ML19322C155

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RO-287/76-09:on 760713,power Increase Exceeded Power Level Cutoff During Feedwater Transient.Caused by Feedwater Demand Decrease.Induced Oscillation Resulted in Increased Flow & Temp Decrease.Manual Control Reduced Power
ML19322C155
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 07/27/1976
From:
DUKE POWER CO.
To:
Shared Package
ML19322C151 List:
References
NUDOCS 8001090565
Download: ML19322C155 (2)


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OCONEE UNIT 3 N- C 9

Report No.: R0-287/76-9 e . , . . ,. 17 Report Date: July 27, 1976 Occurrence Date: July 13, 1976 Facility: Oconee Unit 3, Seneca, South Carolina Identification of Occurrence: Power increase above power level cutoff during feedwater transient Conditions Prior to Occurrence: Unit at 81 percent full power Description of Occurrence:

On July 13, 1976, Oconee Unit 3 was operating at 81 percent full power until xenon conditions as prescribed by Oconee Technical Specification 3.5.2.5.d could allow operation above the power level cutoff of 82.5 percent full power. During this time a feedwater transient caused a reactor pcwer increase of approximately 3 percent. The resulting power level of 84 percent full power therefore exceeded the power level cutoff limit by approximately 112 percent. The control room operator promptly placed the feedwater controls in manual and decreased the feedwater flow to lower reactor power below the power level cutoff.

Apparent Cause of Occurrence:

This occurrence was apparently caused by a feedwater transient resulting from a spurious 80 percent decrease in feedwater demand for approximately two seconds. This inducedan oscillation in the feedwater system resulting in an increase in feedwater flow and a lowering of the average reactor temperature (Tave). Consequently, reactor power was automatically increased by the Integrated Control System in order to maintain Tave- (

l Analysis of Occurrence: l l

This occurrence resulted in a power level increase above the power level l cutoff for a period of less than a minute. At this time the xenon level was j approaching its equilibrium value and the xenon worth was changing very l slowly with time. This very brief power escalation caused no significant I

xenon perturbation or apparent power peaking. All control systems functioned properly and had the control operator not placed the feedwater control in manual, the ICS would have automatically reduced the power level as required.

It is concluded, therefore, that this incident did not affect the health and safety of the public.

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Corrective Action:

The control operator involved promptly performed the appropriate corrective action by placing the feedwater system in manual control and. reducing reactor power below the power level cutoff limit. This is the first incident of this type and investigation of the Integrated Control System did not determine the cause of the transient. It is considered that no further corrective action is-appropriate.

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