ML19326C108

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RO 50-313/76-14:on 760628:svc Water Valve CV-3812 Failed to Open on Command During Surveillance Test.Caused by Apparent Binding Between Stem & Bushing.Stem & Bushing Will Be Replaced
ML19326C108
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 07/16/1976
From: Cook R
ARKANSAS POWER & LIGHT CO.
To:
Shared Package
ML19326C101 List:
References
NUDOCS 8004180768
Download: ML19326C108 (4)


Text

LICENSEE EVENT REPORT CONTROL BLOCK:l l

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NAME LCENSE NUMOFR Y E TY lAIRIAIRIKill 10101-1010101010l-10101 141 l 111 I Il i 1013 l 1

7 89 14 15 25 28 30 31 32 CATEGCRY T

DOCKET NUMBEA EVENT DATE REPORT DATE O 1 CON'T l l

l lLl IOl 5 lo l-l 013 l i 13 l lOl(olZl8lT161 1017lIlGl7161 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTION ss IAL l'ioo kours on ro-28-7eo clu,ino g.urve,itance testin, 9 process l

7 89 80 Eg Ivadiation monitor RI S814, valve CV 3811 Qailed E opes ow cowonawd l

7 89 80 EE l clue ko apparewt 'bindiwg in valve hekweew skemand I)LEshiwq. YAkVe pk& cec}

l 7 89 80 EE lin ES posibiow pey Teck Spec 3.3. New stem and buW will be installect I

7 89 na Ickrina refuelino shut doww(( 50-SI S / 76 -l @,

I 80 7 89 k-y 80 DE CODE C PONENT C M

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F CLITY METHOD OF STATUS

% POWER OTHEA 1TATUS DISCOVERY CISCOVERY DESCAIPTON LGJ 1o101o1 I N A I lbl I

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10 12 13 44 45 48 80 AFLF SED OF L ASE.

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10 11 44 45 80 PERSONNEL EXPOSURES NUMBEA TYPE DESC'ArpTON EE l0lO1 OI LZJ l

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7 89 11 12 80 OFFSITE CONSEQUENCES DE I klA I

7 89 80 LOSS OR OAMAGE TO FACILITY Twf DE LZJ lDESCR'PdTA I

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NAME:

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No.

50-313/76-14

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  • Reportaleic Occurrence Report 2.

,itcport Date: July 16, 1976 3

Occurrence liitt_e,:

June 28, 1976 4

Facility: Arkansas Nuclear.One - Unit 1 Russellville, Arkansas 5.

Identification of Occurrenec:

Reactor Building cooling unit service water valve CV-3812 failed to j

.open on command.

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Canditions Prior to Occurrence:

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Steady-State Power Reactor Power n

Mitth Ilot Standby Net Output n

MIVe Cold Shutdown Percent of Full Power

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't Refueling Shutdown Load Changes During Routine Power Operation Routine Startup Operation Rotitine Shutdown Operation j

Other (specify] 'Not shutdown il 4

7.

Description of Occurrence:

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At approximately 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on June 28, 1976 during surveillance testing of process radiation monitor RI3814, valve CV-3812 failed to open on i

consnand. The valve required ES position is open.

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Attachuent "C" March 23,l1976 NSP-In, Rev. 4 Page 2 of 4 i

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j Ucportable Occurrence !!cport No*

50-313/76-14 Des i gna t ion o f Appa ren t Ca us.e..o.l'..Oc.c..u.r..rence.:

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t Design l'rocedu rc 1

3 thnufacture IJnnsual Service Condit ion y

Including linvi ronmental Installation /

Construction

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Component Failure Operator e

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' Othe r : (speci fy)

A The failure appears to be from binding in the valve.between the valve i

stem and bushing.

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Analysis of Occurrence:

Since the redundant loop was operable and the affected loop was operable when CV-3812 was opened, there was na hazard to the health and safety of the public.

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4 At t nelunent "C"

tb rch 23, 1976 NSP-10, Rev. 4 Page Z "f 4 7

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i Reportaisic Occurrence !!cport do.

50-313/76-14 10.

Corrective Action:

4 The valve can't be inspected internally at this time, but it i

L placed in its ES position per Technical Specification 3.3.

New valve during a refueling shutdown. stems and bushings will be installed in CV-3812 j

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Failure Data:

There has been one other failure of this type reported in 50-313/75-1.

Valve type is Contromatics butterfly valve flodel 600SRIIS 4

Serial No. 83154-A-1-1

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1 l-i At tacInnent "C"

. Alarch ~23, 1976 NSP-10,-Rev. 4 Page 4 of 4 r

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