LER-1980-066, /01T-0:on 800907,reactor Core Isolation Cooling Turbine Tripped on High Turbine Exhaust Pressure.Caused by Improper Valve Positioning Apparently Due to Personnel Error |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3241980066R01 - NRC Website |
|
text
LQiciDNSEL9EF1eis a etesa to>tm o
- ~ - - - ~ - - - -
e s.
1, I
1 1
1 1 p (PLEASE PRINT C3 TYPE ALL RECUIRED INFORMATION)
CoranOL 8tOCx:
8 InlClalElpl21@l0l01-l010101010l-Inlol@l411lililil@l l
Ig 7
8 8 LICENSEE CODE 34 Il L6 CENSE NUMUER 26 26 LICENSE TYPE JO
$7 CATLa CON 7 3$O l 0 l 5 l 0 l - ] O l 3 l 2 l 4 @l 0 I 9 l 0 l 7 l 8 l 0 l@l o l 9 l 1 l 9 l 8 l o l@
o 1 7
4 60 64 DOCsCET NUM8ER 64 69 EVLNT DATE 74 75 REPORT DATE to EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h l o l 2 l lVnile performing the Unit No. 2 RCIC Flow Rate Test at 150 psin reactor pressure.
I l the RCIC turbine tripped on high turbine exhaust pressure. An investigation re-I o 3 l o 141 Ivealed the manually operated stop check in the RCIC turbine exhaust to the torus was I
o s ] locked in the closed position.
In addition the manually operated stop check in the l
[5"lT] lHPCI turbine exhaust to the torus was checked and also found in the closed position.
I 10171 1 I
Technical Specification 3.5.1, 3.7.4, 6.9.1.8f
, o ;g ; ;
5sCiOE COMPONENT CODE SUS O'E E
C C0OE Ffsl I C I E j@ [Aj@ l Bl@ l V l A l L l V l E l X lh W@ l Al @
7 8
9 10 11 12 13 18 IS 23 SEQUENTIAL OCCURRENCE REPORT R EVISION l
LER EVENT YE AR REPORT NO.
CODE TYPE N O.
@,agg/RO 18101 l-l 101616l M
10111 I Tl l-l l0 l
_ 28 22 23 24 26 27 28 23 30 31 32 k
AC 0-ON PLANT HOURS 22 5P IT FORit B.
5 PPLIE MAN FA TURER lXlglJ4X lg lb lg W@
l0l0l010l l Y l@
lYl@
lNl@
lAl3l9l5l@
Z 33 J
36 37 43 41 42 43 44 4y CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l i l o ] lSee attachment.
I li lii l i
Frm i I
i a l I
i 4 I
l 7
8 9 80 ST F
% POWE R OTHERSTATUS 5 QV RY OISCOVErtY DESCR:7T10N I
l@ l l
l l@l NA l
l l@l l
i >
'8 ACuviTv CO TENT RELE ASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELE ASE li Is l 17 l @ l ZI@l NA l
l NA l
PE R50n'Ei E xrO5eES TvPE @lDESCni, TION @
~UvoEn ITTTl 1010 l0 l@l l
NA l
,ERSO~~Et mmLS R,PnON@
~ueui o eES:
l 0 l 0 l 0 l@l.
NA l
i s 7
8 9 19 12 40 LD55 OF OH 04 MAGE TO FACILITY TYPE C E 5C R:'itON lZl@l NA l
i o 7
8 9 10 63 g$gn:PTjQN e
igi.glS!
NA i
il i t iiiiii ii l!
l 2 o 8 9 IJ 68 69
- 83. ;;;
NAME Or rREPARtR PHONE?
80092606'39
e O
- LER ATTICINEI'T - RO NO. 2-80-62 Facility: BSEP Unit No. 2 Event Date:
9-7-80 Title:
HPCI and RCIC Turbine Exhaust Manual Stop Check Valves - Found Closed Initial Conditions:
. Unit No. 2 was in the startup mode on September 7,1980, at approximately 150 psig. The unit had started up on September 3,1980, following the 1980 refueling / maintenance outage.
Reactor pressure had been up to approximately 180 psig during unit starcup. The unit had been held in the startup mode due
~
to problems with condenser leaks, condensate leaks, and HPCI control valve problem during the period from September 3-7, 1980.
Event Descript'fon:
At approximately 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br /> on September 3, 1980, an attempt was made to test RCIC at 150 psig reactor pressure. The RCIC turbine tripped on high exhaust pressure. A subsequent investigation revealed that the RCIC turbine exhaust manual stop check ~ valve (8" Anchor - Rising Handwheel), RCIC F001, was in the locked-closed position.
The HPCI turbine exhaust manual stop-check valve (20" Anchor - Rising Stem),
HPCI F021, was also checked and found to be in the closed position without a lock. Eoth valves, RCIC F001 and HPCI F021, are required to be in the 1ccked open position for normal operation. These valves are containment isolation valves on turbine exhaust lines which penetrate the torus.
Cause Description:
An investigation was initiated following the event to determine the cause of the valves being in the wrong position. The apparent cause is personnel The following~ is a chronology of events related to both valves:
error.
1.
Unit No. 2 reactor was shut down to begin the refueling / maintenance outage on March 1, 1980.
2.
Equipment Clearance No. 2-429 was placed in effect for the torus modification on March 4, which aligned valves RCIC F001 and HPCI F021 in the shut position.
3.
A leak rate test was performed on HPCI F021 in accordance with PT 20.3 on April 7.
Test data sheet shows that the valve was returned to the open position after the test.
6 h
e O
7
e O
Cause Description:
(Cont'd) 4.
The torus clearance was removed on June 14.
Valve alignmant sheets, which require double initials, indicate both valves were restored to the locked opea position.
5.
A leak rate test was performed on valve RCIC F001 in accordance with PT 20.3 on June 26.
Equipment Clearance No. 2-528 hung for this test was cancelled on June 27 and indicated the valve was restored to the shut position.
6.
The RCIC System lincup was co=pleted on July 13.
This lineup indicates that valve RCIC F001 was locked open. The HPCI lineup was apparently mfsplaced and could not be-located.
It was verified as having been accomplished.
7.
Locked valve PT 46.1 was completed on August 28.
Valves RCIC F001 and HPCI F021 were indicated as locked open.
8.
The Unit No. 2 reactor startup occurred on September 3.
An investigation of the known events which involved repositioning or verifying valve position revealed the following:
1.
No instruction exists in PT 20.3 for positioning a valve uhan it cust be Icft in a position other than the normal position.
2.
Certain auxiliary operators performing valve lincups and clearance removals had not completed their qualifications on cicarances or on the systems where these clearances applied.
3.
The auxiliary operators involved in these clearances (which require t
doubic initials) did not independently verify cach valve.
4.
Evidence indicates that some individuals involved did not personally verify valve position.
5.
There was insufficient procedural guidance on how to handle and document unusual situations encountered in valve 11ncups such as interference by cicarances.
6.
Required review of the valve lineups was conducted in insufficient detail to detect these problems.
Corrcetive Actions:
In=cdiate Corrective Action:
1.
Both calves were immediately reponitioned to open and locked.
2.
A complete HPCI lineup was performed with no additional lineup discrepancies found.
2
\\
e e
9 O
Followup Corrective Action:
l.
Instructions were placed in the Daily Instruction to remind all shif ts to use only operators qualified to hang and cancel clearances.
2.
Locked valve PT 46.1 was performed twice on each unit. Valve RCIC-F002 (2" Velan Globe), vacuum pump discharge to the suppression pool, was found locked closed on Unit No. 2.
The valve was repositioned to open and locked. This valve did not render RCIC inoperative.
3.
Based on three valves being found out-of-position, an analysis was performed on Unit No. 2 to determine the necessity for repeating system lineups for Technical Specification systems. The analysis considered the following:
a.
Demonstrated operability.
b.
Remote position indication.
c.
Teclinical Specificatio.n required surveillance tests.
d.
Current lock-valve pts.
Repeat valve lineups on systems where items a-d were not sufficient c.
to positively conclude that system operability was assured.
The following lineups were repeated:
a.
Standby Liquid Control.
b.
Service Water in the Diesel and Reactor Buildings.
Nuclear Boiler - Outside the Drywell.
c.
d.
Reactor Protection.
No discrepancies were found during these lineup checks.
Unit No. 1 lineups were nct repeated based on:
Completion of the last startup program including startup pts and a.
testing o,f ECCS systems.
b.
Demonstrated operability of syste=s.
c.
Remote position indication on RTGB.
d.
Double verification of the locked-valve PT on September 8,19S0.
3 9
e e
e o
Followup Corrective Action:
(Cont'd) 4.
A meeting was held between Operations management personnel (Manager-Operations, Shif t Operating Supervisors, and Shif t Foremen), the Manager-Plant Operations, the plant General Manager, and the Vice President-Nuclear Operations on September 18', 1980. The seriousness of this event and the absolute need to prevent any future occurrences of this type were stressed. Causes and corrective actions were covered.
Management philosophy regarding what is expected of operators and what should be demanded f rom them was discussed.
It was also discussed that absolute integrity is required from cach operator and that deviations from that will result in disciplinary action. Methods for better utilization of management time and training of auxiliary operators were also discussed.
5.
As a followup to Item 4, special off-shift meetings are being held with all shif t personnel to ensure tbnir full understanding of this event and its seriousness.
Permanent Corrective Action:
1.
The clearance procedure will be revised to require that auxiliary operators be qualified on the safety-related systems before hanging or removing clearances on those systems.
For restoring the systems to normal, the person verifying the valve position will also be qualified.
2.
A procedure will be developed on the methods for performing system lineups (including removing clearances and restoring the system lineup). The procedure will include the following:
7' Proper method of checking valve position.
a.
b.
Procedure to be followed in the event exceptions, such as clearance tags, are encountered.
c.
Method of performing double verification.
d.
How to verify position of locked valves.
Who can and cannot perform valve lineups.
c.
3.
Training Instruction, TI-104, will be revised to indicate on-the-job training requirements for:
a.
Hanging and removing clearances.
b.
- Valvo lineups.
4 s
e
.o o
Permanent Corrective Action:
l 4.
Operating procedures will be revised to require that valve lineups for safety systems include verification of cach valve position by a second individual.
5.
General Operating Procedure, CP-1, will be revised to require verifi-cation that valve lineup sheets have been completed.
6.
This LER will be reviewed with all shif t personnel by Shif t Operating Supervisors with emphasis on:
The seriousness of this event and what it can lead to.
b.
Disciplinary action or dismissal will result f rom poor perfor-mance in this area.
7.
PT 20.3 will be revised to accomplish the following:
~
n.
Double verification of restored lincups, b.
. Require signature of persons who actually verified the lineup.
c.
Provide guidance on valves which cannot be restored to normal operating position at the time.
8.
Appropriate corrective or disciplinary actions for individuals and supervisors involved in this event are being taken.
m 5
6 9
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000325/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000325/LER-1980-001-03, /03L-0:on 800102,during Normal Operation, Containment Atmospheric Monitor Had Step Increase of Approx 2%.Caused by Instrument Drift.Instrument Recalibr & Returned to Svc | /03L-0:on 800102,during Normal Operation, Containment Atmospheric Monitor Had Step Increase of Approx 2%.Caused by Instrument Drift.Instrument Recalibr & Returned to Svc | | | 05000324/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000324/LER-1980-001-03, /03L-0:on 800117,during Attempt to Start RHR Room Cooler 2A,breaker Tripped on Magnetics.Cause Could Not Be Determined Due to Inoperable Room Cooler 2B.Breaker Reset & Closed | /03L-0:on 800117,during Attempt to Start RHR Room Cooler 2A,breaker Tripped on Magnetics.Cause Could Not Be Determined Due to Inoperable Room Cooler 2B.Breaker Reset & Closed | | | 05000324/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000324/LER-1980-002-03, /03L-0:on 800102,during Normal Reactor Startup,Rod Sequence Control Sys Would Not Allow Rods to Be Pulled Until Rod 34-27 Was Bypassed full-in. Caused by Defective full- in Reed Switch.Switch Will Be Repaired or Replaced | /03L-0:on 800102,during Normal Reactor Startup,Rod Sequence Control Sys Would Not Allow Rods to Be Pulled Until Rod 34-27 Was Bypassed full-in. Caused by Defective full- in Reed Switch.Switch Will Be Repaired or Replaced | | | 05000325/LER-1980-002-03, /03L-0:on 800106,during Normal Operation,Point 4 of Chloride Intrusion Monitor 1-CO-CR24 Was Reading Downscale.Caused by Defective Relay & Dirty Contacts.Relay Replaced,Contacts Cleaned & Recorder Returned to Svc | /03L-0:on 800106,during Normal Operation,Point 4 of Chloride Intrusion Monitor 1-CO-CR24 Was Reading Downscale.Caused by Defective Relay & Dirty Contacts.Relay Replaced,Contacts Cleaned & Recorder Returned to Svc | | | 05000325/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000324/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000324/LER-1980-003-03, /03L-0:on 800103,during Reactor Startup,Vessel Conductivity Exceeded 2 Umho for 31-h.Caused by Auxiliary Boilers Being Isolated for Months & Supply Lines Containing Stagnant,High Conductivity Water | /03L-0:on 800103,during Reactor Startup,Vessel Conductivity Exceeded 2 Umho for 31-h.Caused by Auxiliary Boilers Being Isolated for Months & Supply Lines Containing Stagnant,High Conductivity Water | | | 05000325/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000325/LER-1980-003-03, /03L-0:on 800114,channel Calibr CST Level Switch 1E41-LSL-N002 Found to Actuate at 23 Feet Decreasing.Caused by Switch Out of Calibr.Instrument Calibr & Returned to Svc | /03L-0:on 800114,channel Calibr CST Level Switch 1E41-LSL-N002 Found to Actuate at 23 Feet Decreasing.Caused by Switch Out of Calibr.Instrument Calibr & Returned to Svc | | | 05000325/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000325/LER-1980-004-03, /03L-0:on 800308,during Normal Plant Operation, Oxygen Channel of Containment Atmospheric Monitor CAC-AT- 1263-2 Experienced 1% Step Change.Caused by Possible Wiring or Connection Problem.Monitor Repair Is Underway | /03L-0:on 800308,during Normal Plant Operation, Oxygen Channel of Containment Atmospheric Monitor CAC-AT- 1263-2 Experienced 1% Step Change.Caused by Possible Wiring or Connection Problem.Monitor Repair Is Underway | | | 05000324/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000324/LER-1980-004-03, /03L-0:on 800127,during Normal Operations, Containment Atmospheric Monitor CAC-AT-1263 Kept Shutting Down Due to Low Flow Following Inerting Operation of Drywell.Cause Undetermined.Instruments to Be Replaced | /03L-0:on 800127,during Normal Operations, Containment Atmospheric Monitor CAC-AT-1263 Kept Shutting Down Due to Low Flow Following Inerting Operation of Drywell.Cause Undetermined.Instruments to Be Replaced | | | 05000325/LER-1980-005-03, /03L-0:on 800113,while Performing Control Rod Operability Check,Control Rod 42-35 Had No Position Indication at Notch 47.Caused by Fault in Reed Switch in Prototypic Inlet Piping Probe | /03L-0:on 800113,while Performing Control Rod Operability Check,Control Rod 42-35 Had No Position Indication at Notch 47.Caused by Fault in Reed Switch in Prototypic Inlet Piping Probe | | | 05000325/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000324/LER-1980-005-03, /03L-0:on 800105,during Normal Operation,Found Isolation Valve for Pressure Switch 2-E11-PS-N010D Shut. Cause Unknown.Counselled Personnel on Necessity to Follow Procedures to Ensure Proper Instrumentation Svc | /03L-0:on 800105,during Normal Operation,Found Isolation Valve for Pressure Switch 2-E11-PS-N010D Shut. Cause Unknown.Counselled Personnel on Necessity to Follow Procedures to Ensure Proper Instrumentation Svc | | | 05000324/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000325/LER-1980-006-03, /03L-0:on 800225,while Working on Trouble Ticket Re Position Indication for RIP Valve 49B,discovered Valve Not Closing Fully When Given Closing Signal.No Cause Stated. Valve Will Be Repaired During 1980 Refueling Outage | /03L-0:on 800225,while Working on Trouble Ticket Re Position Indication for RIP Valve 49B,discovered Valve Not Closing Fully When Given Closing Signal.No Cause Stated. Valve Will Be Repaired During 1980 Refueling Outage | | | 05000325/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000324/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000324/LER-1980-006-03, /03L-0:on 800103,during Normal Startup,Control Rod 26-07 Had No Position Indication at Notch 48.During 800109 Startup,Rod 34-35 Had No Indication at Notch 7.Caused by Faulty Reed Switches in Prototypical Inlet Piping Probes | /03L-0:on 800103,during Normal Startup,Control Rod 26-07 Had No Position Indication at Notch 48.During 800109 Startup,Rod 34-35 Had No Indication at Notch 7.Caused by Faulty Reed Switches in Prototypical Inlet Piping Probes | | | 05000324/LER-1980-007-03, /03L-0:on 800204,when Plant Batteries Were Placed in Equalize,Steam Leak Detection a Logic Topaz Inverter, Model 125-GW 12560,tripped.Caused by Improper Setting on Inverter High Voltage Trip.Inverter Trips Recalibr | /03L-0:on 800204,when Plant Batteries Were Placed in Equalize,Steam Leak Detection a Logic Topaz Inverter, Model 125-GW 12560,tripped.Caused by Improper Setting on Inverter High Voltage Trip.Inverter Trips Recalibr | | | 05000324/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000325/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000325/LER-1980-007-03, /03L-0:on 800114,during Normal Operation,Torus Level Indicator CAC-LI-3342 on Remote Shutdown Panel Was Not in Agreement W/Others in Control Room.Caused by Air Trapped in Demineralizer Water Line to Ref Leg.Instrument Recali | /03L-0:on 800114,during Normal Operation,Torus Level Indicator CAC-LI-3342 on Remote Shutdown Panel Was Not in Agreement W/Others in Control Room.Caused by Air Trapped in Demineralizer Water Line to Ref Leg.Instrument Recalibr | | | 05000324/LER-1980-008-03, /03L-0:on 800110,while Performing Reactor Core Isolation Cooling Instrument Check,Reactor Core Isolation Cooling Trip & Throttle Valve MOV-V8 Would Not Trip.Caused by Burned Solenoid.Solenoid Repaired | /03L-0:on 800110,while Performing Reactor Core Isolation Cooling Instrument Check,Reactor Core Isolation Cooling Trip & Throttle Valve MOV-V8 Would Not Trip.Caused by Burned Solenoid.Solenoid Repaired | | | 05000324/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000325/LER-1980-008-03, /03L-0:on 800115,while Attempting to Start RHR Svs Water Pump 1D to Check for Flange Leaks,Low Suction Pressure Annunciator Would Not Clear,Making B Loop Inoperable.Caused by Failure to re-energize Circuit 19 | /03L-0:on 800115,while Attempting to Start RHR Svs Water Pump 1D to Check for Flange Leaks,Low Suction Pressure Annunciator Would Not Clear,Making B Loop Inoperable.Caused by Failure to re-energize Circuit 19 | | | 05000325/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000325/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000325/LER-1980-009-03, /03L-0:on 800120,during Normal Operation,Control Operator Noticed Containment Atmospheric Monitor Had Step Change for No Apparent Reason.No Cause Determined.Components of Monitor Replaced & Recalibr | /03L-0:on 800120,during Normal Operation,Control Operator Noticed Containment Atmospheric Monitor Had Step Change for No Apparent Reason.No Cause Determined.Components of Monitor Replaced & Recalibr | | | 05000324/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000324/LER-1980-009-03, /03L-0:on 800114,during Normal Operation, Containment Atmospheric Monitor CAC-AT-1259-1 Failed Upscale.Caused by Loose Ground Connection on Span Potentiometer.Connection Tightened | /03L-0:on 800114,during Normal Operation, Containment Atmospheric Monitor CAC-AT-1259-1 Failed Upscale.Caused by Loose Ground Connection on Span Potentiometer.Connection Tightened | | | 05000325/LER-1980-010-03, /03L-0:on 800122,while Performing Main Steam Line High Radiation Functional Check,Drawer 1D12-RM-K603B Found Out of Calibr.Instrument Drift Is Recurring Problem. Drawer Recalibr & Returned to Svc | /03L-0:on 800122,while Performing Main Steam Line High Radiation Functional Check,Drawer 1D12-RM-K603B Found Out of Calibr.Instrument Drift Is Recurring Problem. Drawer Recalibr & Returned to Svc | | | 05000325/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000324/LER-1980-010-03, /03L-0:on 800114,during Normal Plant Operation, Nuclear Engineer Performed OD-1 & Found Max Critical Power Ratio to Exceed Limit.Caused by Low Power Range Monitor Having Two Levels Bypassed & Problems W/Core Flow Input | /03L-0:on 800114,during Normal Plant Operation, Nuclear Engineer Performed OD-1 & Found Max Critical Power Ratio to Exceed Limit.Caused by Low Power Range Monitor Having Two Levels Bypassed & Problems W/Core Flow Input | | | 05000324/LER-1980-010, Supplemental LER 80-010/03L-1:on 800114,during Normal Plant operation,OD-1 Determined That Max Critical Power Ratio Was Below Tech Specs for Bundle 43-28.Caused by Problems W/Low Power Range Monitor & Core Flow Input.Power Redu | Supplemental LER 80-010/03L-1:on 800114,during Normal Plant operation,OD-1 Determined That Max Critical Power Ratio Was Below Tech Specs for Bundle 43-28.Caused by Problems W/Low Power Range Monitor & Core Flow Input.Power Reduced | | | 05000325/LER-1980-011-03, /03L-0:on 800121,during 10-minute Run of HPCI Auxiliary Oil Pump,Stoppage Occurred When Switch Moved from Start to Auto Position.Caused by Loose Wire on RTGB Control Switch.Wire Reattached & Tightened | /03L-0:on 800121,during 10-minute Run of HPCI Auxiliary Oil Pump,Stoppage Occurred When Switch Moved from Start to Auto Position.Caused by Loose Wire on RTGB Control Switch.Wire Reattached & Tightened | | | 05000325/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000324/LER-1980-011-03, /03L-0:on 800110,when Time Was Entered on Computer After Reinitialization,Computer Had Software Stall & Could Not Be Kept on Line,Causing Temp Recorder CAC-7R-1258 to Be Inoperable.New Points Added to Sys | /03L-0:on 800110,when Time Was Entered on Computer After Reinitialization,Computer Had Software Stall & Could Not Be Kept on Line,Causing Temp Recorder CAC-7R-1258 to Be Inoperable.New Points Added to Sys | | | 05000324/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000325/LER-1980-012-03, /03L-0:on 800224,during Normal Plant Operation,Rip Valves,Variable Leg Isolation for Torus Level Transmitter & Variable Leg for Torus Level Pressure Switch Shut & Could Not Be Opened.Caused by Failure of Svc Air Compressors | /03L-0:on 800224,during Normal Plant Operation,Rip Valves,Variable Leg Isolation for Torus Level Transmitter & Variable Leg for Torus Level Pressure Switch Shut & Could Not Be Opened.Caused by Failure of Svc Air Compressors | | | 05000325/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000324/LER-1980-012-03, /03L-0:on 800116,while Performing Torus Water Level Calibr & Functional Check,Level Switch E41-LSH-NOI5A Would Not Actuate.Caused by Switch Out of Calibr.Instrument Recalibr | /03L-0:on 800116,while Performing Torus Water Level Calibr & Functional Check,Level Switch E41-LSH-NOI5A Would Not Actuate.Caused by Switch Out of Calibr.Instrument Recalibr | | | 05000324/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000324/LER-1980-013-03, /03L-0:on 800116,during Normal Operation, Containment Atmospheric Monitor CAC-AQH-1260 Monitor Breaker Had Tripped on Magnetics Rendering CAC-AQH-1262-2 Inoperable.Caused by Short in Power Lead.Lead Taped | /03L-0:on 800116,during Normal Operation, Containment Atmospheric Monitor CAC-AQH-1260 Monitor Breaker Had Tripped on Magnetics Rendering CAC-AQH-1262-2 Inoperable.Caused by Short in Power Lead.Lead Taped | | | 05000325/LER-1980-013-03, /03L-0:on 800125,while Performing Reactor Low Water Level 2 & 3 Channel Calibr & Functional Check,Low Pressure Switch 1B21-LITS-N031A-2 Failed to Actuate.Caused by Instrument Drift.Instruments to Be Replaced | /03L-0:on 800125,while Performing Reactor Low Water Level 2 & 3 Channel Calibr & Functional Check,Low Pressure Switch 1B21-LITS-N031A-2 Failed to Actuate.Caused by Instrument Drift.Instruments to Be Replaced | |
|