ML19329A674

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RO 287/77-02:on 770214,primary-to-secondary Sys Leakage Found in 3B once-through Steam Generator.Caused by Leaking Tube W/Circumferential Crack.Leaking Tube & Ten Others Explosively Plugged.B&W Evaluating Tube Failure Causes
ML19329A674
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 02/28/1977
From:
DUKE POWER CO.
To:
Shared Package
ML19329A667 List:
References
RO-287-77-02, RO-287-77-2, NUDOCS 8001090658
Download: ML19329A674 (2)


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DUKE POWER COMPANY

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OCONEE UNIT 3 Report No.':

RO-287/77-2 Report ' Date':

February 28. 1977 Occurrence Date:

February 14, 1977 Facility:- Oconee Unit.3, Seneca, South Carolina Identification of Occurrence: Primary-to-secondary system leakage in "3B" once-through steam generator

. Conditions Prior to Occurrence:

Unit at 100 percent full power Description of Occurrence:

an increase in ra'iation levels as registered by air d

On February 14, 1977, ejector monitor 3RIA-40 indicated a possible primary-to-secondary system cleak.

Scapling of the steam lines and portable instrument readings con-firmed that primary-to-secondary-leakage was occurring in the "3B" once-t

,through steam generator (OTSG). Within two hours from the time that increasing readings were observed on 3RIA-40, a reactor shutdown was initiated.

Within six hours, reactor shutdown was completed and preparations were made to drain the Reactor Coolant System and investigate the source of the steam generator leakage.

t The Reactor Coolant System was cooled and drained withir 2h days following the initial high radiation indication and an internal fuspection of the

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'"3B" OTSG was initiated.

4 Apparent Cause of Occurrence:

1 Eddy current testing was performed and revealed one leaking tube, identified

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as tube number 19. in row 77. A fiber optics examination of this tube was 0 circumferential also made. The leaking tube was discovered to have a 45 approximately three feet below the upper tube sheet at the fifteenth et plate.

The tube is located along the "open tube lane" towards the o.

,e circumference of the tube bundle.

EddyJeurrent examinations of 142' adjacent tubes which included all tubes on 1

either side of the "open tube lar.e," revealed no additional tube leaks.

However,' characteristic eddy current signal distortions were found on tube 2Lof~ row-75 and tubes.12, 13, 14, 15, 16, 17, 18. 20 and 21 of row 77.

Therefore, as a' precautionary measure, these ten tubes were plugged.

With regard to this and previous Oconee steam generator tube leaks, evaluation

.by: Duke and_the OTSG vendor, the' Babcock & Wilcox Company, is continuing.

However, there is no evidence to date to indicate that the leaks - have resulted

-from tube wastage / thinning, chemical attack, or intergranular stress-corrosion

-cracking.

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e Analysis of Occurrence:

Primary-to-secondary system leakage, resulting from this occurrer was approximately 0.2 gallons per minute and was detected by installed radiation monitoring equipment.

The leakage did not exceed the operational limits of Oconee Technical Specification 3.1.6.1, however, a reactor shutdown was initiated within two hours after the initial leakage indication, following sampling and monitoring of components and systems during this period.

The calculated gaseous activity released to the environment via the air ejectors was 0.079 curies. This amount is considered insignificant in comparison to the station's annual release limit.

This report describes the sixth occurrence of steam generator tube leakage experienced on the three 0conee units.

Defective tubes were previously reported in Reportable Occurrence Reports R0-287/76-10, R0-269/76-17, R0-270/

76-15, R0-269/76-19, and R0-269/77-2 submitted by our letters of August 5, 1976, November 15, 1976, December 20, 1976, December 22, 1976, and January 31, 1977, respectively.

In the first three occurrences and the fifth and sixth occurrences, the defective tubes edged an open tube lane (a radial row with no tubes, used for inspection purposes).

In the fourth instance, the leaking defective tube was angularly located approximately 1500 from the locations of the other defective tubes and was not adjacent to an open tube lane.

It is considered that this incident did not affect the health and safety of the public.

Corrective Action:

The leaking defective tube and ten other tubes with questionable eddy current signals were explosive plugged in the bottom of the tube and plugged from the top by insertion of a metal rod in accordance with a vendor modification package. This method of plugging increases the tube's stability during operation.

As stated in R0-269/77-2 submitted by my letter of January 31, 1977, the OTSG vendor, Babcock & Wilcox, is currently involved in a program to further evaluate the cause of the tube failures.

This program includes a review of deposit samples, a computer evaluation of all available eddy current data, a review of visual observations from fiber-optics and ':1deotapes, and macro-microscopic analysis of two of the defective tubes that were removed from the Oconee Unit 2 "2B" OTSG. Additionally, the open lane flow characteristics are being analyzed and a detailed stress / vibration analysis is being conducted on the tubes in rows 75 and 77.

A review has been made of the Oconee station operating history, the Oconee steam generator manufacturing history and previously conducted OTSG analysis and testing results and no explanation of the phenomena has been determined to date.