LER-1980-032, /01T-0:on 800806,both Containment Spray Pump Compartment Doors Found Open.Caused by Lack of Administrative Controls.Engineering Evaluation Planned Re Effective Controls of Access Through Water Tight Doors |
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- CCF ET N6Me tm 6il 69 EvtNT CAf t 74 IS R El":RT ATE SG E% EN T OESCRIPTION ANC PAC 8ABLE CONsECUENCES h t j:! 10n July 16, 1980, both doors from the torus area to the containment I
to.3, Ispray pump areas were found open in violation of T.S. 3.4.E and 3.4.C.I.
I joi4; t'ecause the required surveillance to verify door closure after entry l
l o i s j :was not performed, T.S. 4.4.C.3 was also violated. The ooeratoryho l
lcse! ifound the doors open closed them insned ia tely and reported the Incident i
1: 67. ito the Group Shift Supervisor. The maximum time that the doors could
,;,ai ihave been open was determined to be eight hours.
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ii ial lThe apparent cause of the occurrence is the lack of administrative i
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Jemey Centmi Power & Ught Company Madison Avenue at Punch Bewt Road Mornstown, New Jersey 07960 (201)455-8200 OYSIER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/80-32/IT Re; ort Date August 14, 1980 Occurrence Date August 6, 1980 identification of Occurrence Violation of the Technical Specifications, paragraph 3 4.E and 3.4.C.1, when both containment spray pump compartment doors were discovered open on a routine tour of the Reactor Building, and paragraph 4.4.C.3 when required surveillance to verify door closure af ter entry was not performed.
These events constitute a reportable occurrence as defined in the Technical Speci fications, paragraph 6.9.2. A.6.
However, this fact was not recognized as such until August 6, 1980.
Conditions Prior to Occurrence Startup testing following a reueling/ maintenance outage was in progress. The major parameters at the time of occurrence were:
Power:
Reactor,188 MWT Generator, O MVe Flow:
Feedwater, 1.2 x 106 lbs/hr Recirculation, 5 3 x 104 gpm 0
Stack Gas: 0.7 x 10 uct/sec I
l Description of Occurrence On July 16, 1980 at approximately 4:30 p.m.,
an operator performing a routine tour of thi Reactor Building discovered that both doors from the torus area to tae con-tainment spray pump areas (northeast and southeast corners of the Reactor Building
@ El. minus 19'-6") were opened.
The operator immediately closed the doors and dogged them shut and reported the incident to the Group Shift Supervisor.
Jersey Central Pcwer & Ught Company is a Memcer of the General Puche Utiht:es System
Reportable Occurrence No. 50-219/80-32/IT August 14, 1980 Page 2 Accarent Cause of Occurrence Although signs are posted on each door indicating that they must be closed and dogged at all times except for passage, there is an apparent lack of administrative controls to ensure that this is done. Personnel workins in the areas inadvertently left the doors open and failed to recognize the fact that they were in violation of the Technical Specifications.
Analysis of Occurrence The containment spray cooling system consists of two independent :coling loops, each capable of removing heat from the primary containment following a loss of coolant accident. Since bcth doors were open, Containment Spray Systems I and 11 were
' considered to be " inoperable" as defined by the Technical Specifications. However, both systems would have perform 4d their designed functions as long as the structural integrity of the torus remained intact.
(i.e. no potential leak paths develop which could cause water to enter the pump rooms).
Based on documented operator tours of the area, the maximum amount of time the water tight doors could have been open was eight hours.
Corrective Action
The pump room doors were closed and dogged shut ir.rediately upon discovery.
An engineering evaluation will be made to determine an effective way of controlling access through the torus / corner room water tight doors.
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l Fa i l u re Da ta Not applicable.
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| 05000219/LER-1980-001-01, /01T-o:on 800105,while Performing Electromatic Relief Valve Operability Test,Emergency Releie Valve D Failed to Open.Caused by Component Failure Due to Retainer Ring Being Backed Off Approx Six Threads | /01T-o:on 800105,while Performing Electromatic Relief Valve Operability Test,Emergency Releie Valve D Failed to Open.Caused by Component Failure Due to Retainer Ring Being Backed Off Approx Six Threads | | | 05000219/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000219/LER-1980-002-03, /03L-0:on 800116,during Fuel Bundle Clip Insp,Fuel Bundle UD-3-023 Was Misoriented & Was Not Properly Seated in Core Cell Location.Caused by Personnel Error & Inadequate Procedural Controls.Procedure 205 Revised | /03L-0:on 800116,during Fuel Bundle Clip Insp,Fuel Bundle UD-3-023 Was Misoriented & Was Not Properly Seated in Core Cell Location.Caused by Personnel Error & Inadequate Procedural Controls.Procedure 205 Revised | | | 05000219/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000219/LER-1980-003-01, /01T-0:on 800116,during Inservice Insp on Core Spray Sparger Piping for Sys Ii,Two Indications of Cracks Discovered.Ultrasonic Test Revealed through-wall Cracks. 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