05000336/LER-1980-007-03, /03L-0:on 800227,during Reactor Plant Startup, Condensate Storage Tank Level Fell Below Tech Spec Limit for Less than 30 Minutes.Caused by Excessive Water Demand from Blowdown & Regeneration Requirements

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/03L-0:on 800227,during Reactor Plant Startup, Condensate Storage Tank Level Fell Below Tech Spec Limit for Less than 30 Minutes.Caused by Excessive Water Demand from Blowdown & Regeneration Requirements
ML19309A853
Person / Time
Site: Millstone 
Issue date: 03/27/1980
From: Stratman R
NORTHEAST UTILITIES
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19309A846 List:
References
LER-80-007-03L, LER-80-7-3L, NUDOCS 8004010417
Download: ML19309A853 (1)


LER-1980-007, /03L-0:on 800227,during Reactor Plant Startup, Condensate Storage Tank Level Fell Below Tech Spec Limit for Less than 30 Minutes.Caused by Excessive Water Demand from Blowdown & Regeneration Requirements
Event date:
Report date:
3361980007R03 - NRC Website

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[iTff, [ Duri nq rqactor plantgtartup,j Condansa tt5toraqa Ter[ Level was belyy: the level j g [ required by Spacification 3.7.1.3 for a perind of less than 30 minutes.

The low level J [o_Lil Leondition was the result of regeneration of the Condensate Polishing Dcninuralizers I

gg [ coincident with increased Stean Generator blo-zdu.in dua to high chlorides and conduc-j [oTiT] [ tivity causing hich water usage.

There are no probable consegunnces b2cause the unit I [T]T] l was operated in accordance with Technical Specification 3.7.1.3.

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li 121 I Upon noting the low level in the Condensate Storage Tank the operability of the backup I t i l a i i fire water system was verified and tank level restored.

The low level alarm will be l

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