS 8012010493
Download: ML19345B527 (1)


LER-1980-033, /03L-0:on 801028,steam Flow Transmitter 1FT-464 Observed Reading Low.Caused by Zero Adjustment Shift in Barton Model 384 Differential Pressure Transmitter.Device Recalibr
Event date:
Report date:
2821980033R03 - NRC Website

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60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h l0l2l l During str. cup, steam flow transmitter lfT-464 was observed to be reading low.

I At recalibration it was determined that the MSIV closure signal and the reactor trip l 1013 l l ITT71 l Signal from this channel could have occurred as much as21% above Tech Spec limits.

l loisl l Repetitive; recent sita11ar event was RO 80-27.

Tech Spec Tables 3.5-land -2 apply.

l I O is l l NO effect on public health or safety since redundant equipment was operable.

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33 36 36 3d 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS li l0 l l Zero adjustment shift in Barton Model 384 differential pressure transmitter.

l li li j l Appropriate bistables were placed in trip.

The device was recalibrated and I

returned to service. These transmitters are scheduled to be replaced during i

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