05000327/LER-1980-003-01, /01T-0:on 800310,following Initial Fuel Loading, Flow Through Auxiliary Bldg Exhaust Sampler Not Maintained for 3.25-h.Caused by Misunderstanding of Tech Specs. Personnel Reinstructed in Applicable Requirements

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/01T-0:on 800310,following Initial Fuel Loading, Flow Through Auxiliary Bldg Exhaust Sampler Not Maintained for 3.25-h.Caused by Misunderstanding of Tech Specs. Personnel Reinstructed in Applicable Requirements
ML19309A842
Person / Time
Site: Sequoyah 
Issue date: 03/24/1980
From: Record D
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19309A840 List:
References
LER-80-003-01T, LER-80-3-1T, NUDOCS 8004010403
Download: ML19309A842 (2)


LER-1980-003, /01T-0:on 800310,following Initial Fuel Loading, Flow Through Auxiliary Bldg Exhaust Sampler Not Maintained for 3.25-h.Caused by Misunderstanding of Tech Specs. Personnel Reinstructed in Applicable Requirements
Event date:
Report date:
3271980003R01 - NRC Website

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Tennessee Valley Authority Sequoyah Nuclear Plant LER SUPPLEMENTAL INFORMATION SQRO-50-327/80 03 Technical Specification Involved 3.3.3.10 Reported Under Technical Specification 6.9.1.12.b Date of Occurrence: 3/10/80 Time of Occurrence: 0730 CST Unit 1 Identification and Description of Occurrence:

For three hours and fifteen minutes sampler flow through the Iodine and Particulate filters in the Auxiliary Building Ventilation System Gaseous Effluent Monitor was not maintained. This is in violation of LCO 3.3.3.10 Action 36.

Grab samples were obtained as required by Action 34.

Conditions Prior to Occurrence:

Unit 1 in Mode 6 with initial fuel loading complete.

Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment. Describe.

N/A Apparent Cause of Occurrence:

Misunderstanding of Technical Specifications requirements.

Analysis of Occurrence:

There was no hazard to the health and safety of the public.

Corrective Action

All necessary personnel reinstructed as to applicable Technical Specification requirements.

Failure Data:

N/A l