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D. M. Smith i
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October 25, 1989 l-Docket No. 50-278 j
i Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555 i
SUBJECT:
Licensee Event Report Peach Bottom Atomic Power Station - Unit 3 p
This LER concerns an Engineered Safety Feature (ESF) actuation as a result l
of not following plant approved procedures, j
Reference:
Docket No. 50-278 Report Number:
3-89-004 l
Revision Number:
00 i
Event Date:
09/26/89 l
Report Date:
10/25/89 l
Facility:
Peach Bottom Atomic Powcr Station RD 1, Box 208A, Delta, PA 17314
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This LER is being submitted pursuant to the requirements of 10 CFR 50.73(a)(2)(iv).
Sincerely, i
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T. P. Johnson, USNRC Senior Resident inspector W. T. Russell, USNRC, Region 1 l
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At 0902 am, on September 26, 1989, with Unit 3 in Cold Shutdown, a Group IIA Primary Containment Isolation actuated, resulting in automatic closure of the Reactor Water Cleanup (RWCU) System (inboard)isolationvalveandtrippingofthe"3B"RWCUpump.
The root cause of the event was improper action resulting from a personnel error. A non-licensed utility maintenance planner opened a RWCU Low Pressure side Instrument Drain Valve. Opening the Instrument Drain Valve simulated a high flow condition in the RWCU suction piping and the isolation occurred as designed. At 0932 am the isolation logic was reset and the RWCU System was returned to service.
No safety consequences occurred as a result of this event. Had this event occurred at power, the temporary isolation of the RWCU System would have no significant impact on continued power operations or reactor water chemistry.
The individual involved in the event was counselled. This event and its consequences were discussed with appropriate Maintenance, Instrument and Control, and Plant Supervisory personnel. There were no previous similar events.
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c ac=-amami Recuirements for the Report This report is required per 10 CFR 50.73(a)(2)(iv) because an event occurred which resultedinanautomaticactuationofanEngineeredSafetyFeature(ESF).
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Unit Status at Time of the Event j
Unit 3 was shutdown with the Reactor Mode Switch (E!!S HS) in the shutdown position.
l 83B" Reactor Water Cleanup (RWCU) (EIISICE) pump (EIIStP) was operating.
The RWCU pump Differential Pressure Indicator (DPI) (EIIS DPI) was indicating down scale with the RWCU System in operation.
Description of the Event On September 26, 1989 at 9:02 am a Group !!A Inboard Primary Containment Isolation (PCI) (E!!S JM) occurred as a result of opening the Low Pressure side Instrument Drain Valve (LPIDV) (EIIS V) of the RWCU Differential Pressure Indicator Switch (DPIS)(EIIS:PDIS). A Group IIA inboard PCI results in tripping the RWCU pumps and l
1solatingtheRWCUSystembyclosingtheinboardRWCUsuctionvalve(M0-3-12-15)
(E!!S V)
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l The RWCU DPI was indicating down scale with the RWCU System in operation.
It was l
thought that the sensing line may be clogged.
In an attempt to determine if blockage j
l existed in the instrument lines a non-licensed utility maintenance planner individually opened the High Pressure side Instrument Drain Valve (HPIDV) and LPIDV to the RWCU DPIS. Drain flow was noticed from each side of the DPIS. Opening the LPIDV simulated a high flow condition in the RWCU suction piping (EIIS:FSP) and a Group IIA inboard PCI occurred as designed. Control Room Annunciators alerted the Control Room Operators of the Group IIA inboard PCI.
Subsequent investi At 0932 am the isolation logic (gationE!!d:#) was determined the cause of the isolation.
reset and the RWCU System was returned to service.
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Cause of the Event
The proximate cause of this event was failure to follow Plant approved work control procedures. The root cause of this event was an inappropriate action based on an incorrect perception that formal troubleshooting controls did not have to be followec'. This incorrect perception was based on the following conditions:
a) the RWCU DPI read down scale, and b) the HPIDV and LPIDV had tygon tubing connected to them leading to the floor drain (E!!S:DRN). Based on the long term shutdown of Unit i
3, with most systems having been out of service and the Instrument Drain Valves (IDV) having tygon tubing set up for the function the maintenance planner wanted to l
l perform, he opened the valves to check for blockage in the instrument lines.
One additional error was made which may have prevented this event.
The maintsnance planner failed to communicate with Control Room personnel, as required by plant procedures, his prospective actions prior to opening a valve. During the post incident investigation, the individual stated he realized he was not permitted to manipulate valves or controls.
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Analysis of the Event
No safety consequences occurred as a result of this event.
f The equipment properly responded to this event.
The isolation of the dump flow path andtheresultantincreaseofReactorPressureVessel(RPV)(E!!S:RPV)waterlevel l
increased the margin of safety with respect to adequate covering of the core (Ells:AC).
The regulation of reactor temperature utilizing the Residual Heat Removal (E!!S:BO) and Reactor Recirculation System (Ells:AD) was unaffected by the isolation l
of the RWCU System.
If this event occurred during power operations, there would be no actual or adverse consequences whether the RWCU System was aligned for normal operation or discharge to radwaste (E!!S WD).
During normal operation, the RWCU System removes water from the RPV for purification and returns water to the vessel via the feedwater (Ells:SJ) inlet resulting in no net inventory change.
During the discharge to radwaste mode of operation, up to approximately 7.0E4 lbs/hr of water may be withdrawn from the RPV.
t If the isolation had occurred under these circumstances, the change in RPV mass outflow would be insignificant, and is well within the capability of the feedwater control system to maintain RPV water level.
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During this event, the purification function of the RWCU System was unavailable for r
30 minutes.
The RWCU System could have been quickly returned to service, had this event occurred during power operation, and the effect on primary coolant chemistry would have been minimal.
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Corrective Actions
The Group IIA inboard PCI was reset, and the "3B" RWCU pump was returned to service.
The individual involved in the incident was counselled.
This event and its consequences were discussed with appropriate Maintenance.
l Instrument and Control, and Plant Supervisory personnel. The purpose of these discussions were to insure appropriate troubleshooting procedures are used, and stress the importance of realizing actions in the plant may have significant consequences including jeopardizinq personnel safety and challenging plant safety systems.
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Previous Similar Events
There were no previous LERs identified that resulted in an inboard Group IIA PCI as a result of failing to follow procedures.
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| 05000277/LER-1989-001-01, :on 890120,discovered That Instrument Calibr Requirements Associated w/intermediate-range Monitor Input Into Rod Block Instrumentation Not Satisfied by Existing Procedures.Caused by Personnel Inadequacies |
- on 890120,discovered That Instrument Calibr Requirements Associated w/intermediate-range Monitor Input Into Rod Block Instrumentation Not Satisfied by Existing Procedures.Caused by Personnel Inadequacies
| 10 CFR 50.73(a)(2)(1) | | 05000278/LER-1989-001-03, :on 890720,flow Estimate Not Performed When Reactor Bldg Exhaust Flow Recorder Made Inoperable.Caused by Procedure Not Requiring That Flow Rate Be Estimated within 4 H of Removing Recorder.Personnel Counseled |
- on 890720,flow Estimate Not Performed When Reactor Bldg Exhaust Flow Recorder Made Inoperable.Caused by Procedure Not Requiring That Flow Rate Be Estimated within 4 H of Removing Recorder.Personnel Counseled
| 10 CFR 50.73(a)(2)(1) | | 05000278/LER-1989-002-03, :on 890829,reactor Vessel lo-lo-lo Level Signal Generated Resulting in Unit 2 RHR Pump Trip Signal.Caused by Combination of Personnel Error & Degraded Equipment.Trip Alarms Cleared & Isolation Valve Replaced |
- on 890829,reactor Vessel lo-lo-lo Level Signal Generated Resulting in Unit 2 RHR Pump Trip Signal.Caused by Combination of Personnel Error & Degraded Equipment.Trip Alarms Cleared & Isolation Valve Replaced
| | | 05000277/LER-1989-002-01, :on 890202,determined That Several Conditions Found During Analysis of Unsuccessful Special Test of Emergency Cooling Sys May Inhibit Function of Sys Needed to Maintain Safe Shutdown |
- on 890202,determined That Several Conditions Found During Analysis of Unsuccessful Special Test of Emergency Cooling Sys May Inhibit Function of Sys Needed to Maintain Safe Shutdown
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000278/LER-1989-003-03, :on 890808,subsequent Sys Walkdown & Analysis Revealed That as-found Configuration Would Result in Piping Stresses Adjacent to Valves Exceeding Code Limits.Caused by Design & Installation Error |
- on 890808,subsequent Sys Walkdown & Analysis Revealed That as-found Configuration Would Result in Piping Stresses Adjacent to Valves Exceeding Code Limits.Caused by Design & Installation Error
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1989-003-01, :on 890207,group 2C Primary Containment Isolation Sys Valve Isolation Occurred Resulting in motor- Operated Feedwater Flush Valves Receiving Signals to Close. Caused by Stated Inadvertent Signals |
- on 890207,group 2C Primary Containment Isolation Sys Valve Isolation Occurred Resulting in motor- Operated Feedwater Flush Valves Receiving Signals to Close. Caused by Stated Inadvertent Signals
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-003, :on 890207,Group 2C Primary Containment Isolation Sys Valve Isolation Occurred & Reactor Scrammed. Caused by Inadvertent Reactor Vessel Pressure Signals. Scram Reset & Isolation Valve Replaced |
- on 890207,Group 2C Primary Containment Isolation Sys Valve Isolation Occurred & Reactor Scrammed. Caused by Inadvertent Reactor Vessel Pressure Signals. Scram Reset & Isolation Valve Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000278/LER-1989-004-03, :on 890926,Group Iia Primary Containment Isolation Actuated Closing of RWCU Sys Isolation Valve & Tripping RWCU Pump 3B.Caused by Personnel Error.Isolation Logic Reset & Individual Counselled |
- on 890926,Group Iia Primary Containment Isolation Actuated Closing of RWCU Sys Isolation Valve & Tripping RWCU Pump 3B.Caused by Personnel Error.Isolation Logic Reset & Individual Counselled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-004-01, :on 890320,HPCI Sys Unable to Fulfill Safety Function During Postulated Design Basis Events.Caused by Design Deficiency.On 890330,step Starting Resistors Removed from Power Circuits |
- on 890320,HPCI Sys Unable to Fulfill Safety Function During Postulated Design Basis Events.Caused by Design Deficiency.On 890330,step Starting Resistors Removed from Power Circuits
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000278/LER-1989-005-03, :on 891020,reactor Protection Sys Actuation & Primary Containment Isolation Sys Actuation Occurred Due to False High Reactor Pressure Signal & lo-lo Reactor Vessel Level Signal,Respectively.Caused by Spike |
- on 891020,reactor Protection Sys Actuation & Primary Containment Isolation Sys Actuation Occurred Due to False High Reactor Pressure Signal & lo-lo Reactor Vessel Level Signal,Respectively.Caused by Spike
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-005-01, :on 890406,determined That Numerous Pull Apart Terminal Blocks Found Not to Be Securely Fastened Causing Failure of Safety Function.Caused by Deficiency Inadequacy. Pull Apart Terminal Blocks Refastened |
- on 890406,determined That Numerous Pull Apart Terminal Blocks Found Not to Be Securely Fastened Causing Failure of Safety Function.Caused by Deficiency Inadequacy. Pull Apart Terminal Blocks Refastened
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1989-006, Corrected LER 89-006-00:on 890209 & 25,determined That Tubing to Containment Isolation Valve Installed W/Inadequate Support & Containment Atmosphere Control & Dilution Sys Not Per Applicable Installation Criteria.Controls Estab | Corrected LER 89-006-00:on 890209 & 25,determined That Tubing to Containment Isolation Valve Installed W/Inadequate Support & Containment Atmosphere Control & Dilution Sys Not Per Applicable Installation Criteria.Controls Established | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000278/LER-1989-006-04, :on 891023,during Reactor Temp Adjustment, Reactor High Pressure Scram Occurred.Caused by Improper Planning & Coordination of Multiple Evolutions.Surveillance & Hydrostatic Test Revised |
- on 891023,during Reactor Temp Adjustment, Reactor High Pressure Scram Occurred.Caused by Improper Planning & Coordination of Multiple Evolutions.Surveillance & Hydrostatic Test Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-006-01, :on 890209,NRC Inspector Discovered That Tubing to Torus Air & Nitrogen Purge 18 Inch Containment Isolation Valve Installed W/Inadequate Support.Caused by Deficient Installation & Maint Instructions |
- on 890209,NRC Inspector Discovered That Tubing to Torus Air & Nitrogen Purge 18 Inch Containment Isolation Valve Installed W/Inadequate Support.Caused by Deficient Installation & Maint Instructions
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1989-007, Corrected LER 89-007-00:on 890411,green Discoloration Discovered in Grease on Stabs of Control Fuses in Switchgear.Root Cause of Event Under Investigation.Stabs Lubricated W/Different Type of Approved Grease | Corrected LER 89-007-00:on 890411,green Discoloration Discovered in Grease on Stabs of Control Fuses in Switchgear.Root Cause of Event Under Investigation.Stabs Lubricated W/Different Type of Approved Grease | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000278/LER-1989-007-04, :on 891026,reactor Vessel Temp & Reactor Coolant Pressure Not Logged Every 15 Minutes as Required by Tech Spec 4.6.A.2 During Performance Integrated Leak Rate Testing.Caused by Procedure Deficiency |
- on 891026,reactor Vessel Temp & Reactor Coolant Pressure Not Logged Every 15 Minutes as Required by Tech Spec 4.6.A.2 During Performance Integrated Leak Rate Testing.Caused by Procedure Deficiency
| 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1989-007-01, :on 890401,green Discoloration Discovered in Grease on Stabs of Several Control Fuses in 4 Kv Switchgear. Cause Under Investigation.Switchgear Fuse Boxes Inspected & Cleaned as Necessary |
- on 890401,green Discoloration Discovered in Grease on Stabs of Several Control Fuses in 4 Kv Switchgear. Cause Under Investigation.Switchgear Fuse Boxes Inspected & Cleaned as Necessary
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1989-008-01, :on 890415,incorrect Undervoltage Trip Fuses Placement by Operator Occurred Due to Inadequacy of Training Resulting in Isolation of RWCU Sys.Caused by Administrative Deficiency.Training Ltr Will Be Issued |
- on 890415,incorrect Undervoltage Trip Fuses Placement by Operator Occurred Due to Inadequacy of Training Resulting in Isolation of RWCU Sys.Caused by Administrative Deficiency.Training Ltr Will Be Issued
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000278/LER-1989-008-03, :on 891027,primary Containment Isolation Sys Group II & III Isolations Occurred When Spurious Reactor Low Level Signal Sensed by Instruments.Possibly Caused by Air Bubble in Sensing Lines.Line Backfilled |
- on 891027,primary Containment Isolation Sys Group II & III Isolations Occurred When Spurious Reactor Low Level Signal Sensed by Instruments.Possibly Caused by Air Bubble in Sensing Lines.Line Backfilled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000278/LER-1989-009-03, :on 891207,HPCI Sys Declared Inoperable When Sys Failed to Start During Pump,Valve & Flow Surveillance Test.Caused by Loose Lock Nut on HPCI Oil Sys Relief Valve. Lead Seal Wire to Be Placed on Valve Caps |
- on 891207,HPCI Sys Declared Inoperable When Sys Failed to Start During Pump,Valve & Flow Surveillance Test.Caused by Loose Lock Nut on HPCI Oil Sys Relief Valve. Lead Seal Wire to Be Placed on Valve Caps
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1989-009-01, :on 890505,while Performing HPCI Operability Testing,Hpci Sys Did Not Respond Properly to Flow Control Signals.Caused by Failure to Follow Installation Instructions.Mod Process Enhancements Planned |
- on 890505,while Performing HPCI Operability Testing,Hpci Sys Did Not Respond Properly to Flow Control Signals.Caused by Failure to Follow Installation Instructions.Mod Process Enhancements Planned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000278/LER-1989-010-03, :on 891211,monthly Surveillance Test ST 9.7 Not Performed within Surveillance Interval Established by Tech Spec Table 4.1.1.Caused by Combination of Programmatic Weaknesses.Review Performed |
- on 891211,monthly Surveillance Test ST 9.7 Not Performed within Surveillance Interval Established by Tech Spec Table 4.1.1.Caused by Combination of Programmatic Weaknesses.Review Performed
| 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1989-010-01, :on 890514,50% Control Rod Density Exceeded W/O Demonstrating Operability of Rod Sequence Control Sys.Caused by Personnel Error.Shift Manager Counseled & Control Rod Pull Sheet Revised |
- on 890514,50% Control Rod Density Exceeded W/O Demonstrating Operability of Rod Sequence Control Sys.Caused by Personnel Error.Shift Manager Counseled & Control Rod Pull Sheet Revised
| 10 CFR 50.73(a)(2) | | 05000278/LER-1989-011-03, :on 891213,discovered That Two Surveillance Tests of Turbine Stop & Control Valve Encl Not Performed Per Tech Specs.Caused by Incorrect Std Practice of Surveillance Testing.Programmatic Controls Established |
- on 891213,discovered That Two Surveillance Tests of Turbine Stop & Control Valve Encl Not Performed Per Tech Specs.Caused by Incorrect Std Practice of Surveillance Testing.Programmatic Controls Established
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1989-011, :on 890424,scram Discharge Vol Drain & Vent Valve Stroking Surveillance Test Not Performed.Caused by Procedural Deficiency & Scheduling Error.Surveillance Test Completed Satisfactorily on 890429 |
- on 890424,scram Discharge Vol Drain & Vent Valve Stroking Surveillance Test Not Performed.Caused by Procedural Deficiency & Scheduling Error.Surveillance Test Completed Satisfactorily on 890429
| 10 CFR 50.73(a)(2)(1) | | 05000278/LER-1989-012-01, :on 891222,determination Made That Potential Existed for Loss of Reactor Coolant Inventory Beyond Makeup Capability of RCIC Sys Relied Upon in Fire Protection Program Analysis for Fire in Fire Area 13N |
- on 891222,determination Made That Potential Existed for Loss of Reactor Coolant Inventory Beyond Makeup Capability of RCIC Sys Relied Upon in Fire Protection Program Analysis for Fire in Fire Area 13N
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000277/LER-1989-012-01, :on 890519,feedwater Control Malfunction Occurred Resulting in Low Level Reactor Scram.Caused by Failure of Feedwater Level Control Selector Switch.Failed Switch Replaced & Procedures Enhanced |
- on 890519,feedwater Control Malfunction Occurred Resulting in Low Level Reactor Scram.Caused by Failure of Feedwater Level Control Selector Switch.Failed Switch Replaced & Procedures Enhanced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-012, :on 890519,reactor Hi Lo Level Alarm Sounded & Reactor Feed Pumps B & C Tripped Simultaneously.Caused by Failure of Feedwater Level Control Switch.Switch Replaced, Amplifier Replaced & Procedures Revised |
- on 890519,reactor Hi Lo Level Alarm Sounded & Reactor Feed Pumps B & C Tripped Simultaneously.Caused by Failure of Feedwater Level Control Switch.Switch Replaced, Amplifier Replaced & Procedures Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-013-01, :on 890603,required Test for Diesel Generator Cardox Room Smoke Detectors Was Not Performed.Caused by Lack of Effective Method for Communicating Surveillance Test Status to Shift Manager |
- on 890603,required Test for Diesel Generator Cardox Room Smoke Detectors Was Not Performed.Caused by Lack of Effective Method for Communicating Surveillance Test Status to Shift Manager
| 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1989-014-01, :on 890517,noted That Required Surveillance Test for Radwaste Bldg 116 Ft Elevation Chemical Addition & Laundry Room Smoke Detectors Overdue. Caused by Procedural Deficiency |
- on 890517,noted That Required Surveillance Test for Radwaste Bldg 116 Ft Elevation Chemical Addition & Laundry Room Smoke Detectors Overdue. Caused by Procedural Deficiency
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1989-015-01, :on 890721,main Turbine Bypass & Control Valves Opened,Causing Main Steam Line Pressure to Decrease to Approx 480 Psig & Full Reactor Scram.Caused by Malfunction of Pressure Regulator Set.Component Replaced |
- on 890721,main Turbine Bypass & Control Valves Opened,Causing Main Steam Line Pressure to Decrease to Approx 480 Psig & Full Reactor Scram.Caused by Malfunction of Pressure Regulator Set.Component Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-015, :on 890721,while Attempting to Remove Malfunctioning Reactor Pressure Vessel Regulator Set,Bypass & Control Valves Opened,Causing Steam Line Pressure to Increase to 480 Psig.Components Replaced |
- on 890721,while Attempting to Remove Malfunctioning Reactor Pressure Vessel Regulator Set,Bypass & Control Valves Opened,Causing Steam Line Pressure to Increase to 480 Psig.Components Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-016-01, :on 890722,APRM hi-hi Signal Caused LPRM Detector 4B-40-33 to Spike Upscale.Caused by Output Signal of LPRM Detector Spiking High.Detector Placed in Bypass Position & Scram Signal Reset |
- on 890722,APRM hi-hi Signal Caused LPRM Detector 4B-40-33 to Spike Upscale.Caused by Output Signal of LPRM Detector Spiking High.Detector Placed in Bypass Position & Scram Signal Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-016, :on 890720 & 22,LPRM Detector 4B-40-33 Spiked High,Resulting in Full Reactor Scram Signal While in Cold Shutdown.Caused by Design/Mfg Defect in GE Detector. Detector Placed in Bypass Position |
- on 890720 & 22,LPRM Detector 4B-40-33 Spiked High,Resulting in Full Reactor Scram Signal While in Cold Shutdown.Caused by Design/Mfg Defect in GE Detector. Detector Placed in Bypass Position
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-017-01, :on 890815,failure to Establish Continuous Fire Watch Occurred Due to Inoperable Sprinkler Sys.Caused by Ineffective Fire Protection Sys Training.Event Reviewed W/Personnel |
- on 890815,failure to Establish Continuous Fire Watch Occurred Due to Inoperable Sprinkler Sys.Caused by Ineffective Fire Protection Sys Training.Event Reviewed W/Personnel
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1989-018-01, :on 890818,personnel Failed to Place APRM Rod Block Settings in Tripped Condition within 1 H of Determining Nonconservative Settings.Total Core Flow Calibr & APRM Sys Calibr Revised Re Personnel Actions |
- on 890818,personnel Failed to Place APRM Rod Block Settings in Tripped Condition within 1 H of Determining Nonconservative Settings.Total Core Flow Calibr & APRM Sys Calibr Revised Re Personnel Actions
| 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1989-019-01, :on 890830,discovered That Five Doors Requiring Monthly Functional Tests,Per Tech Specs,Not Included on Surveillance Test.Caused by Deficiency in Methodology & Refs Used During Surveillance |
- on 890830,discovered That Five Doors Requiring Monthly Functional Tests,Per Tech Specs,Not Included on Surveillance Test.Caused by Deficiency in Methodology & Refs Used During Surveillance
| 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1989-020-02, :on 890915,discovered That RHR Pump Motors & Core Spray Pump Motors Had Nonconforming Boot Installation Configuration.Caused by Less than Adequate or Incomplete Procedures.Splice Configurations Restored |
- on 890915,discovered That RHR Pump Motors & Core Spray Pump Motors Had Nonconforming Boot Installation Configuration.Caused by Less than Adequate or Incomplete Procedures.Splice Configurations Restored
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1989-021-01, :on 890920,control Room Emergency Ventilation Actuation Occurred Due to False High Radiation Signal.Cause Unknown.Wire Connections to Terminal Strip Verified to Be Tight |
- on 890920,control Room Emergency Ventilation Actuation Occurred Due to False High Radiation Signal.Cause Unknown.Wire Connections to Terminal Strip Verified to Be Tight
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-022-01, :on 891003,unterminated Lead in Circuit to HPCI Trip Solenoid Rendered HPCI Stop Valve Trip Functions Inoperable.Caused by Leads Loosely Hanging Inside Door Panel.Hanging Leads Secured & Panel Inspected |
- on 891003,unterminated Lead in Circuit to HPCI Trip Solenoid Rendered HPCI Stop Valve Trip Functions Inoperable.Caused by Leads Loosely Hanging Inside Door Panel.Hanging Leads Secured & Panel Inspected
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1989-023-01, :on 891005,outboard MSIV Ac Solenoid Pilot Valves de-energized,resulting in Expected Closure of Outboard MSIV D & Automatic Reactor Scram.Caused by Incomplete Guidance.Procedure Revised |
- on 891005,outboard MSIV Ac Solenoid Pilot Valves de-energized,resulting in Expected Closure of Outboard MSIV D & Automatic Reactor Scram.Caused by Incomplete Guidance.Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-024, :on 891006,local Power Range Monitor Spike Caused Reactor Scram Signal While in Hot Shutdown.Caused by Design &/Or Mfg Process as Identified by Ge.Detector Placed in Bypass Position & Scram Signal Reset |
- on 891006,local Power Range Monitor Spike Caused Reactor Scram Signal While in Hot Shutdown.Caused by Design &/Or Mfg Process as Identified by Ge.Detector Placed in Bypass Position & Scram Signal Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-024-01, :on 891006,reactor Protection Sys Initiated Full Reactor Scram Signal.Caused by Output Signal for LPRM 40-33A Spiking High.Lprm Detector Placed in Bypass Position & Scram Signal Reset |
- on 891006,reactor Protection Sys Initiated Full Reactor Scram Signal.Caused by Output Signal for LPRM 40-33A Spiking High.Lprm Detector Placed in Bypass Position & Scram Signal Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-025-01, :on 891007,determined That nonsafety-related Bellows Leak Detecting Pressure Switches Installed on Main Steam Relief Valves Could Prevent Opening During Design Basis Condition.Plant Alteration Installed |
- on 891007,determined That nonsafety-related Bellows Leak Detecting Pressure Switches Installed on Main Steam Relief Valves Could Prevent Opening During Design Basis Condition.Plant Alteration Installed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1989-026-01, :on 891012,control Room Emergency Ventilation Sys Actuation Occurred Due to Momentary False High Radiation Signal from Control Room Radiation Monitor B.Caused by Sensitivity of Thumbwheel Switch |
- on 891012,control Room Emergency Ventilation Sys Actuation Occurred Due to Momentary False High Radiation Signal from Control Room Radiation Monitor B.Caused by Sensitivity of Thumbwheel Switch
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-027-01, :on 891016,observation & Logging of Suppression Pool Temp as Required by Tech Spec 4.7.2 Not Met.Caused by Personnel Error.Operations Shift Team Counseled |
- on 891016,observation & Logging of Suppression Pool Temp as Required by Tech Spec 4.7.2 Not Met.Caused by Personnel Error.Operations Shift Team Counseled
| 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1989-028-01, :on 891108,review Determined That Standby Gas Treatment Sys Heater Control Relays Unqualified for post-LOCA Radiation Environ & Declared Inoperable.Cause Undetermined.Radiation Shielding Installed |
- on 891108,review Determined That Standby Gas Treatment Sys Heater Control Relays Unqualified for post-LOCA Radiation Environ & Declared Inoperable.Cause Undetermined.Radiation Shielding Installed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1989-028, :on 891108,determined That Standby Gas Treatment Sys Heater Control Relays Installed W/O Environ Qualification.Caused by Lack of Procedural Guidance.Relays Relocated |
- on 891108,determined That Standby Gas Treatment Sys Heater Control Relays Installed W/O Environ Qualification.Caused by Lack of Procedural Guidance.Relays Relocated
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1989-029, :on 891117,primary Containment Isolation Sys Actuation Occurred During Performance of Refueling Floor Ventilation Exhaust Radiation Monitor Testing.Cause Unknown. Selector Switch & Relay Contacts Cleaned |
- on 891117,primary Containment Isolation Sys Actuation Occurred During Performance of Refueling Floor Ventilation Exhaust Radiation Monitor Testing.Cause Unknown. Selector Switch & Relay Contacts Cleaned
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000277/LER-1989-029-01, :on 891117,Group III Primary Containment Isolation Sys Actuation Occurred During Refueling Floor Ventilation Exhaust Radiation Monitor Testing.Cause Unknown. Test Procedure to Be Revised |
- on 891117,Group III Primary Containment Isolation Sys Actuation Occurred During Refueling Floor Ventilation Exhaust Radiation Monitor Testing.Cause Unknown. Test Procedure to Be Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
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