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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20029A5461991-02-12012 February 1991 Special Rept 91-01:on 910113,inoperable Condenser Bay Sprinkler Sys 2 Not Restored within 14 Days.Caused by Steam Leak in Vicinity of Sprinkler Head.Sprinkler Will Be Replaced During Refueling Outage 13R ML20043A7901990-05-11011 May 1990 Special Rept 90-03:on 900412,Fire Diesel Pump 1-1 Not Restored to Functional Status within 7 Days.Pump Removed from Svc to Install Mod.Mod Completed,Tested & Returned to Functional Status on 900420 ML20012F5171990-04-0303 April 1990 Special Rept 90-02:on 900309,stack Radioactive Effluent Monitoring Sys High Range Monitor Not Repaired within 7 Days,Per Tech Spec 3.13.H.Caused by Acceptance Criteria Test Procedure.Test Procedure Revised ML20042D8401990-03-30030 March 1990 Supplement to 900105 Special Rept Re Inoperability of Diesel Fire Pump Due to Failure in Right Angle Gear Drive. Broken Studs Replaced W/Cap Screws Per Vendor Recommendations & Preventive Maint Activity Added ML20012C6861990-03-15015 March 1990 Ro:On 900204,daily Functional Test Not Done for Portable Fire Detection Sys.Caused by Shift Supervisor Failure to Ensure That Test Was Done.Requirements of Daily Functional Test Will Be Added to Operations Dept Monthly Activity Log ML20005F4401990-01-0505 January 1990 Special Rept:On 891129,diesel Fire Pump Failed While Providing Water to Support Cleaning Activity Unrelated to Fire Protection Sys.Caused by Broken Studs.Broken Studs Replaced W/Cap Screws Per Vendor Current Recommendation ML19351A3001989-10-11011 October 1989 Special Rept 89-03:on 890904,during Weekly Surveillance of Fire Barrier Doors,Door Between Fire Zones RB-FZ-1E & RB-FZ-1F4 Did Not Meet Acceptance Criteria.Door Unable to Latch W/O Assistance.Fire Watch Established & Door Repaired ML20028D6511983-01-0707 January 1983 RO 82-9:on 821208,temp Sensor Instrumentation Located Upstream of Us Route 9 Bridge Did Not Meet Overall Sys Accuracy Limits.Caused by Downdrift of Temp Transmitter Zero & Span Adjustments.Temp Transmitter Recalibr ML20028D6631983-01-0707 January 1983 RO 82-10:on 821210,during shutdown,364 Dead or Severely Stressed Fish Collected.Caused by Temp in Discharge Canal Below Lethal Temp for Affected Species ML20050D9991982-04-0202 April 1982 RO 50-219/82-20/01P:on 820401,abnormal Degradation of Primary Containment Identified,Based on MSIV Leak Rates Outside of Acceptable Limits.Cause Under Investigation.Msivs Adjusted & Repaired ML20050D5471982-04-0101 April 1982 RO 50-219/82-19/01P:on 820331,results of Leak Rate Testing on Main Steam Isolation Drain Valves Identified Abnormal Degradation of Primary Containment.Cause Unknown.Valve V-1-106 Repaired & Valve V-1-111 Will Be Replaced ML20050A9651982-03-22022 March 1982 RO NP-09-82-02:on 820222,free Chlorine Discharged in Excess of Ets,Section 2.3.1 Limit of 2-h Per Day.Caused by Equipment Deficiency.Feed Rate Will Be Verified During Chlorination Sys Lineup Changes ML20049H4711982-02-19019 February 1982 RO 82-10/01P:on 820218,determined Apparent Deficiency in Safety Evaluation 218.77-81 Re safety-related Sys.Electrical Fire on 820109 Caused Deluge Sys to Actuate.Ac & Dc Ground Faults Occurred Due to Water Damage ML20041A9821982-02-11011 February 1982 RO 82-06/01P:on 811203,control Power Fuses 16F301A,16F302A, 16F303A & 16F304A Removed from Svc for Maint on Electromatic Relief Valve Pressure Switch,Rendering Valve a & Automatic Depressurization Sys Inoperable.Switch Replaced ML20040G1191982-02-0303 February 1982 RO NP-09-82-01:on 820104,max Discharge Temp Above Ambient Lake Temp Limit Was Exceeded During Unusual Weather Change. Alarm T189 Setpoint Changed from 15 F to 17 F ML20040F4981982-02-0101 February 1982 RO 82-01:on 820117,fire Suppression Water Sys Declared Inoperable.Caused by Inoperability of Fire Diesels Due to Extremely Low Temps.Space Heaters Repaired & Returned to Svc.Fuel Oil Temp Problem Under Investigation ML20040C6731982-01-18018 January 1982 RO 219/82-01:on 820117,fire Diesels 1-1 & 1-2 Shut Down for Maint,Rendering Fire Suppression Water Sys Inoperable.Caused by Frozen Cooling Water Lines & Fuel Oil Due to Failure of Two Space Heaters.Heaters Replaced ML20040C6071981-12-22022 December 1981 Nonroutine Environ Operating Rept 50-219/81-3-2:on 811128, Less than Two Dilution Pumps Were Operating for Greater than 15 Minutes & Ambient Water Temp Was Less than 60 F.Caused by Loose Pump Impeller on Pump 1-1 ML20040C6151981-12-22022 December 1981 Nonroutine Environ Operating Rept 50-219/81-4-2:on 811124, Dilution Pump 1-2 Tripped Leaving Only Dilution Pump 1-3 Operating for More than 15 Minutes & Ambient Water Temp Less than 60 F.Cause of Trip Not Determined ML20040C6201981-12-22022 December 1981 Nonroutine Environ Operating Rept 50-219/81-5-2:on 811202, Dilution Pump 1-2 Tripped Leaving Only Dilution Pump 1-3 Operating for More than 15 Minutes & Ambient Water Temp Less than 60 F.Caused by High Oil Temps Due to Clogged Screen ML20040C6261981-12-22022 December 1981 Nonroutine Environ Operating Rept 50-219/81-6-2:on 811121, Dilution Pump 1-2 Tripped Leaving Only Dilution Pump 1-1 Operating for More than 15 Minutes & Ambient Water Temp Less than 60 F.Cause of Trip Not Determined ML20040C6311981-12-22022 December 1981 Nonroutine Environ Operating Rept 50-219/81-7-1:on 811207, Intake Temp Was 37.3 F & Discharge Temp 61.9 F Resulting in Temp Difference of 24.6 F Exceeding Permit Level of 23 F. Caused by Grass Clogging Intake & Reducing Flow ML20039B2831981-12-10010 December 1981 RO 50-219/81-65-01P:on 811203 & 09,two Isolation Valves for Isolation Condenser Sys Found to Have Defects & Valve V-14-30 Found Inoperable.Damaged Threads in Lower Part of Stem Nut Repaired.Cause Under Investigation ML20038C7161981-12-0909 December 1981 RO 50-219/81-64/01P:on 811203,containment Spray High Drywell Pressure Switches IP-154A,IP-15B,IP-15C & IP-15D Tripped at Value Greater than Tech Specs.Caused by Instrument Repeatability.Switches Reset ML20010G3071981-08-31031 August 1981 Ro:Ie Bulletin 80-11 Analysis Determined That Listed Walls Would Be Overstressed During Seismic Event ML20010E7131981-08-28028 August 1981 RO 50-219/81-42/01P:on 810828,stack Gas Not Continuously Monitored as Required by Tech Spec Due to Trip of Stack Gas Sample Pump B.Probably Caused by Failure of Bearings &/Or Micarta Vanes in Pump ML20009E3471981-07-15015 July 1981 RO 81-030/01P-0:on 810714,during Required Surveillance at steady-state Power Standby Gas Treatment Sys 1 Failed to Start & Reactor Bldg Main Exhaust Valve V-28-22 Failed to Close.Caused by Faulty Tube Flow Sensor ML20005B3831981-06-25025 June 1981 RO NP-09-81-01:on 810526,max Discharge Temp Differential, Above Ambient Lake Temp,Was Slightly Exceeded.Caused by Difficulty in Maintaining Balance Between Operating to Prevent Exceeding Limit & to Prevent Cooling Tower Damage ML20004C8401981-06-0101 June 1981 Ro:On 800728 & 1219,data from 10-meter Wind Direction Monitoring Sys Was Lost.Caused by V76 Central Computer Disk Failure & Simultaneous Electronic Failure of Esterline Angus L1152S Recorder.Equipment Repaired ML19345H2541981-04-27027 April 1981 RO 81-001:on 810415 & 16,two Dilution Pumps Tripped & Reserve Pump Would Not Start.Caused by Component Failure. Flow Switch Jumpered After First Event,Lube Oil Cooler Switch Reset After Second ML19350C2261981-03-17017 March 1981 Corrected Page 3 to Supplemental Info for LER 80-090 ML19341C2391981-02-18018 February 1981 Forwards Revised Supplemental Info Sheets for LER 79-050 Re Unplanned Reactivity Insertion.Caused by Mechanical, Personnel & Procedural Error.Valve Mu 39 Disassembled & Gaskets Installed ML19343B4331980-12-17017 December 1980 RO 50-219/80-13:on 801204,plant Intake Water Level Reached Critically Low Elevation,Affecting Supply of Cooling Water to Main Condenser,Reactor & Turbine Bldgs.Caused by Environ & Svc Conditions.Dilution Pumps 1-2 & 1-3 Restarted ML19347C7461980-12-17017 December 1980 RO:801121 Fire Diesel 1-2 Removed from Svc to Determine Cause of Failure to Start Automatically on Decrease in Sys Pressure.Caused by Failure of Corrosion Resistor Element in Cooling Water Line Resulting in Diesel Overheat ML19345C8111980-12-0202 December 1980 Nonroutine Environ Operating Rept 50-219/80-12:on 801122 During Reactor Shutdown W/Three Circulating Pumps in Svc, Water Temp in Discharge Canal Fell Below Lower Lethal Temp, Resulting in Fishkill.Blocking Devices Considered ML19340C8281980-12-0101 December 1980 Supplemental Info Re RO NP-32-80-12:on 800724,w/unit in Mode 5,loss of Decay Heat Flow Observed.No Indication for Valve Position of Decay Heat Isolation Valve DH12.Revision Replaces Supplemental Info for RO 80-058 ML19350A0641980-11-25025 November 1980 Nonroutine Environ Operating Rept 80-219/80-11:on 801118, Fish Were Found Dead in Creek.Caused by Apparent Distraction from Fall Migration Due to Warm Water from Facility. Installation of Blocking Devices Under Review ML19345C3411980-11-21021 November 1980 Nonroutine Environ Operating Rept 50-219/80-10:on 801111,ETS Limiting Condition Exceeded When Less than Two Dilution Pumps Worked for 25 Minutes W/Ambient Intake Water Temp at Less than 60 F.Caused by Unusual Svc Condition ML19345B4361980-11-21021 November 1980 Nonroutine Environ Operating Rept 50-219/80-10:on 801111, Dilution Pump 1-2 Tripped.Caused by Debris in Barnegat Bay Clogging Pump Seal Water Strainers,Reducing Pressure.Lines cleared.Long-term Corrective Action Being Reviewed ML19345A8461980-11-18018 November 1980 Ro:On 801117 All Four Containment Pressure Transmitters Found to Be Inoperable Due to Surveillance Test Procedure Error.Emergency Tech Spec Relief Requested ML19340C1791980-11-0606 November 1980 RO 50-219/80-49/1P:on 801105,while Removing Isolation Condenser B from Svc to Repair Leak on Isolation Valve V-14-19,valves V-14-1 & V-14-19 Failed to Close.Cause Undetermined ML19339C0881980-11-0303 November 1980 Nonroutine Environ Operating Rept 50-219/80-9:on 801026, Intake Trash Racks,Ristroph Traveling Screens,Turbine Bldg Closed Cooling Water Heat Exchangers & Main Condensers Were Fouled W/Seaweed & Blue Crabs.Caused by 801025 Storm ML19340B5461980-11-0303 November 1980 RO 50-219/80-9:on 801026,intake Trash Racks,Ristroph Traveling Screens,Turbine Bldg Closed Cooling Water Heat Exchangers & Main Condensers Were Fouled W/Seaweed & Approx 10,000 Blue Crabs Due to Intense 801025 Northeast Storm ML19338E6451980-09-25025 September 1980 Nonroutine Environ Operating Rept 50-219/80-8: on 800910, Second Dilution Pump Was Not Placed Into Operation W/Water Temp Exceeding 87 F for Period More Tht 2-h 15 Minutes. Caused by Damaged Inboard Motor Bearing ML19347A7461980-09-25025 September 1980 Nonroutine Environ Operating Rept 50-219/80-08:on 800910, Second Dilution Pump Placed Into Operation W/Bridge Water Temp Below ETS Requirements.Caused by Insufficient Pump Quota.Damaged Pump Removed & Repaired ML19337A8341980-09-19019 September 1980 Nonroutine Environ Operating Rept 80-7:on 800901,02 & 04, Four Individual Dilution Pump Trips Occurred During Which Inoperative or Reserve Pump Could Not Be Started within Required 15 Minutes.Caused by Component Failure ML19337B4281980-09-0909 September 1980 RO NP-09-80-01:on 800116 & 0210,discharge Temp for Liquid Effluents Exceeded 20 F Above Lake Temp Due to Procedural Deficiencies.Cooling Tower Was Operated in Bypass Mode Causing Temp to Elevate Above Normal Temp During Startup ML19331E0541980-08-26026 August 1980 Nonroutine Environ Operating Rept 50-219/80-5.Total of Ten Dilution Pump Trips Occurred Between 800808 & 800812.Caused by High Lubricating Oil Temp.Evaluation Completed for Upgrading Cooling Water Sys ML19344E6331980-08-26026 August 1980 RO 50-219/80-5:on 800808,09,11 & 12,during Steady State power,10 Dilution Pump Trips Occurred,Exceeding Limiting Condition Per Tech Spec.Caused by High Lubricating Oil Temp Due to Low Cooling Water Pressure ML19344E6451980-08-26026 August 1980 Nonroutine Environ Operating Rept 50-219/80-6:on 800811,at Steady State Power,Condenser Discharge Temp Exceeded 106 F. Caused by Shift in Meteorological Conditions.Load Reduction Initiated & Temp Stablilized 1991-02-12
[Table view] Category:LER)
MONTHYEARML20029A5461991-02-12012 February 1991 Special Rept 91-01:on 910113,inoperable Condenser Bay Sprinkler Sys 2 Not Restored within 14 Days.Caused by Steam Leak in Vicinity of Sprinkler Head.Sprinkler Will Be Replaced During Refueling Outage 13R ML20043A7901990-05-11011 May 1990 Special Rept 90-03:on 900412,Fire Diesel Pump 1-1 Not Restored to Functional Status within 7 Days.Pump Removed from Svc to Install Mod.Mod Completed,Tested & Returned to Functional Status on 900420 ML20012F5171990-04-0303 April 1990 Special Rept 90-02:on 900309,stack Radioactive Effluent Monitoring Sys High Range Monitor Not Repaired within 7 Days,Per Tech Spec 3.13.H.Caused by Acceptance Criteria Test Procedure.Test Procedure Revised ML20042D8401990-03-30030 March 1990 Supplement to 900105 Special Rept Re Inoperability of Diesel Fire Pump Due to Failure in Right Angle Gear Drive. Broken Studs Replaced W/Cap Screws Per Vendor Recommendations & Preventive Maint Activity Added ML20012C6861990-03-15015 March 1990 Ro:On 900204,daily Functional Test Not Done for Portable Fire Detection Sys.Caused by Shift Supervisor Failure to Ensure That Test Was Done.Requirements of Daily Functional Test Will Be Added to Operations Dept Monthly Activity Log ML20005F4401990-01-0505 January 1990 Special Rept:On 891129,diesel Fire Pump Failed While Providing Water to Support Cleaning Activity Unrelated to Fire Protection Sys.Caused by Broken Studs.Broken Studs Replaced W/Cap Screws Per Vendor Current Recommendation ML19351A3001989-10-11011 October 1989 Special Rept 89-03:on 890904,during Weekly Surveillance of Fire Barrier Doors,Door Between Fire Zones RB-FZ-1E & RB-FZ-1F4 Did Not Meet Acceptance Criteria.Door Unable to Latch W/O Assistance.Fire Watch Established & Door Repaired ML20028D6511983-01-0707 January 1983 RO 82-9:on 821208,temp Sensor Instrumentation Located Upstream of Us Route 9 Bridge Did Not Meet Overall Sys Accuracy Limits.Caused by Downdrift of Temp Transmitter Zero & Span Adjustments.Temp Transmitter Recalibr ML20028D6631983-01-0707 January 1983 RO 82-10:on 821210,during shutdown,364 Dead or Severely Stressed Fish Collected.Caused by Temp in Discharge Canal Below Lethal Temp for Affected Species ML20050D9991982-04-0202 April 1982 RO 50-219/82-20/01P:on 820401,abnormal Degradation of Primary Containment Identified,Based on MSIV Leak Rates Outside of Acceptable Limits.Cause Under Investigation.Msivs Adjusted & Repaired ML20050D5471982-04-0101 April 1982 RO 50-219/82-19/01P:on 820331,results of Leak Rate Testing on Main Steam Isolation Drain Valves Identified Abnormal Degradation of Primary Containment.Cause Unknown.Valve V-1-106 Repaired & Valve V-1-111 Will Be Replaced ML20050A9651982-03-22022 March 1982 RO NP-09-82-02:on 820222,free Chlorine Discharged in Excess of Ets,Section 2.3.1 Limit of 2-h Per Day.Caused by Equipment Deficiency.Feed Rate Will Be Verified During Chlorination Sys Lineup Changes ML20049H4711982-02-19019 February 1982 RO 82-10/01P:on 820218,determined Apparent Deficiency in Safety Evaluation 218.77-81 Re safety-related Sys.Electrical Fire on 820109 Caused Deluge Sys to Actuate.Ac & Dc Ground Faults Occurred Due to Water Damage ML20041A9821982-02-11011 February 1982 RO 82-06/01P:on 811203,control Power Fuses 16F301A,16F302A, 16F303A & 16F304A Removed from Svc for Maint on Electromatic Relief Valve Pressure Switch,Rendering Valve a & Automatic Depressurization Sys Inoperable.Switch Replaced ML20040G1191982-02-0303 February 1982 RO NP-09-82-01:on 820104,max Discharge Temp Above Ambient Lake Temp Limit Was Exceeded During Unusual Weather Change. Alarm T189 Setpoint Changed from 15 F to 17 F ML20040F4981982-02-0101 February 1982 RO 82-01:on 820117,fire Suppression Water Sys Declared Inoperable.Caused by Inoperability of Fire Diesels Due to Extremely Low Temps.Space Heaters Repaired & Returned to Svc.Fuel Oil Temp Problem Under Investigation ML20040C6731982-01-18018 January 1982 RO 219/82-01:on 820117,fire Diesels 1-1 & 1-2 Shut Down for Maint,Rendering Fire Suppression Water Sys Inoperable.Caused by Frozen Cooling Water Lines & Fuel Oil Due to Failure of Two Space Heaters.Heaters Replaced ML20040C6071981-12-22022 December 1981 Nonroutine Environ Operating Rept 50-219/81-3-2:on 811128, Less than Two Dilution Pumps Were Operating for Greater than 15 Minutes & Ambient Water Temp Was Less than 60 F.Caused by Loose Pump Impeller on Pump 1-1 ML20040C6151981-12-22022 December 1981 Nonroutine Environ Operating Rept 50-219/81-4-2:on 811124, Dilution Pump 1-2 Tripped Leaving Only Dilution Pump 1-3 Operating for More than 15 Minutes & Ambient Water Temp Less than 60 F.Cause of Trip Not Determined ML20040C6201981-12-22022 December 1981 Nonroutine Environ Operating Rept 50-219/81-5-2:on 811202, Dilution Pump 1-2 Tripped Leaving Only Dilution Pump 1-3 Operating for More than 15 Minutes & Ambient Water Temp Less than 60 F.Caused by High Oil Temps Due to Clogged Screen ML20040C6261981-12-22022 December 1981 Nonroutine Environ Operating Rept 50-219/81-6-2:on 811121, Dilution Pump 1-2 Tripped Leaving Only Dilution Pump 1-1 Operating for More than 15 Minutes & Ambient Water Temp Less than 60 F.Cause of Trip Not Determined ML20040C6311981-12-22022 December 1981 Nonroutine Environ Operating Rept 50-219/81-7-1:on 811207, Intake Temp Was 37.3 F & Discharge Temp 61.9 F Resulting in Temp Difference of 24.6 F Exceeding Permit Level of 23 F. Caused by Grass Clogging Intake & Reducing Flow ML20039B2831981-12-10010 December 1981 RO 50-219/81-65-01P:on 811203 & 09,two Isolation Valves for Isolation Condenser Sys Found to Have Defects & Valve V-14-30 Found Inoperable.Damaged Threads in Lower Part of Stem Nut Repaired.Cause Under Investigation ML20038C7161981-12-0909 December 1981 RO 50-219/81-64/01P:on 811203,containment Spray High Drywell Pressure Switches IP-154A,IP-15B,IP-15C & IP-15D Tripped at Value Greater than Tech Specs.Caused by Instrument Repeatability.Switches Reset ML20010G3071981-08-31031 August 1981 Ro:Ie Bulletin 80-11 Analysis Determined That Listed Walls Would Be Overstressed During Seismic Event ML20010E7131981-08-28028 August 1981 RO 50-219/81-42/01P:on 810828,stack Gas Not Continuously Monitored as Required by Tech Spec Due to Trip of Stack Gas Sample Pump B.Probably Caused by Failure of Bearings &/Or Micarta Vanes in Pump ML20009E3471981-07-15015 July 1981 RO 81-030/01P-0:on 810714,during Required Surveillance at steady-state Power Standby Gas Treatment Sys 1 Failed to Start & Reactor Bldg Main Exhaust Valve V-28-22 Failed to Close.Caused by Faulty Tube Flow Sensor ML20005B3831981-06-25025 June 1981 RO NP-09-81-01:on 810526,max Discharge Temp Differential, Above Ambient Lake Temp,Was Slightly Exceeded.Caused by Difficulty in Maintaining Balance Between Operating to Prevent Exceeding Limit & to Prevent Cooling Tower Damage ML20004C8401981-06-0101 June 1981 Ro:On 800728 & 1219,data from 10-meter Wind Direction Monitoring Sys Was Lost.Caused by V76 Central Computer Disk Failure & Simultaneous Electronic Failure of Esterline Angus L1152S Recorder.Equipment Repaired ML19345H2541981-04-27027 April 1981 RO 81-001:on 810415 & 16,two Dilution Pumps Tripped & Reserve Pump Would Not Start.Caused by Component Failure. Flow Switch Jumpered After First Event,Lube Oil Cooler Switch Reset After Second ML19350C2261981-03-17017 March 1981 Corrected Page 3 to Supplemental Info for LER 80-090 ML19341C2391981-02-18018 February 1981 Forwards Revised Supplemental Info Sheets for LER 79-050 Re Unplanned Reactivity Insertion.Caused by Mechanical, Personnel & Procedural Error.Valve Mu 39 Disassembled & Gaskets Installed ML19343B4331980-12-17017 December 1980 RO 50-219/80-13:on 801204,plant Intake Water Level Reached Critically Low Elevation,Affecting Supply of Cooling Water to Main Condenser,Reactor & Turbine Bldgs.Caused by Environ & Svc Conditions.Dilution Pumps 1-2 & 1-3 Restarted ML19347C7461980-12-17017 December 1980 RO:801121 Fire Diesel 1-2 Removed from Svc to Determine Cause of Failure to Start Automatically on Decrease in Sys Pressure.Caused by Failure of Corrosion Resistor Element in Cooling Water Line Resulting in Diesel Overheat ML19345C8111980-12-0202 December 1980 Nonroutine Environ Operating Rept 50-219/80-12:on 801122 During Reactor Shutdown W/Three Circulating Pumps in Svc, Water Temp in Discharge Canal Fell Below Lower Lethal Temp, Resulting in Fishkill.Blocking Devices Considered ML19340C8281980-12-0101 December 1980 Supplemental Info Re RO NP-32-80-12:on 800724,w/unit in Mode 5,loss of Decay Heat Flow Observed.No Indication for Valve Position of Decay Heat Isolation Valve DH12.Revision Replaces Supplemental Info for RO 80-058 ML19350A0641980-11-25025 November 1980 Nonroutine Environ Operating Rept 80-219/80-11:on 801118, Fish Were Found Dead in Creek.Caused by Apparent Distraction from Fall Migration Due to Warm Water from Facility. Installation of Blocking Devices Under Review ML19345C3411980-11-21021 November 1980 Nonroutine Environ Operating Rept 50-219/80-10:on 801111,ETS Limiting Condition Exceeded When Less than Two Dilution Pumps Worked for 25 Minutes W/Ambient Intake Water Temp at Less than 60 F.Caused by Unusual Svc Condition ML19345B4361980-11-21021 November 1980 Nonroutine Environ Operating Rept 50-219/80-10:on 801111, Dilution Pump 1-2 Tripped.Caused by Debris in Barnegat Bay Clogging Pump Seal Water Strainers,Reducing Pressure.Lines cleared.Long-term Corrective Action Being Reviewed ML19345A8461980-11-18018 November 1980 Ro:On 801117 All Four Containment Pressure Transmitters Found to Be Inoperable Due to Surveillance Test Procedure Error.Emergency Tech Spec Relief Requested ML19340C1791980-11-0606 November 1980 RO 50-219/80-49/1P:on 801105,while Removing Isolation Condenser B from Svc to Repair Leak on Isolation Valve V-14-19,valves V-14-1 & V-14-19 Failed to Close.Cause Undetermined ML19339C0881980-11-0303 November 1980 Nonroutine Environ Operating Rept 50-219/80-9:on 801026, Intake Trash Racks,Ristroph Traveling Screens,Turbine Bldg Closed Cooling Water Heat Exchangers & Main Condensers Were Fouled W/Seaweed & Blue Crabs.Caused by 801025 Storm ML19340B5461980-11-0303 November 1980 RO 50-219/80-9:on 801026,intake Trash Racks,Ristroph Traveling Screens,Turbine Bldg Closed Cooling Water Heat Exchangers & Main Condensers Were Fouled W/Seaweed & Approx 10,000 Blue Crabs Due to Intense 801025 Northeast Storm ML19338E6451980-09-25025 September 1980 Nonroutine Environ Operating Rept 50-219/80-8: on 800910, Second Dilution Pump Was Not Placed Into Operation W/Water Temp Exceeding 87 F for Period More Tht 2-h 15 Minutes. Caused by Damaged Inboard Motor Bearing ML19347A7461980-09-25025 September 1980 Nonroutine Environ Operating Rept 50-219/80-08:on 800910, Second Dilution Pump Placed Into Operation W/Bridge Water Temp Below ETS Requirements.Caused by Insufficient Pump Quota.Damaged Pump Removed & Repaired ML19337A8341980-09-19019 September 1980 Nonroutine Environ Operating Rept 80-7:on 800901,02 & 04, Four Individual Dilution Pump Trips Occurred During Which Inoperative or Reserve Pump Could Not Be Started within Required 15 Minutes.Caused by Component Failure ML19337B4281980-09-0909 September 1980 RO NP-09-80-01:on 800116 & 0210,discharge Temp for Liquid Effluents Exceeded 20 F Above Lake Temp Due to Procedural Deficiencies.Cooling Tower Was Operated in Bypass Mode Causing Temp to Elevate Above Normal Temp During Startup ML19331E0541980-08-26026 August 1980 Nonroutine Environ Operating Rept 50-219/80-5.Total of Ten Dilution Pump Trips Occurred Between 800808 & 800812.Caused by High Lubricating Oil Temp.Evaluation Completed for Upgrading Cooling Water Sys ML19344E6331980-08-26026 August 1980 RO 50-219/80-5:on 800808,09,11 & 12,during Steady State power,10 Dilution Pump Trips Occurred,Exceeding Limiting Condition Per Tech Spec.Caused by High Lubricating Oil Temp Due to Low Cooling Water Pressure ML19344E6451980-08-26026 August 1980 Nonroutine Environ Operating Rept 50-219/80-6:on 800811,at Steady State Power,Condenser Discharge Temp Exceeded 106 F. Caused by Shift in Meteorological Conditions.Load Reduction Initiated & Temp Stablilized 1991-02-12
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & Pnpp QA Program ML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 1999-09-30
[Table view] |
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d N ^w Jersey Central Power (r& Light Cornpany W.
i MAOISON AVENWE AT PUNcN BOWL. MO Ao e MoR AISTOWN, N.J. 0794o e 333.stit
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October 6, 1972 ~
J -
epBLl]f ur.v4 q Mr. A. Giambusso g b W- N,.
Deputy Director for Reactor Projects .
[,',7/.0 Directorata of Licensing ,
Cij United States Atomic Energy Comission
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si Washington, D. C. 20545 ,
Daar Mr. Cia =busso:
L 3,3 ' '. ' -*'
O!%nI
Subject:
Oyster Creek Station Docket No. 50-219
. Inoperabia Standby Liquid Control Syste=
, h a purpose of this letter is to report to yo'u an incident that occurred at Oyster Creek on Septe=ber 26, 1972 in which it was discovered that the two pu=ps in the standby liquid control syste=
were inoperabia at the sa=a ti=a'. .
At 10:45 a.=.'on Septe=ber 25, 1972, the "A" standby liquid control pu=p was re=oved fro service for replace =ent of the pu=p packing. De pu=p was taken out of service using Technical Specification 3.2.C.3 as the basis. It states, "If one standby liquid control syste= pumping circuit becomes in-operable during the run code and specification 3.2.A is =et, \
D3 "i
. the reactor =ay rs=ain in operation for a period not to exece '// 4
.savan days, provided the pu=p in the other circuit is de=en D #
strated daily to be operable". Specification 3.2.A is =et,p (,
"A" pump breaker was racked out and the pu=p ' g8 7 therefore, the secured in accordance with plant safety procedures, new r- O/ li~ ,j fp,.g*gi was not. co=placed by the end of the day shif t, and the "A" 6 f pump was left in an inoperable condition. At 4:20 a.=. on cgpi k/
Septe=ber 26,1972', the "3" liquid control syste= pu=p was to be run to comply with Technical Specification 3.2.C.3.
g A4/ /
t y gg When the operator depressed the start button, the pump did
~
not start.
An interlock in the starting circuitry prevents two l standby liquid control pu=ps fro = being run si=ultaneously.
his interlock also prevents the "3" pu=p frc= starting when the "A" pu=p breaker is in the racked out position. ne interlock is cc= posed of a nor ally closed contact in the Oi starting circuit of each pump. This contact is operated fro = a relay in the opposite pu=p circuit. If the "A" standby liquid control pu=p is started either fro = the control roo= with tha key lock switch or locally from the .
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8001 #
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n The Toledo Edison Company The results of your review are requested within sixty days. This information should be provided with one signed original and thirty-nine additional copies. ,
Sincerely,
. aW
- A. Schwencer, Chief Pressurized Water Reactors Branch No. 4 Directorate of Licensing
Enclosures:
Licensee's reports on occurrences cc: Leslie Henry, Esquire j
]
O Fuller, Seney, Henry & Hodge 800 Owens-Illinois Building 405 Madison Avenue Toledo, Ohio 43604 Gerald Charnoff, Esquire
- Shaw, Pittman, Potts, Trowbridge
,- and Madden 910 - 17th Street, N.W.
Washington, D.C. 20006 Donald H. Hauser, Esquire The Cleveland Electric Illuminating Company P.O. Box 5000, Room 610
! Cleveland, Ohio 44101 l
O
~ . . . %. ) e 4 - e
( ,
s /- .
\ :
Dr. Peter A. Morris ;
Page II - *
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April 20, 1972 -
The logic circuit was restored by disconnecting the motor leads from the breaker and racking-in the breaker. At 9:20 a.m.
' on April 11, 1972, an operability check of Reactor Building Isolation was conducted and proved to be satisfactory. A caution tag was placed at the fan control switches in the Control Roo= to notify operators that if a supply fan breaker is racked-ou; the Reactor Building supply da=per isolation control logic is defeated unless a ju=per is installed in the breaker cabinet. A s1=11ar caution note is being stenciled locally on the supply fan breakars.
As noted in the FDSAR, the primary objective of the Secondary Contain=ent System is to minimize ground level release of airborne radioactive =aterials and to provide for controlled elevated release of the building at=osphere under accident conditions. The contain=ent
- syste=s, ?r1=ary and Secondary, provide the principle =echaniss for mitigation of accident consequences. The off-site accident consequences, howeyer, are relatively insensitive to the Reactor Building in-leakage
_s rate as long as the Standby Cas Trest = cat System can =aintain the building at a vacuum. In this particular instance, the supply and s,,, N) exhaust fans tripped, the exhaust dampers closed, and the Standby Cas Treatment System was initiated. With the above situation, the air supply to the building was not only via the various in-leakage paths but also, and no doubt pri=arily, via the Reactor Building supply dampers.
Any accident conditions postulated that require sedondary contain=ent in determining environmental releases would, under these conditions, have a second path permitting release of the Reactor Building air at approximately a 60-foot elevation.
.I.n order to prevent a reoccurrence of this ircident, a circuit design change will be i=ple=ented that will pea =it a Reactor Building supply fan breaker to be racked-out for =aintenance without defeating the Reactor Building supply da=per isolation logic. Until this design change can be.imple=ented, a standing order will be issued
- - fastructing plant personnel in the appropriate practice to be followed to avoid defeating the Reactor Building supply da=per isolation logic.
1 Very truly yours, l
M . .d h*- /
'~' Ivan R. Finftock' Jr.
Manager, Nuclear Generating Stations
\' '
IRF/pk Enclosuces cc: Mr. J. P. O'Reilly, Director Division of.Co=pliance, Region I 1
'I .
. October 6, 1972 .
- 1. r push button station, a relay is picked up which opens the nor= ally closed contact in the "B" standby liquid control pu=p starting circuit which prevents this pu=p from operating with the "A" pump running. The reverse is true if the "B" pump is started. The problem developed when the breaker for the "A" pu=p was racked out. It disabled the pu=p and at the same time it physically removed the contact in the startir.g circuitry for the "3" pu=p which s1=ulated an open contact. This prevented the "3" puny from starting. -
As soon as the Shift Foreman was aware of the inoperability of both pumps, he started a nor=al shutdown of the plant. In the meantime, he received permission to clear the maintenance safety tags and rack the "A" pump breaker to its nor=al position. He
- then ran a successful operability check on the "B" pup.p. The load reduction was stopped and the plant returned to full load.
In order to prevent a recurrence of this event, operating procedures have been changed so that operability tests of redundant engineered safeguards syste= cc=penents will be made i= ediately following any action that requires one of the systems to be ,
inoperable for maintenance purposes.
We are enclosing forty copies of this letter.
Very truly yours. -
[O7 }. [l lf 4/ .
Ivan R. Finfro'ck, h.
, .Vice President ,
IRF/pk
cc: Mr. J. P. 0.'Rei.11y, Director Directorate of Regulatory Operations, Region 1 .
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