05000327/LER-1980-138-03, /03L-0:on 800801,during Heavy Thunderstorm,Cooling Tower Blowdown Line Effluent Monitor Declared Inoperable. Caused by Nearby Lightning Strike or Power Line Surge. Damaged Parts Being Repaired & Backup Channel Installed

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/03L-0:on 800801,during Heavy Thunderstorm,Cooling Tower Blowdown Line Effluent Monitor Declared Inoperable. Caused by Nearby Lightning Strike or Power Line Surge. Damaged Parts Being Repaired & Backup Channel Installed
ML19338C915
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 08/29/1980
From: Smithson J
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19338C914 List:
References
LER-80-138-03L, LER-80-138-3L, NUDOCS 8009080356
Download: ML19338C915 (1)


LER-1980-138, /03L-0:on 800801,during Heavy Thunderstorm,Cooling Tower Blowdown Line Effluent Monitor Declared Inoperable. Caused by Nearby Lightning Strike or Power Line Surge. Damaged Parts Being Repaired & Backup Channel Installed
Event date:
Report date:
3271980138R03 - NRC Website

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