LER-1980-084, /03L-0:on 801128,switch PSL107D Would Not Reset After Actuating on Low Steam Pressure & Auxiliary Feedwater Sys Declared Inoperable.Caused by Defective Actuation Switch & Actuator in PSL107D.Parts Replaced |
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O.S. NUCLE AR REGULi TORY COMMISSION NRC FORM 363 87 77)
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60 61 DOCKET NUMBER 6d ta EVENT DATE F4 75 REPORT D ATE 80 EVENT OESCRIPTION AND PROSABLE CONSEQUENCES h lOl2l l (NP-33-E0-110) On 11/28/80 at approximately 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> while performine surveillance 1 l0l3l l testing, operations personnel noted that PSL107D would not reset after actuating on i
ITT71 I low steam pressure. With this pressure switch inoperable. Auxiliary Feedwater SystemI lO t si I 1-2 was declared inoperable. This placed the unit in the action statement of Technt-1 I cls l l cal Specification 3.7.1.2.
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[ o i 7 l l or to station personnel. Auxiliary Feedwater (AW) Train 1-1 was still operable.
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47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lijollThe cause was a defective actuation switch and actuator in PSL107D. The actuating i
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DVR 80-197 Dan haumm PHONE:
NAME OF PREPARMH.
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TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-80-110 j
DATE OF EVENT: November 28, 1980 FACILITY: Davis-Besse Unit 1 IDENTIFICATICM 01 OCCURRENCE: Auxiliary Feed Pump Turbine (AFPT) 1-2 Suction Line Pressure Switch PSL 107D Failed to Reset Conditions Prior to Occurrence: The unit was in Mode 1 with Power (MRI) = 2525 and Load (Gross MWE) = 853.
Description of Occurrence: On November 28, 1980 at approximately 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> during the performance of ST 5071.04, Auxiliary Feedwater Channel Functional Test, it was noted by operations personnel that PSL 107D would not reset after actuating on low steam PSL 107D is one of four pressure switches located between the AFPT trip throt-pressure.
tle valve and the AFFT steam isolation valve on each main steam line. The purpose of a main these pressure suitches is to close the AFPT main steam isolation valves should steam line break occur between the AFP room and the islation valves in the auxiliary building. The control logic requires actuation of both PSL 107A and PSL 107C or PSL 107B and PSL 107D to cause steam isolation to the AFPT. With this pressure switch inoperable h mfifary Feedwater System 1-2 was declared inocerable.
This placed the unit in the action statement of Technical Spec'ification 3.7.1.2 which states that with one Auxiliary Feedwater System inoperable, restore the inoperable system to operable stetus within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in hot shutdown with. n the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.
i Designation of Apparent Cause of Occurrence: The apparent cause of the occurrence was determined to be a defective actuation switch and actuator in PSL 107D. The actuating stem in the microswitch was worn.
Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. Auxiliary Feedwater Train 1-1 Vas still operable.
Corrective Action
Maintenance Work Order IC-802-80 was issued to perform maintenance on PSL 107D. PSL 107D was removed, the defective parts replaced and the repaired switch Multiple checks were made on the pressure switch calibration, both out' of sys-installed.
tem and in the system and results proved satisfactory. The applicable portion of ST 5071.04 was re-performed satisfactorily, and Auxiliary Feedwater Train 1-2 was declared operable at 2250 hours0.026 days <br />0.625 hours <br />0.00372 weeks <br />8.56125e-4 months <br /> on November 28, 1980.
Further investigation into the cause of the worn part will be undertaken.
Failure Data: There have been no previous similar occurrences of worn parts causing a pressure switch failure.
LER #80-084 u-
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