ML19308D087
| ML19308D087 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 02/09/1977 |
| From: | Stewart W FLORIDA POWER CORP. |
| To: | |
| Shared Package | |
| ML19308D077 | List: |
| References | |
| NUDOCS 8002270585 | |
| Download: ML19308D087 (1) | |
Text
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UCENSEE EVENT REPORT S
CoNTRot stCCx:l Di / l 71 / I/, r71 cmass mer au. mumm mamariam 1 -
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'7,'"E uCE,..E o u.ER 8 Ivi ti eI nl Pi si I O ! O I - 1 0 1 01 01 01 01 - l 0 1 0 I I411Iil1111 10111 7 89 14 15 25 26 30 31 32 rYpE 95[
00CxET NuuSER EVENT CATE REPORT DATE CATEGORY s
O 1 CCN'T l.04 8@ W y l0 l 5 p l-l 0l 3l 0l 2l l0 l1l 2l 6l 7l 7l l0 l2 l0 l 9 ] 7J 7l 7 8 57 58 59 60 61 88 89 74 75 80 EVENtOESCREC 012 l L While in Mode 3 01 e Standby) during start-up, Boron concentration was found l
7 89 80
$l to be approximately 50 ppa diluted causing a 0.57" reactivity insertion.
l 7 89 80 at4 l Recovering frem trio of 4160V unit bus the "A" Fakaun and Purifiention deminerali=el-7 89 80
$I k na 4,2av r
.,c1, s..,
,12,.a in.
ry'e..
ehucamm enr.<n,. mined 4.%" A1the.
l 7 89 80 6 1 Dominera112er was immediately b y passed.
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l 7 89 80 coy CoupoPdNT CoCE MAF4#ACR R VOLADON
[opj lC l Gl W l Dl El Ml Il N l Xl
[N l l3 l0 l1 l5 l lNl 7 89 10 11 12 17 43 44 4/
us CAUSE DESCRIPTION gl Operator erred in placing Morated nixed bed Demin. on line. Tagging now l
7 89 80
]58 9 l
employed to alert operators vi ' ch unit is to be out of service.
l BC
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7 8S 8
,. cur, utn.co o,
$1Arus 4 POWER of>ER STATUS CISCCVERY CISCCVERY DESCmp1CN W
l0l0l 0l l Mode 3 l
l3 l l Routine Chemistry Surveillance l
7 8 9
10 12 13 44 45 48 80 Rh E st o o AucuNT OF ACTMTV LOCATCN OF REEASE 12 (M
jl N/A l
l l
7 8 9
10 11 44 45 80 PERSCNfdl. EXPOSURES NupeEn type oEsCasmon It' I cl<'l E) l N/A l
13 7 89 11 1?
13 80 PERSONNEL INJURIES NuweER CEscapfe" N/A
@ l^l21Cl l
l j
7 89 11 12 80 l
LTSITE CONSEQUENCES 15 l N/A l
7 89 80 LOSS CR DAMAGE TO FAC3.!TY tveE
- EsCDerTCN ggl N/A l
7 89 10 80 8 o 02 27 o #f gi N/A 89 80 AOCITIONAL FACTCAS j
l Plant was in Mode 3 OTot Standhv), Rhutdown margin remained greater than 4" AK/K, l 7 89 80 l
Safety Rod Groups were withdrawn and cocked.
l 1
7 89 y
80 ti. P. Stewart e UT /
(813) 866-4159 m
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