LER-1980-202, /03L-0:on 801225,steamline Pressure & Flow Channel S/G-3 Train a Failed High & S/G-1,2 & 4 Train B Failed Low. Caused by Freezing of Unprotected Sense Lines.Lines Thawed. Design Changes Initiated |
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60 Gl DOC u t T NUMO E M G8 t9 (VENT DAf t 74 JS REFQRT DAT E 80 EVENT DESCAtPTION AND PROSA8LE CONSEQUENCES h loi2l l At 86% RTP, S/G-3 train A steamline pressure and flow channels failed high at 0441 CST. I l o t a l l Action statements of' LCO 3.3.3.7(a), 3.3.1.1(7), and 3.3.2.1(16) were in effect until i
Iop4l l operability was restored at 0621 CST. At 0649 CST S/G-1, 2, & 4 train B feedwater flow l ib6TO I channels failed low and plant entered action statement 7 of LCO 3.3.1.1.
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l o !s j l train A feedwater flow channel subsequently failed low at 0852 CST, the plant prepared l loj7; l for shutdown per LCO 3.0.3 but remaine4 at power when operability was restored at 0934 l go;eil CST. No effect on public health or safety. Previous occurrences - none.
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I liiil lThe 14nas were thnwed by acolvine t o-nne rary heat and insulation. D e si en chnneaa hava Iil2I l been initiated to have the recuired heat tracing and insulation installed to orevent i1 i3l l re-occurrence.
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Tennassaa Vallsy Authority Seqt'oyah Nuclear Plant LER SUPPLEMENTAL LNFORMATION SQRO-50-327/80202 Technical Specification Involved:
3.0.3, 3.3.1.1, 3.3.2.1, 3.3.3.7 Raported Under Technical Specification:
6.9.1.13.b Date of Occurrence:
12/25/80 Time of Occurrence:
0441 CST Identification and Description of Occurrence:
At 0441 CST the train A steamline pressure channel (P-1-20A) and the associated steamline flow channel (F-1-21A) for steam generator #3 failed high. The plant entered action statement "a" of LCO 3.3.3.7 and the affected trip bistables were placed in the manually-tripped co'dition as specified by action statement 7 of LCO 3.3.1.1 and action statement 16 of LCO 3.3.2.1 until operability was restored at 0621 CST. At 0649 CST train B feedwater flow channels for steam generator #1 (F-3-35B), steam generator
- 2 (F-3-48B) and steam generator #4 (F-3-103E) failed low. The affected trip bistables were placed in the manually-tripped condition in accordance with action statement 7 of LCO 3.3.1.1.
Subsequently at 0852 CST the train A feedwater flow channel for steam generator #1- (F-3-35A) also faile d low.
- - Although the flow channels failed in the conservative direction, the plant -
prepared for shutdown in accordance with LCO 3.0.3 but remained in Mede 1 when operability of the flow channels was restored at 0934 CST.
Conditions Prior to Occurrence:
Unit in Mode 1 at 86% RTP Apparent Cause of Occurrence:
The steamline pressure and flow channels failed high because the associated
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steamline pressure transmitter's sense lines in the east valve room were frozen. The transmitter is located near the air intake louvers in the east valve room which were open allowing the sense lines to freeze.
The feedwater flow channels failed low when the associated sense lines became frozen inside a building wall penetration. Heat tracing for the lines did not extend into the penetration and therefore that portion of the sense lines was unprotected.
Analysis of Occurrence:
The f ailure of the steamline pressure channel resulted in one accident monitoring
.steamline pressure channel for steam generator #3 being inoperable for less chan two hours. Since the steamline flow and pressure channels failed high, the associated reactor. protection and ESF trip functions were performed.
Since the feedwAP.er flow channels failed low, the required protective functions were performed and operation of the plant was never less conservative than the-limiting condition for operation specified by LCO 3.3.1.1.
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LER SUPPLEMENTAL INFORMATION (Continued)
Corrective Action
The sense lines were taawed by applying additional heat and insulation. A design change request has been initiated to have the necessary heat tracing and insulation installed to prevent re-occurrence.
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| 05000327/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000327/LER-1980-001-01, /01T-0:on 800301-03,during Initial Fuel Loading, Licensee Failed to Estimate Flowrate from Svc Bldg Exhaust at 4-h Intervals.Caused by Misunderstanding of Tech Spec Requirements.Plant Instructions Revised | /01T-0:on 800301-03,during Initial Fuel Loading, Licensee Failed to Estimate Flowrate from Svc Bldg Exhaust at 4-h Intervals.Caused by Misunderstanding of Tech Spec Requirements.Plant Instructions Revised | | | 05000327/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000327/LER-1980-002-01, /01T-0:on 800306,contents of Task Decontamination Collector Tank Discharged Via Liquid Radwaste Effluent Line to Cooling Tower Blowdown W/O Flow Estimates Being Performed.Caused by Misunderstanding of Tech Specs | /01T-0:on 800306,contents of Task Decontamination Collector Tank Discharged Via Liquid Radwaste Effluent Line to Cooling Tower Blowdown W/O Flow Estimates Being Performed.Caused by Misunderstanding of Tech Specs | | | 05000327/LER-1980-003-01, /01T-0:on 800310,following Initial Fuel Loading, Flow Through Auxiliary Bldg Exhaust Sampler Not Maintained for 3.25-h.Caused by Misunderstanding of Tech Specs. Personnel Reinstructed in Applicable Requirements | /01T-0:on 800310,following Initial Fuel Loading, Flow Through Auxiliary Bldg Exhaust Sampler Not Maintained for 3.25-h.Caused by Misunderstanding of Tech Specs. Personnel Reinstructed in Applicable Requirements | | | 05000327/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000327/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000327/LER-1980-004-01, /01T-0:on 800311,following Initial Fuel Loading, Flow Estimates for Auxiliary Bldg Vent Monitor Not Performed for 10-h.Caused by Misunderstanding of Tech Specs.Personnel Reinstructed Re Applicable Requirements | /01T-0:on 800311,following Initial Fuel Loading, Flow Estimates for Auxiliary Bldg Vent Monitor Not Performed for 10-h.Caused by Misunderstanding of Tech Specs.Personnel Reinstructed Re Applicable Requirements | | | 05000327/LER-1980-005-03, /03L-0:on 800311,while Performing SI-247.605, Reactor Solid State Protection Sys Was Placed in Input Inhibit Mode,Removing High Voltage from Source Range Channel N31.Caused by Removal of Fuses from Voltage Cut Out Relay | /03L-0:on 800311,while Performing SI-247.605, Reactor Solid State Protection Sys Was Placed in Input Inhibit Mode,Removing High Voltage from Source Range Channel N31.Caused by Removal of Fuses from Voltage Cut Out Relay | | | 05000327/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000327/LER-1980-006-01, /01T-0:on 800314,w/essential Raw Cooling Water Radiation Monitors on Train a Inoperable,Personnel Determined That Limiting Condition of Operation Requires Sampling.Caused by Misinterpretation of Tech Specs | /01T-0:on 800314,w/essential Raw Cooling Water Radiation Monitors on Train a Inoperable,Personnel Determined That Limiting Condition of Operation Requires Sampling.Caused by Misinterpretation of Tech Specs | | | 05000327/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000327/LER-1980-007-01, /01T-0:on 800315,following Initial Core Loading, Found Incorrect (Nonconservative) Valve Operator Weights Used in Seismic Analysis for Component Cooling Water Valves FCV-70-133,134 & 183.Caused by Incorrect Vendor Data | /01T-0:on 800315,following Initial Core Loading, Found Incorrect (Nonconservative) Valve Operator Weights Used in Seismic Analysis for Component Cooling Water Valves FCV-70-133,134 & 183.Caused by Incorrect Vendor Data | | | 05000327/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000327/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000327/LER-1980-008-03, /03L-0:on 800303,cooling Tower Blowdown Effluent Line Flow Monitor O-FR-27-175 Was Declared Inoperable.Flow Monitor Consistently Indicated Higher Flowrate than Actually Existed.Cause Unknown.Different Instrument to Be Instal | /03L-0:on 800303,cooling Tower Blowdown Effluent Line Flow Monitor O-FR-27-175 Was Declared Inoperable.Flow Monitor Consistently Indicated Higher Flowrate than Actually Existed.Cause Unknown.Different Instrument to Be Installed | | | 05000327/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000327/LER-1980-009-03, /03L-0:on 800303,liquid Radwaste Effluent Line Flow Monitor 0-FT-77-42 Consistently Indicated Higher Discharge Flow Rate than Actually Observed.Cause Not Stated.Flow Monitor Modified & Returned to Svc | /03L-0:on 800303,liquid Radwaste Effluent Line Flow Monitor 0-FT-77-42 Consistently Indicated Higher Discharge Flow Rate than Actually Observed.Cause Not Stated.Flow Monitor Modified & Returned to Svc | | | 05000327/LER-1980-010-03, /03L-0:on 800304,gaseous Vent Flow Rate Monitors for Units 1 & 2 Shield Bldgs & Auxiliary Bldg Were Declared Inoperable.Cause Not Stated.Gaseous Flow Rate Monitors to Be Redesigned | /03L-0:on 800304,gaseous Vent Flow Rate Monitors for Units 1 & 2 Shield Bldgs & Auxiliary Bldg Were Declared Inoperable.Cause Not Stated.Gaseous Flow Rate Monitors to Be Redesigned | | | 05000327/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000327/LER-1980-011, Forwards LER 80-011/01T-0 | Forwards LER 80-011/01T-0 | | | 05000327/LER-1980-011-01, /01T-0:on 800314,support Pin Insp at Foreign Plant Revealed Stress Corrosion Cracking in Westinghouse Supplied Pins.Insp Supported Westinghouse Ltr Informing Utils of Potential Hazard.Pins Will Be Replaced | /01T-0:on 800314,support Pin Insp at Foreign Plant Revealed Stress Corrosion Cracking in Westinghouse Supplied Pins.Insp Supported Westinghouse Ltr Informing Utils of Potential Hazard.Pins Will Be Replaced | | | 05000327/LER-1980-012-03, /03L-0:on 800301,during Initial Core Loading,Rhr Flow Secured or Throttled Above Tech Specs.Caused by Intentional Increase to Allow Placement of Fuel Assemblies Near Loop 4 Hot Leg | /03L-0:on 800301,during Initial Core Loading,Rhr Flow Secured or Throttled Above Tech Specs.Caused by Intentional Increase to Allow Placement of Fuel Assemblies Near Loop 4 Hot Leg | | | 05000327/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000327/LER-1980-013-03, /03L-0:on 800302,failed to Analyze Samples from Unit 2 Shield Bldg Exhaust.Caused by Misunderstanding of Surveillance Requirements.Lab Personnel Instructed on Sampling & Analysis Requirements | /03L-0:on 800302,failed to Analyze Samples from Unit 2 Shield Bldg Exhaust.Caused by Misunderstanding of Surveillance Requirements.Lab Personnel Instructed on Sampling & Analysis Requirements | | | 05000327/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000327/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000327/LER-1980-014-03, /03L-0:on 800328,while Performing Check Source Test,Auxiliary Bldg Vent Noble Gas Monitor Had Module Power Problem & Failed in Svc.Caused by Zener Diode IN4740 & Transistor Fmps A13 Shorting Out | /03L-0:on 800328,while Performing Check Source Test,Auxiliary Bldg Vent Noble Gas Monitor Had Module Power Problem & Failed in Svc.Caused by Zener Diode IN4740 & Transistor Fmps A13 Shorting Out | | | 05000327/LER-1980-015-03, /03L-0:on 800305,while in Mode 6 W/Fuel Loading Complete,Pressure Was Only Being Monitored in One Steam Generator & Reactor Pressure Vessel.Caused by Misunderstanding of Surveillance Instruction | /03L-0:on 800305,while in Mode 6 W/Fuel Loading Complete,Pressure Was Only Being Monitored in One Steam Generator & Reactor Pressure Vessel.Caused by Misunderstanding of Surveillance Instruction | | | 05000327/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000327/LER-1980-016, Forwards LER 80-016/03L-0 | Forwards LER 80-016/03L-0 | | | 05000327/LER-1980-016-03, /03L-0:on 800307,at Completion of Fuel Loading & W/Core Alterations Still underway,SI-65 Was Not Performed. Caused by Misinterpretation of Tech Specs by Personnel.No Corrective Actions Necessary | /03L-0:on 800307,at Completion of Fuel Loading & W/Core Alterations Still underway,SI-65 Was Not Performed. Caused by Misinterpretation of Tech Specs by Personnel.No Corrective Actions Necessary | | | 05000327/LER-1980-017-03, /03L-0:on 800310,while in Mode 6,turbine Bldg Sump Monitor O-RM-90-212 Alarm Kept Coming In.Monitor Was Declared Inoperable.Caused by Malfunctioning Flow Switch Not Allowing Sufficient Flow Through Monitor | /03L-0:on 800310,while in Mode 6,turbine Bldg Sump Monitor O-RM-90-212 Alarm Kept Coming In.Monitor Was Declared Inoperable.Caused by Malfunctioning Flow Switch Not Allowing Sufficient Flow Through Monitor | | | 05000327/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000327/LER-1980-018-01, /01T-0:on 800326,while in Mode 6 W/All Fuel Loaded,Exposed Cables Inside Containment Between Conduit & Penetrations Not Qualified to re-evaluated post-LOCA Max Dose Levels.Cables Shielded from Exposure to New Dose Level | /01T-0:on 800326,while in Mode 6 W/All Fuel Loaded,Exposed Cables Inside Containment Between Conduit & Penetrations Not Qualified to re-evaluated post-LOCA Max Dose Levels.Cables Shielded from Exposure to New Dose Level | | | 05000327/LER-1980-018, Forwards LER 80-018/01T-0 | Forwards LER 80-018/01T-0 | | | 05000327/LER-1980-019, Forwards LER 80-019/01T-0 | Forwards LER 80-019/01T-0 | | | 05000327/LER-1980-019-01, /01T-0:on 800326,found Possibility of Not Maintaining Control Room Habitability Due to Leakage of Unfiltered Air.Possibly Caused by Isolation Dampers. Corrective Mods Planned | /01T-0:on 800326,found Possibility of Not Maintaining Control Room Habitability Due to Leakage of Unfiltered Air.Possibly Caused by Isolation Dampers. Corrective Mods Planned | | | 05000327/LER-1980-020, Forwards LER 80-020/01T-0 | Forwards LER 80-020/01T-0 | | | 05000327/LER-1980-020-01, /01T-0:on 800404,investigation Revealed That Several vendor-designed Pipe Supports Were Designed Utilizing Manufacturer Std 0.25-inch U-bolt Which Overstressed During Seismic Event.Caused by Design Error | /01T-0:on 800404,investigation Revealed That Several vendor-designed Pipe Supports Were Designed Utilizing Manufacturer Std 0.25-inch U-bolt Which Overstressed During Seismic Event.Caused by Design Error | | | 05000327/LER-1980-021-03, /03L-0:on 800308,while in Mode 6,flow Rates from Auxiliary Bldg Ventilation Sys Flow Rate Monitor Were Not Recorded for Three Shifts.Caused by Misreading of Notation Used in Surveillance Instruction.Temporary Change Issued | /03L-0:on 800308,while in Mode 6,flow Rates from Auxiliary Bldg Ventilation Sys Flow Rate Monitor Were Not Recorded for Three Shifts.Caused by Misreading of Notation Used in Surveillance Instruction.Temporary Change Issued | | | 05000327/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000327/LER-1980-022-03, /03X-2:on 800318,sample Isolation Valves 1-FCV-90-108,109,110,114,115 & 116 Closed,Isolating Radiation Monitors.Caused by Isolation of Nonessential Control Air to Sample Valves.Valves Reopened | /03X-2:on 800318,sample Isolation Valves 1-FCV-90-108,109,110,114,115 & 116 Closed,Isolating Radiation Monitors.Caused by Isolation of Nonessential Control Air to Sample Valves.Valves Reopened | | | 05000327/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000327/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000327/LER-1980-023-03, /03L-0:on 800402,during Surveillance Testing, Diesel Generator 2A-A Feedbreaker Failed to Close.Caused by Power Contacts Being Dirty.Power Contacts Cleaned | /03L-0:on 800402,during Surveillance Testing, Diesel Generator 2A-A Feedbreaker Failed to Close.Caused by Power Contacts Being Dirty.Power Contacts Cleaned | | | 05000327/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000327/LER-1980-024-03, /03L-0:on 800331,flow Switches on Radiation Monitors ORM-90-212 & 122 Found Inoperable.Caused by Small Particulate Matter in Monitored Liquid.Design Change Request Initiated.Weekly Preventive Maint Program Established | /03L-0:on 800331,flow Switches on Radiation Monitors ORM-90-212 & 122 Found Inoperable.Caused by Small Particulate Matter in Monitored Liquid.Design Change Request Initiated.Weekly Preventive Maint Program Established | | | 05000327/LER-1980-025, Forwards LER 80-025/03L-0 | Forwards LER 80-025/03L-0 | | | 05000327/LER-1980-025-03, /03L-0:on 800313 W/Unit 1 in Mode 6,O-RM-90-225 Condensate Demineralizer Effluent Line Was Taken Out of Svc for Maint.Caused by Weak Transistor.Transistor Replaced & Monitor Returned to Svc | /03L-0:on 800313 W/Unit 1 in Mode 6,O-RM-90-225 Condensate Demineralizer Effluent Line Was Taken Out of Svc for Maint.Caused by Weak Transistor.Transistor Replaced & Monitor Returned to Svc | |
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