ML19322A881

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Insp Rept 50-269/73-03 on 730304-07.Noncompliance Noted:One Senior Reactor Operator Used for Both Unit 1 & Unit 2 & Daily Recording of Wastewater Collection Basin Ph Factor Not Conducted
ML19322A881
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 03/27/1973
From: Murphy C, Warnick R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML19322A878 List:
References
50-269-73-03, 50-269-73-3, NUDOCS 7911270637
Download: ML19322A881 (16)


See also: IR 05000269/1973003

Text

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UNITED STATES

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ATOMIC ENERGY COMMISSION

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DIRECTORATE OF REGULATCRY OPERATIONS

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RO Inspection Report No. 50-269/73-3

Duke Power Conpany

Licensee:

Power Building

422 South Church Street

28201

Charlotte, North Carolina

Facility Name: Oconee Unit 1

Docket No.:

50-269

License No.:

DPR-38

B2

Category:

Oconee County, South Carolina

Location:

B&W, PWR, 2568 MW(t)

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Type of License:

Type of Inspection: Special, Announced

Dates of Tnspection: March 4-7, 1973

February 3-4 and 7-16,1973

Dates of icevious Inspection:

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Principal Inspector:/R. F. Wabiok,)teactor Inspector

Facilities Test and Startup Branch

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None

Accompsaying Inspectors:

None

Other Accompanying Personnel:

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Datie

C. E. Murphy,(Adi:;tf Chief, Facilities Test and

Reviewed By:

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Startup Branch

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RO Rpt. No. 50-269/73-3

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SUMMARY OF FINDINGS

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1.

Enforcement Action

A.

Violations

Technical Specification 6.1.1.6

1.

the Unit 1 minimum shift staffing require-

It appears-that

ments are being violated in that the assistant control

operator on each shift is also the Unit 2 shift supervisor

and has the Unit 2 people reporting to him while Unit 2 is

engaged in the conduct of the preoperational test program.

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(Details I, paragraph 2)

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2.

Technical Soe'cification 6.1.2.1

.

The Station Review Committee (SRC) failed to review and/or

document their review of an approved, safety-related test

(Details I,

procedure as required by the specification.

paragraph 3)

Nonradiological Environmental fechnical Specification 1.2

3.

DPC failed to sample the caste water collection basin for

13, 1973, as. required by the

pH on February 6 throughIn addition, the waste water collection

specification.

basin was outside the allowable pH range (6.0 to 8.5) on

10, 12, 15, 16, 17, 18, and 19, 19 73.

(Details I,

February

paragraph 4)

Criterion V of Accendiy B ;o 10 CFR 50, " Instructions,

4.

Procedures and Drawinas"

'

Contrary to the requirements of Criterion V which states, in

that activities affecting quality shall be prescribed by

part,

documented instructions, procedures, or drawings of a type

appropriate to the circumstances, the work which lead to

the oil fire of March 6,1973, was not covered by a

(Details I, paragraph 5, and attached

written procedure.

Advance Inspection Information memorandum dated March 12,

1973)

3.

Saferv Items

Noce

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RO Rpt. No. 50-269/73-3

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Licensee Action on Previously Identified Enforcement Matters

II.

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A.

Violations

Design Changes (See RO Inspection Report No. 50-269/73-2,

Summary of Findings)

The operations organization had no documented instructions

or procedures to implement the requirements of the fourth

paragraph of Criterion III, " Design Control," pertaining

to the reviews, approvals, and control of design changes

'

including field changes.

This item was not inspected.

.

B.

Safety Items

None

1

III. New Unresolved Items

73-3/1 Nitrogen In-Line Heater Design Change Documentation

Heaters have been added to the nitrogen supply line

feeding the core flood tanks. The design change

documentation was requested for review. Only certain

engineering calculations have been made available to date.

This item will remain unresolved until sufficient information

is available to determine if the requirements of Criterion

III of Appendix B to 10 CFR 50 have been satisfied and until

Region II has inspected the design change.

(Details I,

paragraph 6)

IV.

Status of Previously Reoorted Unresolved Items

,

70-9/16a.

Axial Power Imbalance (R0 Insoection Recort No.

50-269/70-9, Summary - Outstanding Item 16a)

TP-800/24, " Power Imbalance Detector Correlation,"

determines the relationship between the indicated

out-core and in-core power distributions and it verifies

the adequacy of the imbalance system trip setpoints.

This item is closed.

(Details I, paragraph 3)

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RO Rpt. No. 50-269/73-3

(Also RO Inspection Report No.

71-7/1

Thin Walled Valves

50-269/71-5, Details C.3.)_

The licensee's report on the wall thicknesses of valves

within the reactor coolant system pressure boundary has

been received by Region II and remaining deficiencies

identified.1/ The Region is awaiting action by DPC.

Flowmeter Error Analysis and Tests

71-10/1

IP-800/25, "NSS Heat Balance," verifies the accuracy

of the primary flowmeter by determining reactor coolant

This item

system flow using a secondary heat balance.

remains open until appropriate acceptance criteria are

(Details I,

incorporated into the test procedure.

paragraph 3)

Verification of In-Plant Air Flows _

72-8/4

,.

The licensee has determined that air does not flow from

waste handling areas to the normally noncontaminated areas

This item is closed.

of the auxiliary building.

(Details I, paragraph 7)

72-8/15

Verification of Hood Air Flows

This item is

Hood air flows have been measured.

closed.

(Details I, paragraph 8)

J

Filter Test of Hydrogen Purge Svstem

t

72-8/16

The efficiency of the high efficiency particulate air

filters installed in the hydrogen purge system was

,

This item is close,d.

(REPA)

tested and determined to be 99.98%.

f

(Details I, paragraph 9)

Resolutien of Test Deficiencies

73-1/2

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(Details I, paragraph 10)

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This item remains active.

50-269/73-1, Details VII, paragraph 3.

1/ See 20 Inspection Report No.

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RO Rpt. No. 50-269/73-3

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73-1/4

Preoperational Tests to be Completed Prior to Initial

Criticality

This item remains active since all tests have not yet

been completed.

(Details I, paragraph 11)

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73-1/6

Analysis and Aporoval of Preonerational Test Results

Required Prior to Initial Criticality

.

This item remains active. The reviews have not yet

been completed.

(Details I. paragraph 11)

73-1/7

Emergency Operating Procedures

.

Of the nine emergency conditions remaining to be

co.vered by written procedures, five are now covered

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  • by new approved procedures, two are covered in

previously existing procedures, and two remain to be

written.

(Details I, paragraph 12)

73-1/8

Alarm Procedures

Alarm procedures for all o-fety related systems have

been rewritten. Thess will be approved prior to initial

criticality.

.

V.

Design Changes

None

VI.

Unusual Occurrences

None

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VII. Other Significanc Findings

None

VIII. Management Interview

At the conclusion of the inspection, a management interview was

held on March 7, 1973, with the following DPC representatives

present:

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RO Rpt. No. 50-269/73-3

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J. E. Smith - Plant Superintendent

J. W. Hampton - Assistant Plant Superintendent

K. S. Canady - Nuclear Engineer

D. C. Holt - Assistant Nuclear Test Engineer

R. M. Koehler - Technical Support Engineer

,

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L. E. Summerlin - Staff Engineer

The following items were discussed:

A.

Enforcement Action

The status of enforcement action, as described in the summary

of findings, was discussed with the plant superintendent during

the management interview and by telephone following the

inspection. The reportability of the oil fire was also

discuss ed.

B.

Design Chance on Nitrogen In-Line Heaters

The inspector stated that this would be carried as an unresolved

item until the design change documentation including design

description, evaluation, reviews, and approvals are made

available fc- kegion II to review, and the review is completc.d.

(Details I, paragraph 6)

C.

Previous 1v Reported Unresolved Items

,

The status of previously reported unresolved items, as

described in the summary of findings, was discussed.

D.

Power Ascension Test Procedures

The inspector stated that he had reviewed 17 out of 31 power

ascension test procedures, that one more would be reviewed in

,

the regional office, and that Region II comments had been

discussed with station management. The inspector repeated

each of the comments and his understanding of DPC's position

on each comment. The inspector was informed that his

understandings were correct.

(Details I, paragraph 3)

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R0 Report No. 50-269/73-3

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DETAILS I

Prepared By: N

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Date

.R. F. Wkrdicy7 Riactor

Inspector, Facilities

Test and Startup Branch

Dates of Inspection: Marc

4-7, 1973

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Reviewed By:

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C. E. Murpdyy/Acjtng

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Chief, Facilities Test

and Startup Branch

.

1.

Individuals Contacted

Duke Power Cocoany (DPC)

J. E. Smith - Plant Superintendent

J. W. Hampton - Assistant Plant Superintendent

M. D. McIntosh - Operating Engineer

R. M. Koehler - Technical Support Engineer

L. E. Su==erlin - Staff Engineer

R. L. Wilson - Performance Engineer

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G. W. Cage - Assistant Operating Engineer

L. E. Schmidt - Assistant Operating Engineer

R. O. Frink - Assistant Plant Engineer

C. L. Thames - Health Physics Supervisor

O. S. Bradham - Instrument and Control Engineer

2.

Shift, Staffing

that Unit 1

Technical Specification 6.1.1.6 states, in part,

minimam si.ift staffing for other than cold shutdown will be

,

in accordance to Table 6.1.1 and this mini =um operating staff

shall be permitted to assist in the prelicensing activity of

Units 2 and 3 only to the extent that it does not affect their

full availability for Unit 1 operation.

In addition, Table 6.1-1

specifies one shif t supervisor with a senior operator (SRO) license,

.

one con' trol operator with at least a reactor operator (RO) license,

one assistemt control operator with at least an RO license, and

two utility operators.

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R0 Rpt. No. 50-269/73-3

The inspector learned that the~ assistant control operator on each cf

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2 and

the four rotating shifts was also the shift supervisor for Unit

The inspector was assured by DPC

had Unit 2 people reporting to him.

management that the personnel with Unit 1 primary assignments had been

instructed and in fact were involved in Unit 2 prelicensing activities

only to the extent that it does not affect their full availability for

Despite these reassurances, it appears that the Unit 1 shift

staffing requirements are being violated in that the shared responsibilities

Unit 1.

are not of a minor nature.

3.

Power Ascension Test Procedures

The licensee's power ascension test program is described in 31 test

The inspector reviewed TP-800/23, " Controlling Procedure

procedures.

for Power Escalation Sequence," and 17 other power ascension testh

.The contents of the procedures were compared with t e

procedures.

Technical Specifications, and other applicable documentation.

Although TP-800/5, " Reactivity Coef ficients at Power," had been

approved by the Station Review Comnittee (SRC), the minutes of the

SRC meeting in which the test was discussed and approved were not

This appears to be contrary to the requirements of Technical

available.

Specification 6.1.2.1, " Station Review Committee," which states that

1

the SRC will review all proposed tcsts that af fect nuclear safety and

that ninutes of the SRC meetings cf.331 be maintained.

The inspector summarized his comments of the reviewed tests and discussed

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them with the plant superintendenc. The inspector's cccments and the

licensee's response are is follows :

4

In TP-800/23, the reactor protective system overpower trip setting

of 50% at the 15% of full pcwec

.'.s higher than the FSAR implies it

a.

The FSAR states en page 13-8, "The reactor protective

should be.

system power level trip point ~111 initially be set at a low value,

At 40%

and raised as the power. escalation program progresses."

of full power, thE trip setting specified in TP-800/23 is 50%.

The trip setting while at the 15% power level should be more

conservative.

The licensee agreed to set the trips more conservatively at 15%

power, but had not decided on the exact setting.

This will be reported in the next inspection,

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RO Rpt. No. 50-269/73-3

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The acceptance criteria stated in the abstract of TP-800/23 in the

b.

The licensee

FSAR have not been included in the Procedure TP-800/23.

stated they would be included in the test acceptance criteria.

The abstract for TP-800/3, " Biological Shield Survey," in the FSAR

s

talks about neutron ceasurements but no neutron surveys are required

c.

by Procedure TP-800/3.

The licensee stated that they intend to make neutron surveys at each

He stated that the test data sheet requires bcth

power plateau.

neutron and gamma readings to be documented,

Although the reactor vendor commented on the power ascension tes*

d.

procedures, certain applicable B&W ccm=ents were not incorporated

into IP-800/5.

,

The licensee agreed to re-review B&W comments on pcwer ascension

tests to ensure that all applicable comments were incorporated into

the test procedures.

sts do not contain suf ficient instructions for reactor

e.

Cev

For example:

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TP-800/4, "Latural Circulation Test" - This procedure does e.o,t

discuss reactor trip, nor expected reactivity changes, nor operator

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actions concerning control rods and boron concentration.

TP-800/5 - Step 12.1.7 does not tell the. operator what to do with

rods, boron, or power level.

TP-800/13, " Unit Loss of Electrical Load" - This procedure assumes

No

integrated control system (ICS) operation will be smooth.

reference is made to possible proble=s or to operator actions

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concerning reactor control, rods, or boro'n.

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The licensee agreed to re-review all power ascension test procedures

to ensure they contain sufficient instructions for personnel

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operating the reactor.

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Step 6.3 of TP-800/5 states as a limit and precaution that the

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boron concentration in the reactor coolant system shall be within

What

+10 ppm of the concentration in the letdown storage tank.

actions are required if +10 ppm is exceeded?

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R0 Rpt. No. 50-269/73-3

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The licensee stated that this limit applied to equilibrium operation

only and that the step would be clarified.

In TP-800/10, " Xenon Reactivity Worth and Rapid Depletion Test,"

g.

steps 12.1.5, 12.1.7, 12.2.5, 12.2.7, 12.3.5, and 12.3.7 need more

information concerning how reactivity will be plotted and the

xenon peaks determined. Step 12.3.3 should state the maximum

allowable percent power change per minute that power may be reduced.

The licensee agreed to add needed instructions.

h.

In TP-800/5, "NSS Heat Balance," no acceptance criteria is listed

for the reactor coolant system flow determined by a heat balance

of the secondary coolant systems.

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A DPC management representative stated that the desired correlation

between flowmeter instrumentation and the indicated flow based on

the secondary heat balance would be specified in the procedure.

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The inspector reviewed the following power ascension test procedures,

well over 50% of the category I tests:

TP-800/23, " Centro 111ng Procedure for Power Escalatien Sequenre"

TP-800/2, " Nuclear Instrumentation Calibration at Power"

.c

TP-800/3, " Biological Shield Survey"

TP-800/4, " Natural Circulation Test"

TP-800/5, " Reactivity Coefficients at Power"

TP-800/8, " Integrated Control System Tuning"

TP-800/10, " Xenon Reactivity Worth and Rapid 'Jepletion Test"

TP-800/11, " Core Power Distribution"

TP-800/13 " Unit Loss of Electrical Load"

TP-800/14, " Turbine and Reactor / Turbine Trip Test"

TP-800/24, " Power Imbalance Detector Correlation"

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TP-800/23, "NSS Heat Balance"

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TP-800/29, " Unit Load Transient Test"

TP-800/30, " Loss of Control Room"

TP-800/31, "Psuedo Control Rod Ejection Test"

TP-800/32, " Loss of Offsite Power"

TP-800/33, " Dropped Control Rod Test"

TP-710/4, " Initial Radiochemistry"

.

The inspector determined that the power ascension tests and the

power levels at which the various tests will be conducted are in

agreement with the AEC's Guide for the Planning of Initial

Startup Programs.

1/

TP-800/24 satisfied the previously identified unresolved item"

in that it does determine the relatiunship between the indicated

out-core and in-core power distributions and it verified the adequacy

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of the imbalance system trip setpoints. This item is now closed.

TP-8n0/25 satisfies the previously identified unresolved item-2/

in th:t it does verify the accuracy of the primary flowmeter by

determining reactor coolant system flow using a secondary heat

balance. This previously reported unresolved item will be closed

as soon as appropriate acceptance criteria are incorporated into the

test procedure.

4.

Chemical Discharge Limits

Specificacion 1.2 of the Nonradiological Environmental Specifications

requires among other things that all water discharged from the waste water

collection' basin shall have a pH between 6.0 and 8.5 and that the

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pH anu apa.cific conductance of the waste water collection basin shall ,

be determined and recorded daily,

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On February 16, the plant superintendent informed the inspector by phone

that the above requirenents had inadvertently been violated. The

.

inspector received the following details of the violations while at

the site'.

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jf See R0 Inspection Report No. 50-269/70-9, Summary - Outstanding Item 16a.

2/ See RO Inspection Report No. 50-269/71-10,Section II, paragraph 4.

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The first sample of the waste water collection pond, taken on February 10,

some four days after the operating license was issued, indicated the pH

was 8.9.

The next sample, taken on February 12, indicated the -9 was

9.2.

The basin was full, so additional holdup was not possible. The

basin is normally full and continuously overflowing.

Actions to correct the high pH were taken on February 14.

On February 15,

the pH was 5.8 and on February 16, the pH was 4.2.

About the same time that action was taken to correct the low pH, other

high pH water was added to the basin from a draining operation at the

station and again the pH overshot the limit. On February 17, the pH

was 9.3 and it decreased to 9.0 by February 19.

On February 19, twenty gallons of 96% sulfuric acid was' added to the

basin. The sample on February 20 was 6.60, within the requirements

of the Technical Specifications, and subsequent results have also

been within l'imits.

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The licensee informed the inspector that during the time the waste

water collection basin was outside the limits of the specification,

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samples were taken of the yard drain (which includes the overflow

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from waste water collection basin as well as other area drains) and

at all times during the time that the vaete water collection basin

was outside the pH limits, the yard drain discharge to the environment

(Lake Hartwell) was within the pH l'mits.

The SRC has reviewed this violation'of Technical Specifications and has

recommended that the waste water collection basin be enlarged to provide

a longer holdup time and a larger quantity of dilution water, and that

provisions be included so that there are three distinct volumes avail-

able for holdup. They have also recommended a change to the require-

ments of the Technical Specificativas to make the limit apply to the

water being discharged to the environment.

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5.

Oil Fire

.

In addition to the information contained in the attached, Advance

Inspection Information memorandum dated March 12, 1973, the inspector

was informed on March 9 that both the upper and lower motor bearings

were undamaged and that both the a.c. and d.c. oil lift systems were in

service. The licensee was still engaged in determining the extent of

the damage, but is proceeding with cleanup of affected areas.

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Design Change - Nitrogen In-Line Heaters

.

During the January inspection, DPC was requested to make the design

change documentation, for the nitrogen in-line heaters, available

for the RO inspector's review.

During February,' DPC made engineering

calculations available but not prints and evidence of engineering

reviews and approvals connensurate with those received by the original

I

design as required by Criterion III of Appendix B to 10 CFR 50.

This will remain an unresolved item until sufficient information is

available to determine if the requirements of Criterion III have been

met, and until Region II has inspected the design change.

2/

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7.

Verification of In-Plant Air Flows

)

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On February 27, 1973, representatives of DPC and the ventilation contrac-

tor, Gamewell Mechanical, Inc., measured air flows in the auxiliary

building in doorways between waste handling areas and normally noncon-

taminated areas. They determined that in no case does air flow from

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waste handling areas to clean areas.

,

The inspector reviewed the summary of the results of the air flow tests

and then personally *.erified, with a tissue test, that positive air.

flow does exist frem clean to contaminated areas.

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This previously reported unresolved item is closed.

3/

8.

Verification of Air Flow in Laboratory Hoods

On February 27, 1973, representatives of DPC and the ventilation contrac-

tor, Gamewell Mechanical, Inc., measured the air flow in each laboratory

hood.' The air flows in the five hoods ranged from 591 cfm to 847 cfm.

This previously reported unresolved item is closed.

,

1/ See RO Report No. 50-269/73-1, Summary of Details, paragraph V.b.

2/ See RO Report No. 50-269/73-1, Details V, paragraph 5.

3/ See RO Report No. 50-269/73-1, Details V, paragraph 11.

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9.

Filter Testing of Hydrogen Purne System

The inspector reviewed the completed test IP-115/1, " Air Filter Tests

High Efficiency Particulate Air Filters," and verified the results of

the test indicate that the high efficiency particulate air (HEPA)

filters in the gaseous waste disposal (GWD) system are 99.997%

efficient and the HEPA filters in the hydrogen purge system are

99.98% effecient.

The test summary stated the results of the control room ventilation

HEPA filters. The inspector did not verify efficiency calculations;

however, the results met the test acceptance criteria and the requirements

of the Technical Specifications.

This previously reported unresolved item is now closed.

10. Resolution of Preoperational Test Deficiencies

The inspector requested that DPC prepare a su= mary showing the resolution

of the deficiencies described in the su= nary of the results of TP-600/1,

,

" Controlling Procedure for Hot Functional Testing."

A representative of DPC indicated this would be done. This understanding

was ccnfirmed in the management interview.

2/

11. Review of Completed Preocerational Tests

The inspector determined the following tests had been completed,

the results evaluated, reviewed, and approved by DPC:

TP-125/1, " Strong Motion Recorder Calibration"

T?-125/2,

" Peak Recording Accelerometer Calibration"

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TP-150/t0, " Reactor Building Cleaning"

TP-161/3, " Reactor Building Purge System Functional and Operational Test"

TP-161/4A, " Hydrogen Purge System Leak Test".

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TP-170/1, " Auxiliary Building Vent Fans Valve Controls Electrical Test"

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1/ See RO Report No. 50-269/72-1, Details V, paragraph 12.

2/ See R0 Report No. 50-269/73-1, Details II, paragraph 2.b.

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TP-203/6A, "500 PSIG Low Pressure Injection Engineered Safeguard Test"

TP-234/10, " Quench Tank Operational Test"

TP-234/3,

Gaseous Waste Disposal System Waste Gas Decay Tank Discharge

"

Flow"

TP-270/32, " Main Steam Stop Valve Leak Rate Test"

TP-360/1B, " Process Radiation Monitoring System 1 RIA-44 Vent Iodine

Monitor"

TP-360/8, " Process Radiation Monitoring System 12 Point LPSW Monitor,

RIA-31"

,

TP-360/10, " Process Radiation Monitoring System 1 RIA-35 LPSW Discharge

Manitor"

.

TP-600/28, "2iping System Vibration Test"

The following procedures remain to be completed and/or the results

evaluated, reviewed and approved prior to initial approach to criticality.

This was discussed at the management interview.

TP-110/2,

" Penetration Room Flow,; Pressure Drop, and Filter Test"

'"

TP-115/5, "HEPA Filter Inspection Test"

TP-161/4,

" Hydrogen Purge Test"

TP-203/5, " Low Pressure Injection Functional Test"

TP-230/8B, " Coolant Treatment Evap<.rator Functional Test"

TP-230/8C, " Waste Evaporator Fune*.icnal Test"

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TP-302/2, "Incore Instrumentation Electrical Test"

TP-330/1, " Integrated CRD System Test"

TP-600/10, " Reactor Coolant System Hot Leakage Test"

.

.-m

4

.

(..

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RO Rpt. No. 50-269/73-3

1-10

,1_/

12. Emergency Overating Procedures

Since the last inspection, DPC has prepared the following approved

emergency procedures:

,

EP-1800/21, Inoperable Centrol Rods

EP-1800/22, Loss of Flux Indication

EP-1800/23, Loss of Containment Integrity

EP-1800/24, Abnormal Release of Radioactivity

EP-1800/14, Loss of Steam Generator Feedwater

These procedures were reviewed by the inspector and compar'ed with the

requirements of the Technical Specifications. The inspector determined

that the emergency procedures do implement the actions required by

the Technical Specifications.

High activity in the re, actor ccolant system has been covered in alarm

procedure 1708/21, " Process Monitor Radiation High." This was

reviewed by the inspector.

Malfunction of the ptassurizer relief valves is covered by the existing

procedure EP-1800/4, " Loss of Reactor Coolant."

l

Acts of nature (other than earthquake) still remains to be written.

13. Seismic Detectors

Oconee Unit I has nine seismic detectors. The two strong motion

,

recorders have a trip sensitivity of .01g and display a visual

'

signal at the detectors when tripped. The film 'must be processed

.

and evaluated by the detector vendor before the intensity of the

earthquake can be determined. One seismic detector will alarm

in the control room at .05g.

Six peak recording accelerometers

will record acceleration up to .25g.

The inspector was informed

that the recordings can be optically read by DPC personnel at the

site and the intensity of the earthquake determined. Other

information on the seismic detectors was reported previously.2j

,,

1

1/ See R0 Report No9 50-269/73-1, Details III, paragraph 2.a., and

50-269/73-2, Details I, paragraph 7.

,

,

2_/ See R0 Report No. 50-269/72-10, Details I, paragraph 4'.

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