05000327/LER-1980-118-03, /03L-0:on 800711,upper & Lower Containment Air Radiation monitors,1-RM-90-112 & -106,declared Inoperable. Caused by Upstream Sample Air Valves Closing on Loss of Control Air.Cause of Loss of Control Air Unknown

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/03L-0:on 800711,upper & Lower Containment Air Radiation monitors,1-RM-90-112 & -106,declared Inoperable. Caused by Upstream Sample Air Valves Closing on Loss of Control Air.Cause of Loss of Control Air Unknown
ML19331C849
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 08/13/1980
From: Hereford J
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19331C839 List:
References
LER-80-118-03L, LER-80-118-3L, NUDOCS 8008190622
Download: ML19331C849 (1)


LER-1980-118, /03L-0:on 800711,upper & Lower Containment Air Radiation monitors,1-RM-90-112 & -106,declared Inoperable. Caused by Upstream Sample Air Valves Closing on Loss of Control Air.Cause of Loss of Control Air Unknown
Event date:
Report date:
3271980118R03 - NRC Website

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