ML19318A161

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LER 80-062/03L-0:on 800513,while in Mode 3,2 Pairs of Containment Purge Sys Lines Discovered Open.Caused by Instrument Deficiency Soi 30.2A Allowing Operator to Open Lower Purge Valves.Valves Closed Upon Discovery
ML19318A161
Person / Time
Site: Sequoyah Tennessee Valley Authority icon.png
Issue date: 06/11/1980
From: Record D
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19318A155 List:
References
LER-80-062-03L, LER-80-62-3L, NUDOCS 8006180533
Download: ML19318A161 (2)


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LER SUPPLEMENTAL INFORMATION SQRO-50-327/ 8062 Technical Specification Involved 3.6.1.9 Reported Under Technical Specification 6.9.1.13.b Date of occurrence: 5/13/80 Time of occurrence: 1245 Unit 1 Identification and Description of Occurrence:

Two (2) pairs of containment purge system lines were discovered open. The operator was purging lower containment per SOI-30.2A.

An instruction deficiency allowed the operator to open all lower purge valves.

Conditions Prior to Occurrence:

Unit 1 in Mode 3 RCS SE 3350 F and pressurizer pressure 2235 psig.

Apparent Cause of Occurrence:

Instruction deficiency.

Analysis of Occurrence:

There was no danger to public health or safety.

Corrective Action:

The operator was assigned to make a revision to the instruction to clarify the intent of using only one (1) line for purging.

Failure Data:

N/A i

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