ML19308D087

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RO-77-08:on 770126 During Mode 3,boron Concentration Found Diluted,Causing Reactivity Insertion During Startup.Caused by Personnel Error in Placing Unborated Mixed Bed Demineralizer on Line.Unit Tagged When Out of Svc
ML19308D087
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 02/09/1977
From: Stewart W
FLORIDA POWER CORP.
To:
Shared Package
ML19308D077 List:
References
NUDOCS 8002270585
Download: ML19308D087 (1)


Text

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UCENSEE EVENT REPORT S

CoNTRot stCCx:l Di / l 71 / I/, r71 cmass mer au. mumm mamariam 1 -

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'7,'"E uCE,..E o u.ER 8 Ivi ti eI nl Pi si I O ! O I - 1 0 1 01 01 01 01 - l 0 1 0 I I411Iil1111 10111 7 89 14 15 25 26 30 31 32 rYpE 95[

00CxET NuuSER EVENT CATE REPORT DATE CATEGORY s

O 1 CCN'T l.04 8@ W y l0 l 5 p l-l 0l 3l 0l 2l l0 l1l 2l 6l 7l 7l l0 l2 l0 l 9 ] 7J 7l 7 8 57 58 59 60 61 88 89 74 75 80 EVENtOESCREC 012 l L While in Mode 3 01 e Standby) during start-up, Boron concentration was found l

7 89 80

$l to be approximately 50 ppa diluted causing a 0.57" reactivity insertion.

l 7 89 80 at4 l Recovering frem trio of 4160V unit bus the "A" Fakaun and Purifiention deminerali=el-7 89 80

$I k na 4,2av r

.,c1, s..,

,12,.a in.

ry'e..

ehucamm enr.<n,. mined 4.%" A1the.

l 7 89 80 6 1 Dominera112er was immediately b y passed.

-(-2738)-

l 7 89 80 coy CoupoPdNT CoCE MAF4#ACR R VOLADON

[opj lC l Gl W l Dl El Ml Il N l Xl

[N l l3 l0 l1 l5 l lNl 7 89 10 11 12 17 43 44 4/

us CAUSE DESCRIPTION gl Operator erred in placing Morated nixed bed Demin. on line. Tagging now l

7 89 80

]58 9 l

employed to alert operators vi ' ch unit is to be out of service.

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7 8S 8

,. cur, utn.co o,

$1Arus 4 POWER of>ER STATUS CISCCVERY CISCCVERY DESCmp1CN W

l0l0l 0l l Mode 3 l

l3 l l Routine Chemistry Surveillance l

7 8 9

10 12 13 44 45 48 80 Rh E st o o AucuNT OF ACTMTV LOCATCN OF REEASE 12 (M

jl N/A l

l l

7 8 9

10 11 44 45 80 PERSCNfdl. EXPOSURES NupeEn type oEsCasmon It' I cl<'l E) l N/A l

13 7 89 11 1?

13 80 PERSONNEL INJURIES NuweER CEscapfe" N/A

@ l^l21Cl l

l j

7 89 11 12 80 l

LTSITE CONSEQUENCES 15 l N/A l

7 89 80 LOSS CR DAMAGE TO FAC3.!TY tveE

EsCDerTCN ggl N/A l

7 89 10 80 8 o 02 27 o #f gi N/A 89 80 AOCITIONAL FACTCAS j

l Plant was in Mode 3 OTot Standhv), Rhutdown margin remained greater than 4" AK/K, l 7 89 80 l

Safety Rod Groups were withdrawn and cocked.

l 1

7 89 y

80 ti. P. Stewart e UT /

(813) 866-4159 m

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