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Category:TECHNICAL SPECIFICATIONS
MONTHYEARML20217D7961999-10-12012 October 1999 Proposed Tech Specs Pages,Removing Turbine EHC Low Oil Pressure Trip from RPS Trip Function Requirements in TS Sections 2.2 & 3/4.1.A ML20210R8281999-08-13013 August 1999 Revised Bases Page B.3/4.9-6 to TS Section 3/4.9,providing Clarity & Consistency with Sys Design Description in UFSAR Sections 8.3.2.1 & 8.3.2.2 ML20209J2321999-07-16016 July 1999 Proposed Tech Specs 3/4.7.D Replacing Limit for Any One Msli Valve of Less than or Equal 11.5 Sfch with Aggregate Value of Less than or Equal 46 Scfh for All MSIVs ML20209C2951999-06-29029 June 1999 Proposed Tech Specs Section 3/4.3.C, Reactivity Control - Control Rod Operability ML20205L2631999-04-0505 April 1999 Tech Spec Page B 3/4.5-2 to TS Section 3/4.5, ECCS, to Clarify Requirement Discussed in ML20205J9321999-03-30030 March 1999 Proposed Tech Specs 3/4.6.E Changing SRs 4.6.E.2 to Allow one-time Extension of 18 Month Requirement to Pressure Test or Replace One Half of MSSVs to Interval of 24 Months ML20205J9911999-03-30030 March 1999 Proposed Tech Specs Allowing Alternative Methodology for Quantifying RCS Leakage When Normal RCS Leakage Detection Sys Is Inoperable ML20205J9741999-03-30030 March 1999 Proposed Tech Specs,Deleting Various License Conditions That Have Been Completed,Making Editorial Changes & Providing Clarifying Info ML20199L7741999-01-21021 January 1999 Proposed Tech Specs Bases for Sections 3/4.10.K & 3/4.10.L, Provides Description of Design & Operation of RHR SD Cooling Subsystem ML20199L6921999-01-21021 January 1999 Proposed Tech Specs Section 3/4.6.I,relocating from Chemistry TS Requirements to UFSAR ML20196H4571998-11-30030 November 1998 Proposed Tech Specs 3/4.8.J, Safe Shutdown Makeup Pump, Reducing Current AOT from 67 Days to 14 Days ML20196F6451998-11-30030 November 1998 Proposed Tech Specs 3/4.1.A,3/4.10.B & 3/4.12.B,proposing Changes to Relocate Requirement to Remove RPS Shorting Links Which Enable non-coincident Scram for Neutron Instrumentation,To Licensee Controlled Document ML20155D8091998-10-29029 October 1998 Proposed Tech Specs Bases Sections 3/4.2.D & 3/4.5.D, Providing Clarity & Consistency with Sys Design Description Contained in UFSAR Section 5.4.6.2 ML20151S7991998-08-31031 August 1998 Proposed Tech Specs,Increasing Max Allowable MSIV Leakage from 11.5 Scfh to 30 Scfh Per Valve When Tested at 25 Psig, IAW SR 4.7.D.6 ML20236W8401998-07-31031 July 1998 Proposed Tech Specs Bases 3/4.7.C & 3/4.7.12.C,clarifying Testing Requirements for Primary Containment Excess Flow Check Valves ML20247D7761998-05-0505 May 1998 Proposed Tech Specs Page B 3/4.4-1,changing Administrative Error.Bases for Net Quantity of Gallons for Solution Is Changed from 3254 (Correct Quantity) to 3245 ML20246Q3481998-04-29029 April 1998 TS Page B 3/4.5-3,reflecting Change to TS Bases for Section 3/4.5.C ML20217G1481998-03-27027 March 1998 Proposed Tech Specs Bases Section 3/4.5.A,reflecting Design Info Contained in Rev 4 to Ufsar,Dtd Apr 1997 ML20216C6381997-08-29029 August 1997 Proposed Tech Specs,Incorporating New Siemens' Methodologies That Will Enhance Operational Flexibility & Reducing Likelihood of Future Plant Derates ML20196G0271997-05-0101 May 1997 Proposed Tech Specs 4.9.A.8.b Revising Load Value for Diesel Generator to Be Equal to or Greater than Largest Single Load & Revising Frequency & Voltage Requirements During Performance of Test ML20138G3321997-04-29029 April 1997 Proposed Tech Specs,Permitting Loading of ATRIUM-9B Fuel in Plant Unit Core for Operational Modes 3,4 & 5.Modes Will Support Refueling Activities Such as Fuel Load,Vessel re- Assembly & Single Rod Timing ML20138B3231997-04-21021 April 1997 Proposed Tech Specs,Requesting That NRC Grant Exigent Amend to TS 2.1.B & 6.9.A.6.b to Support Plant Unit 2 Cycle 15 Operation Scheduled to Begin 970519 ML20137G3981997-03-26026 March 1997 Proposed Tech Specs 3/4.7.P Re Standby Gas Treatment & TS 5.2.C Re Secondary Containment ML20135F7321997-03-0303 March 1997 Proposed Tech Spec Bases 3/4.9.E,clarifying Purpose of SR 4.9.E ML20135D9461997-02-24024 February 1997 Proposed Tech Specs,Clarifying Bases for TS Surveillance 4.8.D.5.c ML20138L4011997-02-17017 February 1997 Proposed Tech Specs Section 2.1.B Re Thermal Power,Section 3/4.11 Re Power Distribution Limits,Section 3/4.6 Re Primary Sys Boundary,Section 5.3 Re Reactor Core & Section 6.9 Re Reporting Requirements ML20138L3701997-02-17017 February 1997 Proposed Tech Specs 4.9.A.8.h Re Diesel Generator Endurance Test Surveillance Requirements ML20134D2191997-01-27027 January 1997 Proposed Tech Specs Deleting marked-up Sentence from TS Bases for Section 3/4.7.K ML20129C2391996-10-16016 October 1996 Proposed Tech Specs for Dresden 2 & 3 & Quad Cities 1 & 2, marked-up to Show Transition Verbiage ML20129D3981996-09-20020 September 1996 Proposed Tech Specs 3/4.6.K,updating Pressure-Temp Curves to 22 Effective Full Power Yrs & TS Bases ML20113C3571996-06-25025 June 1996 Proposed Tech Specs Re Upgrade Program ML20113A7861996-06-10010 June 1996 Proposed Tech Specs,App A,To Reflect Transition of Fuel Supplier from General Electric to Siemens Power Corp ML20117D7121996-05-0606 May 1996 Proposed Tech Specs,Implementing New LCO & SR Re Revs to TS for 10CFR50,App J,Lrt ML20107A1881996-04-0404 April 1996 Proposed Tech Specs 3.4/4.4 Re Standby Liquid Control Sys ML20101H1381996-03-25025 March 1996 Complete Version of TS Upgrade Program Pages That Reflect Current Configuration of Plant & Specifies SRs That Will Not Be Current Upon Implementation of Tsup Project ML20097D9231996-02-0808 February 1996 Proposed Tech Specs,Upgrading Existing TS 3/4.5, Eccs ML20098A3821995-09-20020 September 1995 Proposed Tech Specs,Revising TS Upgrade Program & Improving Plant Submittals ML20086D4741995-06-30030 June 1995 Proposed Tech Specs Re TS Upgrade Program for Dresden Units 2 & 3 & Quad Cities Units 1 & 2 ML20087H8651995-05-0202 May 1995 Proposed Tech Specs Re TS Upgrade Program Section 3/4.10 ML20082H7481995-04-10010 April 1995 Proposed Tech Specs,Revising SR for HPCI & RCIC Sys ML20080K8171995-02-23023 February 1995 Proposed Tech Specs,Changing Name of Iige to Reflect Results of Merger Between Iige,Mid American Energy Co,Midwest Power Sys Inc & Midwest Resources Inc ML20078E2051995-01-20020 January 1995 Proposed Tech Specs Re Snubber Visual Insp Intervals ML20078Q6061994-12-12012 December 1994 Proposed TS Section 3.4/4.4 Re Standby Liquid Control Sys ML20064J3181994-03-11011 March 1994 Proposed Tech Specs Re Snubber Visual Insp Intervals ML20059A7321993-12-20020 December 1993 Proposed Tech Specs 1.1/2.1-1 Increasing MCPR Safety Limit from 1.06 to 1.07 for Units 1 & 2 ML20059A8301993-10-21021 October 1993 Proposed Tech Specs Deleting Requirements for Demonstrating Operability of Redundant Equipment When ECCS Equipment Is Found Inoperable or Made Inoperable for Maint ML20125D6381992-12-0808 December 1992 Proposed Tech Specs 3/4.1 Re Reactor Protection Sys ML20116J7091992-11-0606 November 1992 Corrected Proposed TS 3.2/4.2-8 Re Administrative Changes ML20106A6221992-09-15015 September 1992 Proposed TS 2.0, Safety Limits & Limiting Safety Sys Settings & 3/4.11, Power Distribution Limits ML20099D7791992-07-29029 July 1992 Proposed Tech Specs Sections 1.0, Definitions, 3/4.0, Applicability & 3/4.3, Reactivity 1999-08-13
[Table view] Category:TECHNICAL SPECIFICATIONS & TEST REPORTS
MONTHYEARML20217D7961999-10-12012 October 1999 Proposed Tech Specs Pages,Removing Turbine EHC Low Oil Pressure Trip from RPS Trip Function Requirements in TS Sections 2.2 & 3/4.1.A ML20210R8281999-08-13013 August 1999 Revised Bases Page B.3/4.9-6 to TS Section 3/4.9,providing Clarity & Consistency with Sys Design Description in UFSAR Sections 8.3.2.1 & 8.3.2.2 ML20209J2321999-07-16016 July 1999 Proposed Tech Specs 3/4.7.D Replacing Limit for Any One Msli Valve of Less than or Equal 11.5 Sfch with Aggregate Value of Less than or Equal 46 Scfh for All MSIVs ML20196K1941999-06-30030 June 1999 Rev 2.0 to Chapter 11 of Quad Cities Offsite Dose Calculation Manual ML20209C2951999-06-29029 June 1999 Proposed Tech Specs Section 3/4.3.C, Reactivity Control - Control Rod Operability ML20211C3311999-04-30030 April 1999 Rev 2.0 to Generic ODCM for Dresden,Quad Cities,Zion, Lasalle,Byron & Braidwood ML20205L2631999-04-0505 April 1999 Tech Spec Page B 3/4.5-2 to TS Section 3/4.5, ECCS, to Clarify Requirement Discussed in ML20205J9741999-03-30030 March 1999 Proposed Tech Specs,Deleting Various License Conditions That Have Been Completed,Making Editorial Changes & Providing Clarifying Info ML20205J9321999-03-30030 March 1999 Proposed Tech Specs 3/4.6.E Changing SRs 4.6.E.2 to Allow one-time Extension of 18 Month Requirement to Pressure Test or Replace One Half of MSSVs to Interval of 24 Months ML20205J9911999-03-30030 March 1999 Proposed Tech Specs Allowing Alternative Methodology for Quantifying RCS Leakage When Normal RCS Leakage Detection Sys Is Inoperable ML20199L6921999-01-21021 January 1999 Proposed Tech Specs Section 3/4.6.I,relocating from Chemistry TS Requirements to UFSAR ML20199L7741999-01-21021 January 1999 Proposed Tech Specs Bases for Sections 3/4.10.K & 3/4.10.L, Provides Description of Design & Operation of RHR SD Cooling Subsystem ML20196H4571998-11-30030 November 1998 Proposed Tech Specs 3/4.8.J, Safe Shutdown Makeup Pump, Reducing Current AOT from 67 Days to 14 Days ML20196F6451998-11-30030 November 1998 Proposed Tech Specs 3/4.1.A,3/4.10.B & 3/4.12.B,proposing Changes to Relocate Requirement to Remove RPS Shorting Links Which Enable non-coincident Scram for Neutron Instrumentation,To Licensee Controlled Document ML20196K5861998-11-0505 November 1998 Rev 3 to Qcap 0280-01, Process Control Program for Processing of Radioactive Wet Wastes at Quad Cities Nuclear Power Station ML20155D8091998-10-29029 October 1998 Proposed Tech Specs Bases Sections 3/4.2.D & 3/4.5.D, Providing Clarity & Consistency with Sys Design Description Contained in UFSAR Section 5.4.6.2 ML20195J9041998-09-24024 September 1998 Rev 0 to TR-VQ1500-02, Clean ECCS Suction Strainer Head Loss Test Rept ML20151S7991998-08-31031 August 1998 Proposed Tech Specs,Increasing Max Allowable MSIV Leakage from 11.5 Scfh to 30 Scfh Per Valve When Tested at 25 Psig, IAW SR 4.7.D.6 ML20236W8401998-07-31031 July 1998 Proposed Tech Specs Bases 3/4.7.C & 3/4.7.12.C,clarifying Testing Requirements for Primary Containment Excess Flow Check Valves ML20247D7761998-05-0505 May 1998 Proposed Tech Specs Page B 3/4.4-1,changing Administrative Error.Bases for Net Quantity of Gallons for Solution Is Changed from 3254 (Correct Quantity) to 3245 ML20246Q3481998-04-29029 April 1998 TS Page B 3/4.5-3,reflecting Change to TS Bases for Section 3/4.5.C ML20217G1481998-03-27027 March 1998 Proposed Tech Specs Bases Section 3/4.5.A,reflecting Design Info Contained in Rev 4 to Ufsar,Dtd Apr 1997 ML20216C6381997-08-29029 August 1997 Proposed Tech Specs,Incorporating New Siemens' Methodologies That Will Enhance Operational Flexibility & Reducing Likelihood of Future Plant Derates ML20196G0271997-05-0101 May 1997 Proposed Tech Specs 4.9.A.8.b Revising Load Value for Diesel Generator to Be Equal to or Greater than Largest Single Load & Revising Frequency & Voltage Requirements During Performance of Test ML20138G3321997-04-29029 April 1997 Proposed Tech Specs,Permitting Loading of ATRIUM-9B Fuel in Plant Unit Core for Operational Modes 3,4 & 5.Modes Will Support Refueling Activities Such as Fuel Load,Vessel re- Assembly & Single Rod Timing ML20138B3231997-04-21021 April 1997 Proposed Tech Specs,Requesting That NRC Grant Exigent Amend to TS 2.1.B & 6.9.A.6.b to Support Plant Unit 2 Cycle 15 Operation Scheduled to Begin 970519 ML20137G3981997-03-26026 March 1997 Proposed Tech Specs 3/4.7.P Re Standby Gas Treatment & TS 5.2.C Re Secondary Containment ML20135F7321997-03-0303 March 1997 Proposed Tech Spec Bases 3/4.9.E,clarifying Purpose of SR 4.9.E ML20135D9461997-02-24024 February 1997 Proposed Tech Specs,Clarifying Bases for TS Surveillance 4.8.D.5.c ML20138L4011997-02-17017 February 1997 Proposed Tech Specs Section 2.1.B Re Thermal Power,Section 3/4.11 Re Power Distribution Limits,Section 3/4.6 Re Primary Sys Boundary,Section 5.3 Re Reactor Core & Section 6.9 Re Reporting Requirements ML20138L3701997-02-17017 February 1997 Proposed Tech Specs 4.9.A.8.h Re Diesel Generator Endurance Test Surveillance Requirements ML20134D2191997-01-27027 January 1997 Proposed Tech Specs Deleting marked-up Sentence from TS Bases for Section 3/4.7.K ML20129K3321996-10-18018 October 1996 Cycle 15 Startup Test Results ML20129C2391996-10-16016 October 1996 Proposed Tech Specs for Dresden 2 & 3 & Quad Cities 1 & 2, marked-up to Show Transition Verbiage ML20129D3981996-09-20020 September 1996 Proposed Tech Specs 3/4.6.K,updating Pressure-Temp Curves to 22 Effective Full Power Yrs & TS Bases ML20216H8841996-06-30030 June 1996 Revs to ODCM for Quad Cities,Including Rev 1.8 to Chapters 10,11,12 & App F ML20116F3971996-06-30030 June 1996 Rev 1.8 to ODCM, Annex,Chapters 10,11,12 & App F ML20113C3571996-06-25025 June 1996 Proposed Tech Specs Re Upgrade Program ML20113A7861996-06-10010 June 1996 Proposed Tech Specs,App A,To Reflect Transition of Fuel Supplier from General Electric to Siemens Power Corp ML20117D7121996-05-0606 May 1996 Proposed Tech Specs,Implementing New LCO & SR Re Revs to TS for 10CFR50,App J,Lrt ML20107A1881996-04-0404 April 1996 Proposed Tech Specs 3.4/4.4 Re Standby Liquid Control Sys ML20101H1381996-03-25025 March 1996 Complete Version of TS Upgrade Program Pages That Reflect Current Configuration of Plant & Specifies SRs That Will Not Be Current Upon Implementation of Tsup Project ML20097D9231996-02-0808 February 1996 Proposed Tech Specs,Upgrading Existing TS 3/4.5, Eccs ML20100C0441996-01-24024 January 1996 Secondary Containment Leak Test Summary ML20093K7721995-10-12012 October 1995 Quad-Cities Nuclear Power Station Unit 2 Cycle 14 Startup Test Results Summary ML20098A3821995-09-20020 September 1995 Proposed Tech Specs,Revising TS Upgrade Program & Improving Plant Submittals ML20086D4741995-06-30030 June 1995 Proposed Tech Specs Re TS Upgrade Program for Dresden Units 2 & 3 & Quad Cities Units 1 & 2 ML20087H8651995-05-0202 May 1995 Proposed Tech Specs Re TS Upgrade Program Section 3/4.10 ML20082H7481995-04-10010 April 1995 Proposed Tech Specs,Revising SR for HPCI & RCIC Sys ML20080K8171995-02-23023 February 1995 Proposed Tech Specs,Changing Name of Iige to Reflect Results of Merger Between Iige,Mid American Energy Co,Midwest Power Sys Inc & Midwest Resources Inc 1999-08-13
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-OPR-29 i TABLE 3.7-1 (Cont'd)
PRIMARY CONTAINMENT ISOLATION Valve Number Number of Maxinum-for i Power-Operated Operating Normal- Action oi Isolation- -Valve- Units Valves Time Operating Group-Identification 1 and 2 Inboard Outboard (sec) Position InitiatiI; Signal
' 1 2 Reactor
" shutdown !
cooling
-supply MD-1001-47~ 1
- 2. Reactor 140 C SC shutdown cooling i suppg, M0-1001-50 1 140 C- SC
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Pressure Suppression '
E 2 Drywell purge-i valve A0-1601-21 1
<10 C SC
.2 Vent valve A0-1601-22 1 710 C SC 2 ~ Drywell vent valve A0-1601-23 1 -
<10 C SC 2 ~ Vent to reactor
' building -
exhaust systes' A0-1601-24 1 110 C SC 2 Nitrogen <
purge A0-1601-55 1 110 0 GC l 2 Torus purge i
valve A0-1601-56 1 <10 0 GC
- 2. Makeup valve MD-1601-57 1 715
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'2- Torus askeup '
valve A0-1601-58 1 115 C SC l 3.7/4.7-34 Amendment No.'114
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TA8LE 3.7-2 1 bs in y PRIMARY:CONTAINMENTlLEAKAGE TEST PENETRATIONS I iDouble-Gasketed Seals'-
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Personnel air _ lock h-4-61. .
! Control. rod drive hatch i'
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-J j- LX-200A & 8' < Suppression chamber access' hatch 1
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L(inspection. hatch)> ) 1 j- y Pipe Pene'tratio' ns ~
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-X-8 X-7A through D.: Main steam't Main steamline' drain l
. .X-9AL& 8-- :Feedwater
- X.10 .-Reactor core isolation cooling -
X-11 -High pressure coolant injection
.X l Residual heat removal s
%i 'X-13A & BL Residual heat removal a
- X - Reactor. coolant cleanup P .X-16A'~& 8. > Core spray
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.X-23 & 24 o iReactor building closed cooling water -
.X-25426 Orywe111 ventilation .. .
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1X-47 : Standby liquid control' .
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' Current Technical Specifications 3.7.D 2 requires that all Isolation Valves contained in Table 3.7-1 be operable during reactor power operation.
Table 3.7-1 contains a description and associated requirements for operating position and operating time for reactor head spray valves HO-1001-60 and H0-1001-63. In addition. Table 3.7-2 describes the Primary Containment 1.eakage L.. : Test Penetrations which includes penetrations for the reactor vessel head t
~ spray and CRD return lines.
The proposed Technical Specification deletes the reference to the reactor vessel head spray and CRD return lines from Table 3.7-1 and 3.7-2 as a l
' result-of-the removal of these lines.
The modifications to the reactor vessel head spray and CRD return lines:were performed as part of the Station's Intergranular Stress Corrosion Cracking ~ mitigation program, as put forth in the response to Generic l.etter 88-01. The piping was determined to be unnecessary and susceptible to IGSCC.
The head spray system provided a means to augment reactor cooldown
-and reduction of pressure following a shutdown. The head-spray system is part i of the Residual Heat Removal system and allows water to be diverted to a spray J nozzle in the steam dome of the vessel. The-operation of the head spray '
system during reactor shutdown is optional. The system is not used to mitigate accidents or.during normal reactor operation, j The CRD return line was previously removed from service to prevent thermal stresses on the reactor vessel due to temperature differential caused ~
by the return of cooler CRD water. The CRD return line provided a return flowpath'to the reactor vessel following CRD movement. The current return flowpath.is reverse flow through the exhaust header and return to the vessel through the CRD seals. Since the return line was capped, the piping was not utilized during any mode of operation.
As a result of the removal of the llead Spray piping, valves H0-1001-60 and HO-1001-63 were eliminated. These valves provided for containment isola-tions and were normally closed. -The valves received a close signal during a Group II initiation signal (low reactor water level, high drywell pressure, or high drywell radiation levels). The remaining plping (reactor side) is blind flanged which provides for-isolation of the pressure boundary. The blind
, flange provides the same or greater level of reactor pressure boundary as the removed isolation valve. j 1
The removal of the CRD return line and head spray piping resulted in the closure of two drywell penetrations which were listed on Table 3-7.2. l This Table delineates the penetrations which require Type C local leak rate testing. The integrity of the penetration closure will continue to be tested ,
during containment integrated leak rate test. The closure of the penetrations l eliminate possible leakage path from containment. The penetration cap was designed to be consistent with containtment design pressures and temperature, f
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AUMMif.KL5 BbS1S FOR NO SlGNIFICANT HAZARDS DETERMIEM10B
,As discussed in the Description of the Proposed Amendment Request, the proposed change revises the current Technical Specification listing for the primary containment isolation valves and primary containment leakage-test penetration.
The changes have been reviewed by Commonwealth Edison. Based on this review, Commonwealth Edison does not believe the changes present a Significant Hazards Consideration. The basis-for the determination is documented below.
Commonwealth Edison has evaluated this proposed amendment and determined that the changes does not involve a,significant hazards consideration. In accordance with 10 CFR 50.92(c):
- 1. The proposed change does not involve a significant increase In the probability or consequence of an accident previously evaluated. 4 I
The probability of a pipe. leak and/or break due to intergranular stress j corrosion cracking (IGSCC) is reduced by the removal of the Head Spray and l Control Rod Drive return lines. The removal of the Head Spray line reduces l the consequences of a loss of coolant accident (LOCA) due to the elimina- i tion of a vessel leakage path. The hydrostatic test of the vessel, performed each cycle, will assure the integrity of the installed blind flange. j i
The probability of an accident is not affected by the closure of the penetrations. The consequences of an accident is reduced since the closed penetrations will not be available as a possible Primary Containment leakage path. The leak tightness of the penetrations will be verified by l the integrated leak rate test (ILRT). The penetration cap is designed to withstand containment design pressures and temperatures.
Finally, since neither the CRD return line nor.the Head Spray system are utilized to mitigate any accident scenarlo, the elimination of the Head Spray system and the CRD return line does not increase the probability or
. consequences of any accident previously evaluated. .j i
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- 2. The proposed change will not create the possibility of a new or different I kind of accident from any previously evaluated.
2 No new interfaces with safety-related equipment, systems or structures or :
any new systems subject to failure or malfunction have been introduced. !
1he proposed change does not introduce any new operational modes. The j
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_ Head Spray system and CRD Return Line were not used for accident mitiga-tion, normal operation or shutdown (use-of Head Spray during.a shutdown is optional). Consequently, the removal will not result on the use of other systems in new or unanalyzed methods. No new or different kinds or accidents from any previously evaluated is therefore created.
- 3. .The proposed _ change does.not involve a significant reduction in the' margin of safety.
The margin of. safety is unchanged as a result of the removal of three possible pathways for leakage. The possibility of failure due to IGSCC in
'the removed piping systems is eliminated as is the possibility of. leakage through the Head Spray-Containment Isolation Valves. The current configuration of the blind flange (reactor side) and pipe cap (RHR side) provides for an adequate isolation of the piping. Reactor vessel hydrostatic ~ testing will ensure integrity of the current configuration.
Closing'the penetrations in the drywell also reduces the possibility of Primary Containment leakage' through these paths. Penetration closure integrity is vertfled using ILRT.
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