ML19320D774

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IE Insp Repts 50-313/80-07 & 50-368/80-07 on 800422-0521. Noncompliance Noted:Incomplete Written Procedures, Insufficient Adherence to Procedures & Poor Housekeeping Measures
ML19320D774
Person / Time
Site: Arkansas Nuclear  
Issue date: 06/04/1980
From: Callahan L, Johnson W, Westerman T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML19320D759 List:
References
50-313-80-07, 50-313-80-7, 50-368-80-07, 50-368-80-7, NUDOCS 8007220197
Download: ML19320D774 (18)


See also: IR 05000313/1980007

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U. S. NUCLEAR REGULATORY COMMISSION

OF W E OF INSPECTION AND ENFORCEMENT

REGION IV

Report No. 50-313/80-07

License No. DPR-51

50-368/80-07

NPF-6

Licensee: Arkansas Power and Light Company

P. O. Box 551

Little Rock, Arkansas

72203

Facility Name: Arkansas Nuclear One (ANO), Units 1 and 2

Inspection at: ANO Site, Russellville, Arkansas

Inspection Conducted: April 22 - May 21, 1980

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Inspectors:

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W. D. Johnson, SenTor Resident Inspector

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/d L. J. Callan, Resident Inspector

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[h S. Dearf, Reactor Inspector

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Approved:

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T. F. Westerman, Chief, Reactor Projects Section

Date

Inspection Summary

Inspection conducted during period of April 22 - May 21, 1980

(Report No. 50-313/80-07)

Areas Inspected: Routine, announced inspection including Confirmatory

Order Follow-up, Follow-up on IE Bulletin 79-27, Follow-up on Open Item,

Operational Safety Verification, and Reactor Coolant Pump Seal Failure.

The

inspection involved 142 inspector-hours on-site by three NRC inspectors.

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8007220199

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Results: Within the five areas inspected, no items of noncompliance were

identified.

Inspection conducted during period of April 22 - May 21, 1980

(Report No. 50-368/80-07)

Areas Inspected: Routine, announced inspection including Follow-up on

IE Bulletin 79-27, Licensee Review of Power Ascession Test Results, Follow-up

on Licensee Event Reports, Inspector Review of Power Ascension Test Data,

Follow-up on Open Item, Isothermal Temperature and Power Coefficients of

Reactivity, Core Power Distribution Operational Safety Verification, and

Surveillance Observation. The inspection involved 126 inspector-hours

on-site by three NRC inspectors.

Results: Within the nine areas inspected, one item of noncompliance was

identified (infraction - adherence to procedure, paragraph 12).

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DETAILS SECTION

1.

Persons Contacted

J. P. O'Hanlon, ANO General Manager

G. H. Miller, Engineering & Technical Support Manager

B. A. Baker, Operations Superintendent

T. N. Cogburn, Plant Analysis Superintendent

E. C. Ewing, Plant Engineering Superintendent

P. Jones, Maintenance Superintendent

F. Foster, Operations and Maintenance Manager

J. McWilliams, Assistant Operations Superintendent

J. Albers, Planning and Scheduling Supervisor

D. D. Snellings, Technical Analysis Superintendent

L. Schempp, Manager of Nuclear Quality Control

M. Bishop, Acting Plant Administrative Manager

R. Tucker, Assistant Maintenance Superintendent

L. Bell, Assistant Operations Superintendent

G. Fiser, Radiochemistry Supervisor

V. Pettus, Assistant Maintenance Superintendent

I. Mosquito, Health Physics Planning & Scheduling Coordinator

D. Wagner, Assistant HP Sepervisor

G. Halverson, Assistant HP Supervisor

J. Lamb, Safety and Fire Protection Coordinator

H. Hollis, Security Coordinator

D. Lomax, Nuclear Engineer

C. Shively, Plant Performance Supervisor

T. Green, Training Coordinator

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D. Glenn, Health Physics Supervisor

G. Fiser, Radiochemistry Supervisor

P. Rogers, Nuclear Support Supervisor

R. Turner, Electrical Engineering Supervisor

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M. Stroud, Engineer

D. Trimble, Manager of Licensing

L. Humphrey, Manager of Quality Assurance

G. Charles, Secretary, Safety Review Committee

D. Sikes, Director, Generation Operations

The inspectors also contacted other plant personnel, including operators,

technicians and administrative personnel.

2.

Follow-up on Previously Identified Item (Units 1 and 2)

(Closed) Open item 313/79-21-02; 368/79-20-01:

Overall review of the

QA Program effectiveness,

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The licensee has issued QA Administrative Procedure QAA-16 entitled

"QA Program Report." This procedure initiates a system for evaluating

the effectiveness of the QA Program.

3.

Inspector Review of Test Data (Unit 2)

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During this inspection, the inspector reviewed certain tests performed

at the 100% power level plateau.

Items considered in this review

included resolution of test deficiencies, licensee evaluation of

test results, acceptability of test data and administrative control

of testing.

Tests reviewed during this inspection included the following:

Test

Title

2.800.01 Appendix L

Process Variable

Intercomparison

2.800.01 Appendix M

Chemistry and Radiochemistry

Test

2.800.01 Appendix P

Core Performance Record

2.800.01 Appendix RR

Turbine Trip

2.800.09

Vibration and Loose Parts

Monitoring

2.800.01 Appendix U

Unit Load Transient Test

Appendix L was performed in January 1980, to compare process instru-

mentation readings obtained from the plaat computer, plant protective

system, the core protection calculators and console meters to verify proper

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agreement between systems. The inspector reviewed the results of this

test and identified no discrepancies which had not been identified and

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resolved by the licensee.

Appendix M was performed in February 1980, at 100% power.

This test

involves the recording of RCS chemistry and radiochemistry data and

comparing results with the process radiation monitor for correlation. The

results of this test did not meet the acceptance criteria.

The

resolution of this is an open item.

(368/80-07-02)

Appendix P was performed at 100% power in January 1980.

The test included

measurement of core radial power distribution and axial power distri-

bution.

Test' data was obtained in an INCA verification file which was

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transmitted to Combustion Engineering for use in the CECOR code to

obtain the power distributions. These measured distributions were then

compared to the predicated valves. The inspector reviewed the

test results and identified no deficiencies.

Appendix RR was performed on January 29, 1980, to demonstrate the

total system performance by the primary and secondary systems in

response to a full load turbine trip.

The inspector witnessed this

test and reported test results in Inspection Report 368/80-03.

The

inspector reviewed the results of this test and identified no

deficiencies which had not been identified and resolved by the

licensee.

Test Procedure 2.800.09 was performed in January 1980, to provide

baseline data ' r core vibration and loose parts monitoring.

The

inspector reviewed the results of this test and identified no

deficiencies.

Appendix U was performed in January-March,1980, to demonstrate

satisfactory operation of plant control systems in the automatic

mode to maintain plant parameters within acceptable limits

during steady state power operations and during transient

conditions.

The inspector revieved the results of this test and

identified no deficiencies.

4.

Licensee Review of Power Ascension Test Results (Unit 2)

The inspector attended a meeting of the Plant Safety Committee on

May 20, 1980. At this meeting, the status of the testing program was

reviewed.

Several tests have not yet been performed; review and analysis

of the data for several tests has not been ompleted; and several tests

need to be repeated.

The inspector will follow the licensee's progress

in completing these items.

5.

Isothermal Temp Coefficient of Reactivity Measurement and Power

Coefficient of Reactivity (Unit 2)

The purpose of this inspection effort was to verify that the measurements

of the Isothermal Temperature Coefficient of Reactivity Measurement

and Power Coefficient of Reactivity were technically correct and

performed in accordance with NRC and licensee requirements.

The

inspector reviewed the following test procedures and randomly sampled

data analysis for accuracy.

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Test Procedure

2.800.01 Appendix R

Variable T average

Revision 2

20% Poser Level 2/21/79 - 2/25/79

2.800.01 Appendix R

Variable T average

Revision 2

50% Power Level 7/29/79 - 8/8/79

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No items of noncompliance or deviations were identified.

6.

Surveillance of Core Power Distribution Limits (Unit 2)

The purpose of this inspection effort was to verify that the reactor

is being operated within the licensed power distribution limits. The

inspector performed a partial review of the following procedures.

Test Procedure

Completed

Core Power Distribution, No. 2304.48, Revision 1

6/12/79

Core Power Distribution, No. 2304.48, Revision 1

6/30/79

Core Power Distribution, No. 2304.48, Revision 2

8/10/79

This inspection effort did not identify any items of noncompliance or

deviations in the areas reviewed. A future inspection will again

examine this area so as to complete the stated inspection purpose.

7.

Licensee Event Reports (LER's) (Unit 2)

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The inspector reviewed certain LER's to verify the following items:

Appropriate corrective action had been taken.

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The event did not involve operation of the facility in a

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manner which constituted ar unreviewed safety question as

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defined in 10 C7R 50.59(a)(2).

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The event did not involve continued operations in violation

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of regulatory requirements or license conditions.

Reporting requirements were met.

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The LER's included in this review are listed below:

79-21/03L-0

79-22/01T-0

79-23/03L-0

79-24/03L-0

79-27/03L-0

79-28/03L-0

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79-29/03L-0

79-30/03L-0

79-31/03L-0

79-32/03L-0

79-33/01T-0

79-37/03L-1

79-38/03L-0

79-39/03X-1

79-41/03L-0

79-42/03L-0

79-44/03L-0

79-45/03L-0

79-46/03L-0

79-47/04L-0

79-48/03L-0

79-49/03L-0

79-51/03L-0

79-52/03L-0

79-55/03L-0

79-56/03L-0

79-57/04L-0

79-58/03L-0

79-58/03X-1

79-59/03L-0

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79-60/03L-0

79-61/03L-0

79-62/03L-0

79-63/03L-0

79-64/03L-b

79-67/04L-0

79-68/03L-0

79-69/03L-0

79-70/03L-0

79-71/03L-0

79-72/03L-0

79-73/03L-0

79-74/03L-0

79-75/03L-0

79-75/03X-1

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79-76/03L-0

79-77/03L-0

79-78/03L-0

79-79/03L-0

79-80/03L-0

79-81/03L-0

79-82/03L-0

79-83/03L-0

79-84/03L-0

79-84/03X-1

79-85/03L-0

79-86/03L-0

79-87/03L-0

79-87/03X-1

79-88/03L-0

79-89/03L-0

79-90/03L-0

79-91/03L-0

79-92/03L-0

79-93/99X-0

79-94/03L-0

79-95/03L-0

79-96/03L-0

79-97/03L-0

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79-98/03L-0

79-99/03L-0

79-101/03L-0

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79-102/03L-0

79-102/03X-1

79-103/03L-0

79-104/03L-0

80-18/03L-0

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LER 368/80-18/03L-0 reported a loss of suction to the

Emergency Feedwater (EFW) pumps on April 7, 1980. The loss of

suction occurred about 15 minutes following a reactor trip from 98%

power caused by a loss of offsite power. Tb suction of the EFW

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pumps had been aligned to the Condensate Starage Tank (CST) and to

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the Startup and Blowdown Demineralizer effluent in parallel.

Prompt

operator action was taken to isolate the EFW pump suction from the Startup

and Blowdown Demineralizer and to vent the EFW pumps.

EFW flow was

reestablished within one minute.

Licensee investigation revealed that the

EFW pump suction loss was caused by flashing in the main feedwater train

forcing hot water through the Startup and Blowdown Demineralizers to the

EFW pump suction where it flashed to steam.

The steam caused

cavitation of the EFW pumps, and the pressure in the EFW suction

header prevented flow from the CST. Action to prevent recurrence

included revising the EFW system. operating procedure and the plant

startup prccedure to require shutting the EFW suction valve from

the startup and Blowdown Demineralizers during plant startup at about

5% full power after the Steam Generator feedwater source has been shifted

to a main feedwater pump.

In addition, the EFW suction valve from

the Startup and Blowdown Demineralizers will be verfied closed once

per shift during Mode 1 operation. Members of the NRC staff in Headquarters

are reviewing this event to determine whether it could occur at other

plants and to determine whether the licensee's action to prevent

recurrence is sufficient.

8.

Confirmatory Order Follow-up (Unit 1)

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a.

On April 22, 1980, the NRC Office of Nuclear Reactor Regulation

issued a Confirmatory Order for Arkansas Nuclear One, Unit No. 1.

This order confirmed licensee commitments to take certain

actions as a result of experience gained from the Crystal River,

Unit No. 3 incident of February 26, 1980, in which a non-nuclear

instrumentation power loss resulted in a series of unexpected

events.

These actions were intended to reduce the probability of a

similar future power loss causing unexpected plant responses and

allow the plant operators to better cope with losses of instrumentation

and control functions.

b.

Part II of the above order specified required actions and referenced

licensee commitments. The inspector's review of these items is

described below:

(1) Required Action No. 1

Actions which will allow the operator to cope with various

combinations of loss of instruction and control functions.

This includes changes in (A) equipment and control systems

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to give clear indications of functions which are lost or

unreliable; (B) procedures and traiaing to assure positive and

safe manual response by the operator in the event that competent

instruments are unavailable.

(a) The licensee has performed design change DCP 80-1027 in

response to this item.

This change provides an alternate

120 volt power supply to the Non-Nuclear Instrumentation

(NNI) cabinets.

Automatic transfer switches were installed

which will transfer to the emergency power supply when the

normal source voltage fails and will transfer back to normal

source ter. minutes after normal source restoration.

The

inspector reviewed this DCP, which was completed under Job

Order 1-9079B-80-4 on April 28, 1980. The inspector checked

the modified wiring against drawing E-547, Sheet 3 of 3,

Revision 8-2, entitled " Connection Diagram-Plant Auxiliary

System Control Power, Y-C48."

Two jumpers in cabinet C-48

on terminal board P-TBY were not in accordance with the

drawing.

The licensee determined that the drawing was in

error and processed a field change to correct the drawing.

The licensee performed Work Plan 1407.01, " Checkout of NNI

Power System Modifications (DCP 80-1027)" on April 29, 1980.

The inspector witnessed the portion of this test which tested

the modifications for NNI "Y."

The test was properly conducted and the modified system

performed in accordance with design specifications.

(b) The licensee has issued Revision 6 to procedure 1203.12,

"Annuniciator Corrective Action." This revision adds

a section addressing the various NNI trouble alarms

annunciated on panel K14. The procedure lists the

causes and required action for the alarms, lists which

controls or indications are lost when various failures

occur, and includes variations in lost functions based

on Control Room selector switch positions. The

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Assistant Operations Superintendent has conducted

informal training sessions on this revised procedure

with operators, but at the end of this inspection, the

licensee had not yet conducted any formal training sessions

on this revised procedure.

(Open Item 313/80-07-01)

(2) Required Action No. 2

Determination of the effects of various combinations of loss of

instrumentation and control functions by design review

analysis and verification by test.

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The licensee's letter of April 18, 1980, to the Commission

provided the results of the design review analysis of the

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effects of the failure of various power supplies to the Non-

Nuclear Instrumentation (NNI) system. The inspector witnessed

the performance of Work Plan 1409.14 on May 4, 1980.

This work plan determined the available critical NNI under

conditions of loss of power to the NNI cabinets.

At the

end of this inspection period, the licensee had identified

one condition requiring correct action.

DCP 80-D-1048,

entitled " Modify A Steam Generator Startup Level Buffer Power

to NNI Y," was completed on May 20, 1980.

This design change

provides power for the A Steam Generator startup level buffer

to computer point P-003 from NNI Y in order to make A Steam

Generator startup level available on computer point P-003 if 24

volt DC Power is lost in NNI X.

The inspector will review the

licensee's written evaluation of the above test when it is

available (0 pen Item 313/80-07-02)

(3) Required Action No. 3

Correction of electrical deficiencies which may allow the

power operated relief valve and pressurizer spray valve to open

on non-nuclear instrumentation power failures, such as, the

even, which occurred at Crystal River, Unit 3 on February 26,

1980.

The licensee performed two design changes in response to this

item. DCP 80-1030, entitled " Modify NNI Control Circuitry for

Pressurizer Pilot Operated Relief Valve," added auxiliary

relays to detect the loss of the 1 24 volt power supply

and open contacts in the PORV control circuit to prevent

this valve from getting an "open" signal upon loss of NNI

power suppli s.

This DCP was completed under Job Order

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1-7503-80-4 and tested in accordance with Work Plan 1408.07 on

April 22, 1980.

The inspector reviewed the completed DCP,

Job Order and Work Plan. DCP 80-1031, entitled " Add Contacts

to Control Circuit for Pressurizer Spray Valve (CV-1008)," was

performed to minimize the issuance of an "open" command to the

spray valve on loss of 1 24 volt power and issue a "close"

command on loss of 1 24 volt power. This design makes use

of the same auxiliary relays installed in DCP 80-1030.

This

DCP was completed under Job Order 1-7504-80-4 and tested in

accordance with Work Plan 1408.07 on April 22, 1980.

The

inspector reviewed the completed DCP, Job Order and Work

Plan.

9.

IE Bulletin 79-27 (Units 1 and 2)

Part III of the above order discussed IE Bulletin 79-27 and Part IV

required that the licensee provide a written response to IEB 79-27

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for Unit 1 by April 28, 1980. The licensee's response to IEB 79-27

for Unit I was dated April 23, 1980. The inspector has verified the

licensee's responses to items 1 and 2 of IEB 79-27 as described above.

The licensee's response to this bulletin for Unit 2 was dated

Februa ry 28, 1980.

The inspector rev ewed the licensee's

response and had no further questionr

10.

Reactor Coolant Pump Seal Failure (Unit 1)

On May 10, 1980, the seal on the "C" Reactor Coolant Pump (RCP) failed,

allowing excessive reactor coolant leakage to the Containment sump.

The unit was rapidly shut down and cooled down as required by Technical Specification 3.1.6.1.

The cooldown rate was within the limits

of Technical Specification 3.1.2.

An adequate margin to saturation

was maintained throughout the transient and no Technical Specification

Safety Limits for Operation were violated.

The NRC was notified of this

event as required by 10 CFR 50.72.

No measurable releases of radioactive

material to the environment were made as a result of this event on May 10,

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1980.

The inspector observed, in part, the plant cooldown and depressurization

and periodically monitored the plant stack radiation monitor to verify

that no non-routine releases were being made.

Licensee activities with

respect to this incident were observed to be well organized, with manage-

ment involvement, technical support and with a concern for the health and

safety of employees and the public.

About 59,000 gallons of reactor coolant water was spilled to the

Containment sump before the leak was stopped by depressurization and

partial draining of the reactor coolant system.

The inspector

observed, in part, the tranfer of this water to holding tanks in the

Auxiliary Building and its processing and clean-up for subsequent

use in the Borated Water Storage Tank and in the reactor coolant

system.

The inspector, together with other members of the NRC staff, reviewed

the licensee's analysis of the Containment atmosphere and the plans

for filtering and ventilating the Containment atmosphere. The NRC

staff performed independent calculations to verify that the licensee's

planned ventilation of the Containment Building would not result

in release of radioactive material to the environment in quantities or

rates in excess of those allowed by Technical Specification (Appendix B)

2.4.2.

The inspector observed the preparations for and the commencement

of the Containment Building ventilation on May 13, 1980.

The inspector

observed several segments of the release, conducted at hourly intervals

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until May 15, 1980, and confirmed that the pre-release calculations were

conservative and that the release rates were well within the Technical

Specification limits.

At the end of this inspection period, RCP seal replacement work was in

progress.

The inspector identified no items of noncompliance or

deviations related to this incident.

11.

Monthlv Surveillance

aspection (Unit 2)

The inspector witnes: ed the following core physics surveillance tests:

Procedure No.

Title

2103.15

Reactivity Balance Calculation

2302.01

Incore Detector Channel Check

2302.05

Core Power Distribution

2302.16

RCS Calorimetric Flow Rate

Calibration

Included in this inspection were the following items:

A review of each of the surveillance procedures for conformance

a.

to technical specification requirements and verification of

proper licensee review and approval.

b.

Observation of portions of each surveillance test.

A review of the test data for accuracy and completeness.

c.

d.

Verification that test results met technical specification

requirements.

Verification that the test was done by qualified personnel.

e.

f.

Verification that the surveillance schedule for the test

was met.

No items of noncompliance were identified.

12.

Operational Safety Verification (Units 1 and 2)

.The inspectors performed certain activities to ascertain that the

facility is Leing operated safely and in conformance with regulatory

requirements and that the licensee's management control system is

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effectively discharging its responsibilities for continued safe

operation.

The inspectors activities and findings in this regard are

described in the following paragraphs.

A.

Certain inspection activities were performed frequently (several

times per week).

(1) Control room observations were made which normally included

the following items:

Verification of licensee adherence to selected Limiting

a.

Conditions for Operation (LCO).

b.

Observation of instrumentation and recorder traces for

abnormalities.

Verification of proper control room and shift manning.

c.

d.

Verification of operator adherence to approved operating

procedures.

(2) 3 elected logs and operating records were reviewed to obtain

information on plant operations, detect trends, determine com-

pliance with regulatory requirements and assess the effectiveness

of communications provided by the logs and records.

B.

Certain inspection activities were performed on a weekly basis.

(1) The operability of selected emergency safeguards features

systems was verified by noting valve positions, breaker positions,

instrumentation availability and general condition of major

system components.

Systems selected for review during this

inspection were both trains of Unit 2 Diesel air start system,

Unit 1 Train A of Emergency Feedwater, and both trains of

Unit 2 High Pressure Safety Injection (HPSI) system.

During the inspection of Unit 2 HPSI system on April 29, 1980,

the inspector noted that 2 SI-5091-3, the bypass isolation

valve around the combined HPSI discharge isolation valve

(2CV-5091), was not mentioned 'in the procedure for going into

shutdown cooling mode.

2SI-5091-3 is a normally locked open

valve and must be unlocked and shut if shutdown cooling

is to be effective.

The inspector determined from discussions

with several operators that, although not required by existing

procedures, the valve is, in fact, unlocked and shut when

the HPSI system is lined up for shutdown cooling mode (0 pen

Item 368/80-07-33).

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Additionally, the in -Letor noted that the electrical junction

box cover (2TB903) was missing for HPSI valve 2CV-5076,

the normally shut valve that opens on an ESF signal to allow

HPSI flow to 'D'

reactor coolant loop. Also, the junction

box door on the supply end was open.

This valve had undergone

recent corrective electrical maintenance under job order

2-2012-80 that was documentei complete on April 7, 1980.

The above findings are contrary to licensee procedure 1004.14,

step 4.20, which requires that ". . . any maintenance work

completed requires checkout prior to returning to service .

. .

the cognizant supervisor makes the determination of checkout

requirements .

. the signature of the assigned person of

.

Item 23 (a line item on the job order form) indicates that

the required checkout is complete and the equipment is ready

to be returned to service." This is an apparent item of

noncompliance (368/80-07-01).

(2) The licensee's equipment control was reviewed for proper

implementation of performance of the following inspection

activities:

Review of tag out records to determine that the licensee

a.

has complied with LCO's with respect to removal of

equipment from service.

b.

Independently verifying the proper return to service of

selected safety-related components or systems.

c.

Independent verification of proper conduct of

selected safety-related tagouts currently in effect.

(3) The inspectors conducted tours of accessible areas of the

facility to assess equipment conditions, plant conditions,

radiological controls, security, safety, and adherence to

regulatory requirements.

During these tours, the inspectors

made observations in the following categories:

General plant / equipment conditions including operability

a.

of standby eqaipment.

b.

Maintenance requests had been ir.itiated for equipment

in need of maintenance, and the appropriate priority

had been assigned.

c.

Fire hazards.

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d.

Control of ignition sources and flammable materials.

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e.

Conduct of activities in progress in accordance with the

licensee's addinistrative controls and approved procedures.

f.

Condition of the futerior of selected electrical and

control cabinete.

g.

Physical Security.

The inspector verified that the security plan is being

implemented by observing:

(1) The security organization is properly manned and

that security personnel are capable of performing

their assigned functions.

(2) Protected area barriers are not degraded.

(3) Isolation zones are clear.

(4) Persons and packages are checked prior to entry

into the protected area.

(5) Vehicles are properly authorized, searched, and

escorted or controlled within the protected area.

(6) Persons within the protected area display photo

identification badges.

Persons requiring escort

are properly escorted.

h.

Radiation Protection Controls.

i.

Plant housekeeping - the inspector noted that many

of the locked rooms in the Unit 1 and Unit 2 auxiliary

buildings, such as the Upper and Lower South Piping

Penetration Rooms in the Unit 2 auxiliary building,

exhibits poor cleanliness, especially with respect

to debris remaining from completed maintenance.

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Radioactive waste system.

(4) The inspectors reviewed the licensee's trouble tickets

to verify the operability of this problem identification

system.

(5) The inspectors conducted discussions with operators and

other plant personnel and observed several shift turnovers.

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C.

Certain inspection activities were performed once during this

reporting period.

(1) ESF System Operability Verification.

(2) The inspector verified that a selected portion of containment

isolation lineup was correct.

Containment penetrations inspected

were:

2P-5, 6, 7, 8, 9, 10, 11, 14, 15, 17, 18, 19, 20, 21, 23, 24,

25, 31, 32, 33, 34 (all penetrations listed are in the Upper

South Piping Penetration Room of Unit 2 auxiliary building).

The inspector checked that motor operated valves were not

mechanically blocked and power was available.

The piping

between containment and the isolation valves were visibly

inspected for leakage or leakage paths.

(3) The inspector verified that plant conditions, equipment status

and operating parameter, fulfill the following LCO's.

Unit 1

3.1.2.3 Reactor Heatup and Cooldown Limitations

3.1.2.5 Pressurizer Heatup and Cooldown Limitations

3.1.9.2 Rod Control Operation

3.2.1.2 Boron Injection Flow paths

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Unit 2

3.1.2.2 Boron Injection Flow paths

3.1.2.4 Charging Pumps - Operating

3.1.3.1 CEA Position

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3.1.3.2 CEA Position Indicator Channels

(4) The inspector reviewed the licensee's Jumper and Bypass

logs and no conflicts with Technical Specifications were

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identified.

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(5) Radioactive Waste Handling

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17

The inspector witnessed a radioactive liquid release and

a.

verified the following items:

(1) The release was conducted in accordance with

approved procedures.

(2) The required release approvals were obtained.

(3) The required samples were taken and analyzed.

(4) The effluent release control instrument was

operable and in use during the release.

The inspector also reviewed a sample of the liquid and

gaseous effluent records for March 1980.

b.

The inspector witnessed portions of a compactable trash

processing operation and verified the following items:

(1) Waste products processed complied with shipping

regulations specified in 49 CFR Parts 100-199 as

required by the Department of Transportation.

(2) Tne licensee ensured all waste products compiled

with disposal site acceptance criteria as

established by Chem-Nuclear Systems, Inc.'s,

Barnwell Site Disposal Criteria, effective

December 1, 1979.

The inspector noted that existing licensee approved

written procedures were not sufficiently detailed to

adequately cover solid waste processing and preparation

for shipment.

Licensee represen atives indicated

that new procedures covering solid waste processing are

being written. This item will remain open pending

inspector review of the new procedures (open item

313/80-07-03; 368/80-07-04).

(6) The inspector verified the implementation of the licensee's

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radiation protection controls by:

a.

Observing portions of an area survey performed by health

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physics personnel.

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b.

Examining randomly selected radiation protection

instruments that are in use and ve.ifying operability

and adherence to calibration frequency.

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Verifying by observation and review that the requirements

c.

of one current RWP were being followed.

d.

Verifying compliance with requirements of 10 CFR 20

regarding posting.

Observing that licensee's procedures are Seing followed.

e.

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13.

Exit Interviews

The inspectors met with Mr. J. P. O'Hanlon (Plant General Manager)

and other members of the AP&L staff at the end of various segments

of this inspection. At these meetings, the inspectors summarized the

scope of the inspection and the findings.

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