ML19317E497

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Monthly Operating Rept for Aug 1978
ML19317E497
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 09/15/1978
From: Reavis J
DUKE POWER CO.
To:
Shared Package
ML19317E486 List:
References
NUDOCS 7912180737
Download: ML19317E497 (6)


Text

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9 OPERATING DATA REPORT DOCKET NO.

50-270 DATE 9-15-78  !

COMPLETED BY J. A. Reavis TELEPHONE (704) 373-8552 OPERATING STATUS  !

i

1. Unit Name: Oconee Unit 2 jot,ar-to-date & cumulative August, 1978 pa e h-
2. Reporting Period: f o 2568 lated using a weighted aver-
3. Licensed Thermal Power (MWt):
4. Nameplate Rating (Gross MWe): 934 age for maximum dependable  ;
5. Design Electrical Rating (Net MWe): 887 capac1ty.
6. Maximum Dependable Capacity (Gross MWe): 899
7. Maximum Dependable Capacity (Net MWe): 860 S. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Sina Last Report, Give Reasons:

None

9. Power Level To Which Restricted,If Any (Net MWe): None
10. Reasons For Restrictions.If Any:

This Month Yr.-to.Date Cumulative

11. Hours in Reporting Period 744.0 5,831.0 34,872.0
12. Number Of Hours Reactor has Critical 488.8 4,671.0 24,358.5
13. Reactor Reserve Shutdown Hours
14. Hours Generator On-Line 472.6 4,615.9 23,698.9
15. Unit Reserve Shutdown Hours
16. Gross Thermal Energy Generated (MWH) 1,092,429 11,454,374 56,153,249 .
17. Gross Clectrical Energy Generated (MWH) 367.03.0_. 3.911.310 19,114,036
18. Net Elec:rical Energy Generated (MWH) 344,800 3.727,909 18,137,092
19. Unit Service Factor 63.5 79.2 68.0
20. Unit Availability Factor 63.5 79.2 68.0
21. Unit Capacir3 Factor (Using MDC Net) 53.9 74.3 60.0
22. Unit Capacity Factor (Using DER Net) 52.3 72.1 58.6
23. Unit Forced Outage Rate 36.5 20.8 23.1
24. Shutdowns Scheduled Over Next 6 Months (Type. Date.and Duration of Each1:

Refueling November 5, 1978

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units in Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION j

7 912180 73 7,g.7,3

!! Nil SilillDOWNS AND l DWER Rl'litfrilDNS Df HTI'I NO.10-270 UNilNAMI Oconee. Unit 7 DA ll: EL5-38 COMpl l'Il O fly .l. A. Reavis Hl'pOH I AION 111_ Augum_lj78 g,jg,not;I: (704) 373-8552

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28 78-08-11 F --

A --

CB PUMPXX Power reduced to check seal leakage instrumentation on "B" RCP.

29 78-08-11 F 34.70 G 3 IA INSTRU Reactor tripped on flux / flow imbalance when operator took 2B2 RCP off.

NI channels C & D readings were above trip point.

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30 78-08-12 F --

B --

CB PUMPXX lloid for seal Icakage evaluation on 2B1 and 2B2 RCP's.

31 78-08-12 F 227.20 A 1 CB PUMPXX Replace seals on 2B1 and 2B2 RCP's.

32 78-08-22 ,

F --

D --

MA ZZZZZZ lloids at 40%, 45%, and 50% power due to radioactive waste storage space.

33 78-08-24 F --

D --

RC FUELXX Xenon hold at 90% power.

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1 4 1:: 1 ori ed Reason: AlcIlioil: l'shilde G - Imtsui tions S Stliednled A l einipment I ailme (1.xplain) 1 -ht.m ual foi l'ecparation of l>ata ll-blaintenance or les! 2 Mannal Sct.no. I'nley Shecis hn I icemre

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DAIt! 9-15-78 COMPl.I:1If p liy J.._A._Reavia ._ _

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34 78-08-24 F 9.49 G 3 CB VESSEL While placing spray valve (2-RC-1) i in auto the reactor trippe<1 due to low press.in the RC system.

35 78-08-24 F --

D --

RC FUELXX Xenon hold.

36 78-08-25 F --

D --

MA ZZZZZZ lloiding for radioactive waste storage space.

37 78-08-26 F --

D --

RC FUELXX Xenon hold at 90% power.

i l

1 _ _ . _ _ _ _ . . _ ___

l 2 .I 4 12: l' ort ed Itcason : kleihoil: lisinliii (; Imiin, tions S S(lieduled A I quipment l'ailuie (i.xplain) 1. Manual fin Picp. nation of Ipaia ll-Maintenance of Icsi 2 Manual Sciam, linisy Sheels sin 1.icensec C Itefueling 1 Automatic Soam. I: vent Repose ll.I'lO l'ile INilitl (;-

D.Iteputatiny itest eiriion

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4 Oihes (lixplain) oliil I l -Operator 1saining A l.itense 1:xamination I . Adminisisative 5

, (;-Opciational 1:nos (1:xplain) I:shibit i S.nne Sinnce l'8/7/ ) 11 Olher (12x pl.iin )

._ l AVERAGE DAILY UNIT POWER LEVEL -

DOCKET NO. 50-270 ,

UNIT Oconee Unit 2 l DATE 9-15-78 COMPLETED BY J. A. Reavis TELEPHONE (704) 373-8552 I l

l MONTH August, 1978 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net i iMWe-Net I i 825 g_ _

3 823 _

33 819 _

3 19 4 812 -

20 5 813 _

3 6 824 144 23 7 823 386 23 8 822 448 24 9 813 25 317 10 823 698 26 11 166 811 27 12 25 823 23 13 29 822 14 819

,0 15 812

_ 3 16 INSTRUCTIONS On this format, list the average dasy unit power levelin MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.

(4 r77)

PKET NO: 50-270 UNIT: Oconee Unit 2 DATE: 9-15-78

- NARRATIVE S12 DIARY PCNTH: August, 1978 Oconee 2 operated at near rated power until August 8 when .1 5% reduction in power was made for maintenance on the discharge control valve for 2D2 heater drain pump (2HD-234). Near rated power was reached again.on August 9.

On August 11 power was reduced to 75% to check seal leakage instrumentation on the 2B2 RCP. The reactor tripped on flux / flow imbalance when the 2B2 RCP was removed from service because of high readings on NI channels C & D. The unit

, returned to service on August 12 and came to 30% power for the evaluation of 2B1 and 2B2 RCP seal leakage flow. This flow indicated too high for operation and the unit was removed from service for seal replacement.

The unit was on line again on August 22 with a slow power increase due to the availability of radioactive waste storage space.

While in a xenon hold at 90% power on August 24 the reactor tripped on low RCS pressure while placing spray valve (2-RC-1) in auto. The unit returned to service on August 25 and reached near rated power on August 27. This power level was continued the remainder of the month.

+

T $ --en r- y -- P a ~r=- r- p ' - - - t 4 T T T

ML.. GLY Re:u..i.ING INFORMATION REs i.ST

1. Facility name: Oconee Unit 2 .
2. Scheduled next refueling shutdevn: November 5, 1978 .
3. Scheduled restart following refueidng: December 18. 1078 .
4. Will refueling or resumption of operation thereaf ter require a technical I specification change or other license amendment? .

If yes, what will these be?

Amendment to incoroorate technical specifications for Cycle 4.

If so, has reload design and core configuraticn been reviewed by Safety Review Committee regarding unreviewed safety questions? .

. If no, when is review scheduled? .

5. Scheduled date(s) for submi d g proposed licensing action and supporring information: September 18, 1978 .
6. I=portant licensing considerations (new or different design or supplier, unreviewed design or performance analysis methods , sig=ificant changes in design or new operating procedures). None
7. Number of fuel assemblies (a) in the core: 177 .

(b) in the spent fuel pool: see Unit 1.

8. Present licensed fuel pool capacity: see Oconee Unit 1 .

Size of requested or planned increase: see Oconee Unit 1 .

9. Projected date of last refuem g which can be accommodated by present licensed capacity: 3/3/80 assuming no transfers to McGuire. ,

DUIE POWER COMPANT Date: September 15, 1978 ,

Name of

Contact:

J. A. Reavis c , . - - - , - - < - - - -n,-n. --, --, , , , - e-n., -~-----r,m r,--n-- -, ,< e- -