ML19323C883
| ML19323C883 | |
| Person / Time | |
|---|---|
| Site: | Oyster Creek |
| Issue date: | 05/13/1980 |
| From: | Baran R, Schofield J JERSEY CENTRAL POWER & LIGHT CO. |
| To: | |
| Shared Package | |
| ML19323C881 | List: |
| References | |
| NUDOCS 8005190367 | |
| Download: ML19323C883 (2) | |
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.Date.or Report Date:
5/13/80
~. Occurrence:
5/12/80 e
Initial Written
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Time of
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13/13/6_0 Occurrence:
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Recortsble 0ccurrence Report tfo. 50-219/an-16 D
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IDENTIriCATI9N
~'Yf oliitt en' or th'e' Technicalfspectrications, par.sgesch.'3.1.A.2.
OF OCCURRENCEL
..(Table 3.1.1-Itet AT2) when pressure swf tch I'3L'O' was found
... defective.and inoperable.
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.,T This event is considered to be a "a. cort.1Ste awarrenca,n da r ined
~ f ;.4 " t M.r.;, 5nI W spar,1etq,giap3, 737 7.pu q,g,2,g,2 COND(TIONS PHOR
- Steady state Power Routine SNtdown TO OCCUR 1tENCE:
rot Staadby '
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Opera tion
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Cold Shutdewn load Channet Ovefnq X
Refueling Shutdown Routine Fewer Operation
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Rootfne Startup Other (Spec li'y)
. Operation N ctnr subv i1.i.41 Reector noda switch locked in refuel Cavity flooded DESCRiprinN On Aorf1 70, loRO. while perromin? surveillanca nn nea.rster GF OCC1JPPENCE:
Iced re f action sansors, crassure switch Mt."0" c roun<<
detfec tive.
Subsequent investigation (5/12/80) revealed that tbt Dressure switch would not have trippad at any pressure dua to a mislocat-d creaittnq tm-within the swf tch hevsing.
9 ? ace *.he piv
- wn 95 :Mmm re 3 -ofu finq r e sca tha switch was rwad and will he replaced with a new switch prior to plant startun.
Surveillance pretadu e records Indicate tM PSL"D" switch perfomed satisfactorfly en 12/70/79 when tha isst surveillance test wu per1 W.
Th.
rore, the switch is considar=1 to bey = baen t ter-re1
- b*twarn IR/20/79 and 1/5/S0 wnen the 1980 Refuelino Ont.1ga began.
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- h. snevsf11 rce narecrwad en a/2C/30. tha e.vfu rida n t orgssure swite.h PSt,"F)~ t et th= sene trio cMnnel was feund ful f g>C" in the independent trip channel ccerable as well as the two r*1undant sensors, PSL"A" and
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Report fio. 50-219/80-i6-1P
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APPARE*fT CAUSE
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Procedure ~ -
0F OCCURRENCE:
- 19enufacture '.
T7 Unusual Service ;ondIt1on r
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Inc.Enviromental L.
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Other (Spectfy)
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ANALY9IS OF The gener=*.or lead rajection sensors are p--nure swf t:Ns
~ OCCURP.ENCE:
.. T '. sensing hydraulic o fi pressure on the turbine accele-atfon relay.
There are four sensors; two redumf ant sensors in
. each of two indeP9"dont trip chann.T=.
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The function of these sensor-15 to provide an anticipatory
- i,3. ycre s ign=1 wh-n la=4 is caja -*ad fete the gaa**5 *~
'.a minf:nize reactor pre?.surintion transients The safety
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....signiffeince or t% failed sensor is censida cd minfra'
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~, ~.since the redundant tefp ctwrmel sensor was nnerable and t.h*
indeca=49nt trf o chann=1 was orareSt e.
The** Fora, the trip w.
4 function was not Inst and a scre would have resultet f f a
' 9enerator f ood re,iection had occurred.
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.TNe defective prassure. switch was disassembled and inspected, CORRECTIVE ACTIOM:
it was found that a plastic linkage that activates the swf tch had fallen out of place and caused the fs11ure.
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' Pean Centrois Im:.
o-~t Sw f M "ce ! %.che "7M - 15
.,_.' ~ Serf 31 Number B70
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Ranoa 50 to 240 05i Sa tUno:
1R0 t',I (Decreasing Traswre)
Peerared by:
U '. - ~ ' * ~ '- -
A-nate:
s' ' o Jim Schoffaid Approved by:
Date:
Ronala# __daran
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