ML19317E371

From kanterella
Jump to navigation Jump to search
Monthly Operating Rept for Jan 1977
ML19317E371
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 02/10/1977
From: Bare L
DUKE POWER CO.
To:
Shared Package
ML19317E369 List:
References
NUDOCS 7912170571
Download: ML19317E371 (3)


Text

_

UNIT Oconto Unit 1 DATE 2/10/77 A ~~

DOCKET NO. 50-269

,d PREPARED BY L.

J. Bare OPERATING STATUS 1.

REPORTING PERIOD: January 1 THROUGH Januarv 31. 1977 GROSS HOURS IN REPORTING PERIOD:

744.0 2.

CURRENTLY AUTHORIZED POWER LEVEL (MWt): 2568 NET CAPABILITY (MWe-Net);

860 3.

POWER LEVEL TO WHICH RESTRICTED (IF ANY):(MWe-Net) 4.

REASONS FOR RESTRICTION (IF ANY) 5.

NUMBER OF HOURS THE REACTOR WAS CRITICAL 505.8 505.8 22621.6 6.

REACTOR RESERVE SHUTDOWN HOURS 7.

HOURS GENERATOR ON-LINE 501.1 501.1 20465.0 8.

UNIT RESERVE SHUTDOWN HOURS 9.

GROSS THERMAL ENERGY GENERATED (MWH) 1280951

.1280951 47666662 10.

GROSS ELECTRICAL ENERGY GENERATED (MWH) 436680 436680 16560110 11.

NET ELECTRICAL ENERGY GENERATED (MWH) 415314 415314 15647847 12.

REACTOR SERVICE FACTOR 68.0 68.0 72.7 13.

REACTOR AVAILABILITY FACTOR 67.4 67.4 68.2 14.

UNIT SERVICE FACTOR 67.4 67.4 65.8 15.

UNIT AVAILABILITY FACTOR 67.4 67.4 65.9 16.

UNIT CAPACITY FACTOR (Using Net 64.9 64.9 58.5 Capability) 17.

UNIT CAPACITY FACTOR (Using Design Mwe) 62.9 62.9 56.7

  • 18.

UNIT FORCED OUTAGE RATE 32.7 32.7 18.2 19.

SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE & DURATION OF EACH:)

Refueling - June 5, 1977 - 6 weeks 20.

IF SHUTDOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP:

REACTOR SERVICE FACTOR = HOURS REACTOR WAS CRITICAT, X 100 HOURS IN REPORTING PERIOD REACTOR AVAIL \\ BILI'lY FACTOR = Hot!PS REACTOR WAS_ AVAIL \\Tst.E TO GPERATE X 100 Il0URS IN REPORTING PERIOD UNIT SERVICE TACTon

= HOUDS GENERATOR ON 1,1NE HOURS IN REPORTING PERIOD

  • UNIT AVAIL \\BILITY FACTOR = UOURS UNTT WAS AVAT1 ABLE TO CE':ERATE X 100 HOURS IN REPok!1NG t'!310D UNIT CAPACITY FACTOR

= NET ELECTHICAL P0hER GENERATFD (Net Capability or Design (Mwe-Net)1 X UOURS IN RO%r.d:

FORCED OUTAGE HOUR 3 7 g } g PERIOD

g UNIT FORCED OLTTACE RATE e HOURS GENERATOR ON LINE + FORCED OU fa%/00

DdCKET NO. 50-269 UNIT SHttTDOWNS UNIT N AM1i Oconee Unit 1 2/10/77 DATii REPORT MONTil January, 1977 TYPE METHOD OF F-FORCED DURATION SHUTTING DOWN NO.

DATE S SCHEDULED (HOURS)

REASON (1)

THE REACTOR (2)

CORRECTIVE ACTIONS / COMMENTS 1

J 1

76-01-l i

F 222.20 A

1 Repair steam generator tube leak 2

76-01-2 i F

20.75 A

N/A Replace control rod drive PI' tube which failed during startup.

(1) RE/. SON (2) METHOD A EQUIPMENT I ALLURE (EXPLAIN) l-MANUAL 8-MAINT. OR TESL 2-MANUAL C-RLl'UELING SCRAM D-REGULATORY RESTRICTION 3-AUTOMATIC E-OPERATOR TRAINING AND SCRAM LICENSE EXAMINATION 4-Other F-ADMINISTR ATIVE G-OPER ATION AL ERROR (EXPLAIN)

Il-0TiiLR (EXPLAIN)

SUMMARY

One major outage this month.

DOCKET NO. 50-269 UNIT Oconee Unit 1 DATE 2/10/77 AVERAGE DAILY UNIT POWER LEVEL MONTH January, 1977 AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL DAY (MWe-net)

DAY (MWe-net) 1 856 37 852 2

18 854 859 4

g 861 5

21 6

859 22 7

861 23 867 8

24 867 9

25 864 481 10 26 866 751 11 27 865 845 12 28 867 66 13 29 863 825 14 30 720 859 15 31 16 DAILY UNir POWER LEVEL FORM INSTRUCTIONS i

On this form, list the average daily unit power level in MWe. net for each da> m the reporting month.

Compute to the nearest whole megawatt.

These figures will be used to plot a graph for each reporting month. Note that by usmg maximum l

dependable capacity for the net ele:trical ratm; of the unit. there may be,t easions when the daily average power level exceeds the 100"i line (or the restrieted power lesel kne). In such c.nes. tne average daily unit power output sheet should be footnoted to explain the apparent anomaly.

_ _ _