05000368/LER-1980-034-03, /03L-0:on 800531,during Mode 1 Operation,Leak Developed on Charging Pump B Suction Pipe at Coupling for Capped Test Connection Line.Caused by Vibration.Defective Pipe Spool Piece Will Be Replaced

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/03L-0:on 800531,during Mode 1 Operation,Leak Developed on Charging Pump B Suction Pipe at Coupling for Capped Test Connection Line.Caused by Vibration.Defective Pipe Spool Piece Will Be Replaced
ML19318C381
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 06/26/1980
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19318C375 List:
References
LER-80-034-03L, LER-80-34-3L, NUDOCS 8007010414
Download: ML19318C381 (1)


LER-1980-034, /03L-0:on 800531,during Mode 1 Operation,Leak Developed on Charging Pump B Suction Pipe at Coupling for Capped Test Connection Line.Caused by Vibration.Defective Pipe Spool Piece Will Be Replaced
Event date:
Report date:
3681980034R03 - NRC Website

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~4 R E poi 4 T C.,4 T E HJ EVE NT DESCRIPTION AND FAOBABLE CONSEGUENCES h ITTT] L_During Mode 1 operation, a leak developed or, the "B" Charging Pump suc-1 11,13; I tion pipe at the coupling for 2 CVC-1168 (a capped test connection 1:ne))

FETT1 1 The leak was isolated.

The two remaining charging pumps remained operab]e f ois; i meeting the requirements of T.S.3.1.2.4.

This occurrence is similar to,

Ic io l I LER's_50-368/19-031 and 80-019.

Reportable per T.S. 6.9.1.9(d).

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