ML19326B941

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Safety Evaluation Supporting Design of Steam Line Break Instrumentation & Control Sys, & Emergency Feedwater & Reactor Protective Sys Mods
ML19326B941
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 02/12/1975
From:
Office of Nuclear Reactor Regulation
To:
Shared Package
ML19326B938 List:
References
NUDOCS 8004180653
Download: ML19326B941 (6)


Text

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RAFETY EVALUATION BY THE DIVISION OF REACTOR LICENSING NUCLEA2 REGULATORY COMMISSION OF MATTERS REMAINING FROM THE FACILITY OPERATIONS LICENSE REVIEW ARKANSAS NICLEAR ONE - UNIT 1 DOCKET NO. 50-313 i

A.

Identification of Review Items When Facility License No. DPR-51 was issued for Arkansas Nuclear One - Unit 1 (ANO-1) on May 21,1974, to Arkansas Power

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. Company (AP&L), two matters were left for post licensing review and resolution. These were the design of the Steam Line Break Instrumentation and Control System and the interconnection of a non-safety grade control system to components'of the safety related Emergency Feedwater System. A third item, a modification of the shutdown bypass circuitry in the Reactor Protective System, was submitted for our review by AP&L on April 29, 1974.

B.

Shutdown Bypass Circuitry Modification The addition of another RPS power trip bistable in the shutdown bypass circuit of each of the four redundant channels enhances safety in that it replaces an administrative control function with an automatic function, and it reduces possibilities of error in resetting the overpower trip setpoint.

This modification does not affect any other safety related system.

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The detailed drawings of this modification which were furnished to the NRC staff were reviewed. The staff finds that the modifi-cation satisfies the requirements of IEEE Std 279-1971 and concludes that this modification enhances safety and is acceptable.

C.

Emergency Feedwater System When the ANO-1 reactor is shut down, decay heat must be removed from the reactor through at least one of the steam generators until the plant has been coole4 and depressurized sufficiently to permit use of the Decay Heat Removal System. As long as offsite power is available, the Main Feedwater and Condensate Systems are able to furnish the needed flow to the steam generator. However, to provide an assured source of feedwater if offsite power is lost, AP&L has provided the Emergency Feedwater System (EFWS). The EFWS consists of two full capacity EFW pumps, two s,arces of feed-water and the piping, valves, and controls needed to deliver feed-water to either or both steam generators.

The decay heat removal is achieved by delivering feedwater to at least one steam generator and venting the generated steam through the turbine bypass valves, the atmospheric dump valves, or the steam relief valves. AP&L was advised that the EFW system is required for safety and as such, it should meet the single failure criterion; and the instrumentation, control and electrical equipment should be designed to conform with IEEE Std 279-1971 and IEEE Std 308-1971. AP&L amended the design to satisfy the above stated criterion and standcrds.

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Both manual arJ utomatic controls are provided to establish EFW flow paths to 6de steam generators. The automatic function is accomplished through the Integrated Control System (ICS).

In view of the non-safety gradastatus of the ICS, an analysis has been performed by AP&L to establish that in the event of a failure in the autematic control system there is sufficient time for the operator to initiate the operation of the EFW system manually before the core is endangered.

In addition, AP&L proposed to install Class IE isolation devices between the ICS and the EFW System so that failures in the ICS could not propagate to the i

EFWS and prevent operator control of that system when manual control is needed. While the use of these isolation devices was under review, AP&L agreed to disconnect the automatic ICS controls from the EFWS. We have reviewed the final design of the EFWS with the use of ICS control through Class IE isolation devices and have concluded that the design satisfies the single failure criterion, IEEE Std 279-1971 and IEEE Std 308-1971 and is acceptable. This control arrangement does not affect any other safety related system.

D. Steam Line Break Instrumentation and Control System The applicant has analyzed the response of the ANO-1 reactor to the uncontrolled blowdown of a single steam generator caused by a postulated steam line break. As presented in Section 14.2.2 of the FSAR, the analysis shows a return to 2.6% power after blowdown 9

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of one steam generator, occurring in less than one minute. The analysis of a blowdown of both steam generators was requested since the main steam block valves were set up for remote manual control and the main feedwater valves are closed by the non-safety grade ICS.

The applicant committed to install a reliable system of iso-lating the seismic category I section of the system to preclude such double blowdown.

This system, the steam line break instru-mentation and control system (SLBIC), : rill sense low steam pres-sure and automatically close the main steam and main feedwater block valves. We reviewed the original design of the SLBIC and found it unacceptable since it did not meet all the requirements of IEEE Std 279-1971.

Recognizing that the arount of reactivity inserted by a steam generator blowdown increases with core burnup, AP6L analyzed double steam generator blowdown to establish how far in core burnup the plant could proceed without the risk of unacceptable reactivity insertion. AP&L's final analysis of blowdown of both steam genera-tors showed acceptable consequences up to 225 full power days (after which the SLBIC would be needed).

The applicant has since revised the design of the SLBIC and resub-mitted sufficient information in Amendment No. 46 to the Final Safety Analysis. Report and in supporting letters dated l

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The final revisions to the SLBIC design included the following changes to resolve I

staff concerns:

a.

The SLBIC cabinets were relocated to the protected environ-ment of the class I electrical equipment room.

b.

The SLBIC pressure switches were relocated to the air com-i prescor room outside the electrical equipment room so that the effects of a pressure sensing steam line rupture would not impair the operability of equipment in the electrical equipment room.

c.

The SLBIC emergency power supply channels were electrically and physically separated.

d.

Logic channel circuitry revisions were made to provide full testability and status indication.

We have reviewed the final design of the SLBIC and concluded that the design satisfies the single failure criterion and IEEE Std 279-1971 and is acceptable.

The SLBIC shall be installed and its operability required by Technical Specifications before the first core burnup exceeds 225 effective full power days.

, E.

Conclusion We have concluded, based on the considerations discussed above, that these three matters are acceptably resolved as indicated, O

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undue risk to the health and safety of the public.

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