ML19338C439

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LER 80-025/03L-0:on 800712,during Inservice Operability Testing,Turbine Driven Auxiliary Feed Pump Tripped Below Normal Trip Setpoint.Caused by Normal Wear of Emergency Tappet Nut.Nut Adjusted to Improve Contact W/Trip Lever
ML19338C439
Person / Time
Site: Millstone Dominion icon.png
Issue date: 08/07/1980
From:
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19338C436 List:
References
LER-80-025-03L, LER-80-25-3L, NUDOCS 8008150410
Download: ML19338C439 (1)


Text

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L VEtJ T Dlf,CnlPilON AND rnOD AOLE CONSLOUE'JCES h JB [ During inservice operabili_ty testing, the turbine driven auxiliary feed pump tripped 1 "

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[g l 670 rpm below the normal trip setpoint preveriting completion of surveillance require- l JB 1 mentsjer Technical Specification 4.7.1.2.b.2. The electric driven feed __p_umpLwere I ,

[B 1 verified, operable and the plant was operated in accordance with Action Statement i j The turbine driven auxiliary _feedlump__was returned to service within two 1 I

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. E l_liotmal_ wear _nf_the emer9cacyv__La_pnel_Dut (part no d 5_on Terry Turbine Drawinn A-9319) g l reduced holding force on the Yip lever such that normal machine vibration caused turbinEi

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