ML19318B824
| ML19318B824 | |
| Person / Time | |
|---|---|
| Site: | Perkins, Cherokee |
| Issue date: | 05/13/1980 |
| From: | James O'Reilly NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | Dail L DUKE POWER CO. |
| References | |
| NUDOCS 8006300123 | |
| Download: ML19318B824 (2) | |
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'o UNITED STATES 8
g NUCLEAR REGULATORY COMMISSION o
g a
REGION 11 o
101 MARlETTA ST., N.W., SUITE 3100 g
ATLANTA, GEORGIA 30303 In Reply Refer To:
MAY 131980 RII:JPO sMI).101-9C 150_-493,' 50-488 s
50-489, 50-490 s
Duke Power Company Attn:
L. C. Dail, Vice President Design Engineering P. O. Box 33189 Charlotte, NC 27602 Gentlemen:
The enclosed IE Circular No. 80-11 is forwarded to you for information.
No written response is required. Should you have any questions related to your understanding of the recomme Jations on this matter, please contact this office.
Sincerely,
_ N James P. O'Reilly Director
Enclosures:
1.
IE Circular No. 80-11 2.
List of Recently Issued IE Circulars f
8006300\\1)
MAY 131980 Duka Power Comp:ny.
cc w/ enc 1:
J. T. Moore, Proje'et.lianager Post Office Box 422 Gaffney, South Carolina 29340 l
f e
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SSINS No.: 6830 Accession No.:
UNITED STATES 8002280662 NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT l
WASHINGTON, D.C. 20555 J
May 13, 1980 IE Circular No. 80-11 EMERGENCY DIESEL GENERATOR LUBE OIL COOLER FAILURES s
Description of Circumstances:
Within a two week period (August 27 to September 11, 1979), the tube sheets failed in the lube oil coolers of both emergency diesel generators for Arkansas Nuclear One (ANO) Unic No. 1.
The introduction of water into the diesel lube oil system resulted in trips of both diesels during surveillance testing. The diesels were not considered capable of sustained operation. These events were previously identified to all operating license and construction permit holders by Information Notice 79-23, Emergency Diesel Generator Lube Oil Cooler on September 25, 1979. The emergency diesel generators involved were manufac-tured by the Electro-Motive Division (EMD) of the General Motors Corporation and the failures occurred on engines 71-Al-1117 and 71-Al-1130. The failed lube oil coolers were manufactured by the Young Radiator Company.
An analysis of the failed coolers performed by EMD resulted in the conclusion that the failures were caused by severe corrosion of the solder which sealed the tubes to the tube sheets. The corrosion inhititor in use at ANO was Calgon CS, a borate-nitrite type inhibitor. The manufacturer of this type of inhibitor has recommended the use of hard solder in CS treated sys ems. EMD does not recommend the use of Calgon CS since the puddle solder used in EMD radiators i
and oil coolers is considered to be soft solder of a lead-tin composition.
Recommended Action for Licensees' Consideration:
i Based on the above, it is recommended that licensees:
1 Verify that the corrosion inhibitor used in cooling water systems of the emc. ancy diesel generators is cowpatible with all-materials wetted by the cooling water and the engine manufacturer's specific recommendations.
Also, by means of the engine maintenance history, verify that the system corrosion inhibitor has been properly monitored and maintained at the recommended concentration.
2.
If Item 1 cannot be successfully performed, the affected components should be inspected in accordance with the manufacturer's recommendations.
No written response to this Circular is required.
If you desire additional information regarding this matter, contact the Director of the appropriate NRC Regional Office.
M w
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v e
IE Circular No. 80-11 Enclosure May 13, 1980 RECENTLY ISSUED IE CIRCULARS Circular Subject Date of Issued to No.
Issue 80-11 Emergency Diesel Generator 5/13/80 All' holders of Reactor Lube Oil Cooler Failures OLs'and cps 80-10 Failure to Maintain 4/29/80 All holders of Reactor Environmental Qualification OLs and cps of Equipment 80-09 Problems With Plant Internal 4/28/80 All holders of a power Communications Systems reactor OL or CP 80-08 dWR Technical Specification 4/18/80 All General Electric Inconsistency - RPS Response BWR's holding a power Time reactor OL 80-07 Problems with HPCI Turbine 4/3/80 All holders of a power Oil System reactor OL or CP f.;-06 Control and Accountability 4/14/80 Medical licensees in Systems for Implant Therapy Categories G and G1 Sources 80-05 Emergency Diesel-Generator 4/1/80 All holders of a power Lubricating Oil Addition and reactor OL or CP Onsite Supply 80-04 Securing of Threaded Locking 3/14/80 All holders of a power Devices on Safety-Related reactor OL or CP Equipment 80-03 Protection from Toxic Gas 3/6/80
- All holders of a Hazards power reactor OL 80-02 Nuclear Power Plant Staff 2/1/80 All holders of Reactor Work Hours OLs, including research and test reactors, and cps 80-01 Service Advice for GE 1/17/80 All licensees of Induction Disc Relays nuclear power reactor operating facilities and hol.ders of nuclear power t..ector cps k