05000334/LER-1980-112-03, /03L-0:on 801213,sample Pump for Containment Atmospheric Gaseous & Particulate Radiation Monitors Failed. Cause Not Stated.Sample Pump,Motor & Drive Pulley Replaced

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/03L-0:on 801213,sample Pump for Containment Atmospheric Gaseous & Particulate Radiation Monitors Failed. Cause Not Stated.Sample Pump,Motor & Drive Pulley Replaced
ML19340F126
Person / Time
Site: Beaver Valley
Issue date: 01/12/1981
From: Lacey W
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19340F125 List:
References
LER-80-112-03L, LER-80-112-3L, NUDOCS 8101190477
Download: ML19340F126 (2)


LER-1980-112, /03L-0:on 801213,sample Pump for Containment Atmospheric Gaseous & Particulate Radiation Monitors Failed. Cause Not Stated.Sample Pump,Motor & Drive Pulley Replaced
Event date:
Report date:
3341980112R03 - NRC Website

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EVENT CESCRIPTION ANO P A08 A8LE CCNSECUENCES h l o ! : 1 l On 12/13 NO at 1410 hnurs, the sa-nle numn for the cantain-ent nt-ocnheri-m er.us I

I and particulate radiation monitors failed. At the time. an alarmed condition on thel go43; The monitors, wnich are used to detect l

l a j,j l caseous monitor was beine investicated.

Jois)l Reactor Coolant System (RCS) Icakace, were declared inoperable nor Technical l

I o is j i Soecification 3.4.6.1.

The health and safety of the noblic vac not inarardized I

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No RCS Icak was I

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l i l o I l On 12/13/30 at 1640 hours0.019 days <br />0.456 hours <br />0.00271 weeks <br />6.2402e-4 months <br />, the meriters were returned to service bv establishine I

vacuum pump.

On 12/15/80 after I

l flow throuch them usine the stand v containment li s i )

lreplacinC the sample pump, it's motor and a broken drive pullev, normal service was 1 i,,,,

This type of incident has occurred l 1 ' ! 11 l restored to the monitors usine the sample pumo.

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O{Q0 ti Attachment To LER 80-112/03L Beaver Val.'cy Power Station Duquesne Light Company Docket No. 50-334 No further information is availabic or needed to satisfy the reporting requirement.

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