LER-1980-106, /01T-0:on 801226,HPCI Sys Tripped Immediately After Low Level 2 auto-initiation on High Steam Line Exhaust Pressure Signal.Caused by Water Hammer Event in Exhaust Line.Hpci Sys Trip Reset |
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| 3241980106R01 - NRC Website |
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EVE *.T.0ESCRIPTION AND PRO 8 A8LE CONSF.M,'ENCES h i
! [TT q l Following a reactor scram on low water level, the. HPCI system trioned irrediateiv 4
,after a Low Level 2 auto-initiation on a high steam line exhaust pressure signal.
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3J 35 36 37 40 el 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h (TTTI IThe HPCI system trip was i= mediately reset and the system started to return vessel l
g l level to normal. An investigation determined that a water hammer event in the exhaust l A plant modifiedtion 1
l m ;line caused the.high pressure signal which tripped the system.
lhas been writen to correct the problem which allowed water to enter this line.
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% POWER OTHER STATUS IS Y
DISCOVERY DESCRIPTION Q [Gj@ {0l0l0l@l NA l
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i LER ATTACHMINT - RO # 2-80-106 Facility: BSEP Unit No.
2 Event Date:
12-26-80 Following a low level reactor scram caused by the loss of the operating feed pump, the HPCI and RCIC Systems received an auto-initiation signal at Low Level 2 (-38").
Both systems started; however, the HPCI System immediately tripped due to a high exhaust steam line pressure signal.
The HPCI System was immedi-ately reset and system started to restore vessel level.
i While investigating the cause for the high exhaust steam line pressure trip, three snubbers on the steam exhaust line were found to be physically damaged.
The remaining snubbers on this line were functionally tested and four were found inoperable. The inoperable snubbers and their problems were as follows:
- 1) 2E41-6SS35 and 2E41-6SS37 were found to have all four mounting bolts broken;
- 2) 2E41-6SS64 had a broken piston rod; 3) 2E41-6SS32, 2E41-6SS33, 2E41-6SS36 and 2E41-6SS38 all failed to lock-up on the functional test.
The damaged snubbers were removed and new snubbers were functionally tested and installed in their place. All four snubbers which failed to lock-up were disassembled,-
rebuilt using new seal kits, puppets, and springr, functionally tested, and returned to service. No reason for the snubber lock-up failures could be found during the inspection. The three broken snubbers were damaged during a water hammer event in the steam exhaust line.
Further investigation of the high steam line exhaust pressure and the water hammer event determined that the HPCI inlet steam line drain pot had become filled and allowed condensate to back up into the inlet steam line. When the system was scarted, this water was carried through the turbine and into the exhaast line causing a momentary high pr2ssure and a water hammer event.
Due to failures of the drain pot level switch, 2E41-LSH-N014, to function and open the drain valve, 2E41-F054, a plant modification was written to replace this switch with an analog type instrument. Due to hardware problems with the new instrumentation and unreliability of the installed switch, the automatic drain function of the switch was recoved from the drain valve in February 1980, and a requirement was placed on the control operator's Daily Surveillance Report (DSR) to require that the inlet drain pot be manually drained for 10-15 seconds twice per shift.
Apparently, in this case, this amount of draining was not sufficient to assure that the drain pot was drained. To prevent a recur-rence of this problem, the control operator's DSR has been revised to require draining the inlet drain pot twice per shif t, and to drain until a temperature increase is noted in the Reactor Building Equipment Drain Tank (RBEDT).
This j
temperature increase will indicate that the drain pot is empty., We plan to complete the instrumentation modification at the next long-term scheduled outage for each unit.
l The HPCI turbine and associated piping were inspected and no problems were noted. Before the unit was returned to power, operational and vibration surveillance tests were performed on the HPCI System and all tests were satisfactory.
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| 05000325/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000325/LER-1980-001-03, /03L-0:on 800102,during Normal Operation, Containment Atmospheric Monitor Had Step Increase of Approx 2%.Caused by Instrument Drift.Instrument Recalibr & Returned to Svc | /03L-0:on 800102,during Normal Operation, Containment Atmospheric Monitor Had Step Increase of Approx 2%.Caused by Instrument Drift.Instrument Recalibr & Returned to Svc | | | 05000324/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000324/LER-1980-001-03, /03L-0:on 800117,during Attempt to Start RHR Room Cooler 2A,breaker Tripped on Magnetics.Cause Could Not Be Determined Due to Inoperable Room Cooler 2B.Breaker Reset & Closed | /03L-0:on 800117,during Attempt to Start RHR Room Cooler 2A,breaker Tripped on Magnetics.Cause Could Not Be Determined Due to Inoperable Room Cooler 2B.Breaker Reset & Closed | | | 05000324/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000324/LER-1980-002-03, /03L-0:on 800102,during Normal Reactor Startup,Rod Sequence Control Sys Would Not Allow Rods to Be Pulled Until Rod 34-27 Was Bypassed full-in. 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Drawer Recalibr & Returned to Svc | /03L-0:on 800122,while Performing Main Steam Line High Radiation Functional Check,Drawer 1D12-RM-K603B Found Out of Calibr.Instrument Drift Is Recurring Problem. Drawer Recalibr & Returned to Svc | | | 05000325/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000324/LER-1980-010-03, /03L-0:on 800114,during Normal Plant Operation, Nuclear Engineer Performed OD-1 & Found Max Critical Power Ratio to Exceed Limit.Caused by Low Power Range Monitor Having Two Levels Bypassed & Problems W/Core Flow Input | /03L-0:on 800114,during Normal Plant Operation, Nuclear Engineer Performed OD-1 & Found Max Critical Power Ratio to Exceed Limit.Caused by Low Power Range Monitor Having Two Levels Bypassed & Problems W/Core Flow Input | | | 05000324/LER-1980-010, Supplemental LER 80-010/03L-1:on 800114,during Normal Plant operation,OD-1 Determined That Max Critical Power Ratio Was Below Tech Specs for Bundle 43-28.Caused by Problems W/Low Power Range Monitor & Core Flow Input.Power Redu | Supplemental LER 80-010/03L-1:on 800114,during Normal Plant operation,OD-1 Determined That Max Critical Power Ratio Was Below Tech Specs for Bundle 43-28.Caused by Problems W/Low Power Range Monitor & Core Flow Input.Power Reduced | | | 05000325/LER-1980-011-03, /03L-0:on 800121,during 10-minute Run of HPCI Auxiliary Oil Pump,Stoppage Occurred When Switch Moved from Start to Auto Position.Caused by Loose Wire on RTGB Control Switch.Wire Reattached & Tightened | /03L-0:on 800121,during 10-minute Run of HPCI Auxiliary Oil Pump,Stoppage Occurred When Switch Moved from Start to Auto Position.Caused by Loose Wire on RTGB Control Switch.Wire Reattached & Tightened | | | 05000325/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000324/LER-1980-011-03, /03L-0:on 800110,when Time Was Entered on Computer After Reinitialization,Computer Had Software Stall & Could Not Be Kept on Line,Causing Temp Recorder CAC-7R-1258 to Be Inoperable.New Points Added to Sys | /03L-0:on 800110,when Time Was Entered on Computer After Reinitialization,Computer Had Software Stall & Could Not Be Kept on Line,Causing Temp Recorder CAC-7R-1258 to Be Inoperable.New Points Added to Sys | | | 05000324/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000325/LER-1980-012-03, /03L-0:on 800224,during Normal Plant Operation,Rip Valves,Variable Leg Isolation for Torus Level Transmitter & Variable Leg for Torus Level Pressure Switch Shut & Could Not Be Opened.Caused by Failure of Svc Air Compressors | /03L-0:on 800224,during Normal Plant Operation,Rip Valves,Variable Leg Isolation for Torus Level Transmitter & Variable Leg for Torus Level Pressure Switch Shut & Could Not Be Opened.Caused by Failure of Svc Air Compressors | | | 05000325/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000324/LER-1980-012-03, /03L-0:on 800116,while Performing Torus Water Level Calibr & Functional Check,Level Switch E41-LSH-NOI5A Would Not Actuate.Caused by Switch Out of Calibr.Instrument Recalibr | /03L-0:on 800116,while Performing Torus Water Level Calibr & Functional Check,Level Switch E41-LSH-NOI5A Would Not Actuate.Caused by Switch Out of Calibr.Instrument Recalibr | | | 05000324/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000324/LER-1980-013-03, /03L-0:on 800116,during Normal Operation, Containment Atmospheric Monitor CAC-AQH-1260 Monitor Breaker Had Tripped on Magnetics Rendering CAC-AQH-1262-2 Inoperable.Caused by Short in Power Lead.Lead Taped | /03L-0:on 800116,during Normal Operation, Containment Atmospheric Monitor CAC-AQH-1260 Monitor Breaker Had Tripped on Magnetics Rendering CAC-AQH-1262-2 Inoperable.Caused by Short in Power Lead.Lead Taped | | | 05000325/LER-1980-013-03, /03L-0:on 800125,while Performing Reactor Low Water Level 2 & 3 Channel Calibr & Functional Check,Low Pressure Switch 1B21-LITS-N031A-2 Failed to Actuate.Caused by Instrument Drift.Instruments to Be Replaced | /03L-0:on 800125,while Performing Reactor Low Water Level 2 & 3 Channel Calibr & Functional Check,Low Pressure Switch 1B21-LITS-N031A-2 Failed to Actuate.Caused by Instrument Drift.Instruments to Be Replaced | |
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