ML19308B520

From kanterella
Jump to navigation Jump to search
LER 78-007/03L-0:on 780208,suction Valve 3LPSW-123 Observed Closed During 3B Pump Startup.Valve Closure Cause Unknown. Probably Caused by Erroneous Closing During Repairs on on Pervious Day.Valve Opened & Pump Checked for Damages
ML19308B520
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 03/13/1978
From: Ken Wilson
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19308B517 List:
References
LER-78-007-03L-01, LER-78-7-3L-1, NUDOCS 8001090526
Download: ML19308B520 (2)


Text

- - - -

MAC Po24 384 f1 A1 u. 5. NUCLEAR RECULATORY CCMMi551oM LICENSEE EVENT REPORT EXHIBIT A CONTROL 5 Lock: l l l l l l l@ (PLEASE PRINT OR TYPE ALL REQUIRED INFORM 4TIONI l

- l a 8t .i l I si 7

c i CCOt uCENSEE n I v i el' 3 l@16o fuCENSE

i. ol -lNow.ER o I o f olo I o I 4- 10 *,

11 11 l o I5@a il 11@l53 GaI r sel@

ucgust ry,g .o con'T

~

I, o l ' 1=

Uu'*,% =

L2.j@lo I s b I olo i 2 I a I 7. GI..o i 2 f o i s I 7 I 8 Gl o I- 31t 13 I 7 I 8 l@

.. coC..r vo... iv r o.r. i. 1 ..,c.,o.r. ..

avENT oescaimom Ano esce AeLs ccNsECUENCES h 1o121 1 Durine startup of 3B LPSW pump operator noticed that the suction valve, [

lo is t l 3LPSW-123 was closed. He ceased startup immediately. The pump was restarted, EI after the valve was onened and found to be undamaged. The valve closure l lo t s t I removed one train of the LPSW system from service but the other train was y is is 1 I available to handle any accident situations. No adverse effect on public ,

LoJ.rJ l henith and safety was caused by this incident. g 10 t d l l

, . . I

=

GCE CO E Sb C G COM8CNENT COO 4 fue C'E Su E laisi

, . IW ID l@ W@ l X l@ [ Zl Zl Z l ZlZ l Z l@ lZ l@ [Z_J

. i. i, is is i. i. :o SV emf TfAp 3EQuthTi.L QCCUMagNCE .tPCMT AEVISICM.

  • EPCRT NC. CCCE Tvet go.

@ ,"LIRt.O

,5g l0 f01 7l lu7 l 81 u

[--J n u l/l lo l 3 l l Ll [] y u

a a a a u n EN *c2EJ cEa?ET '"w*Eo' sT cues 22 'E'E#5* ,Ea".ide. '"sL",'.?s7 uf=*u",'.*EE=*en I.,X_j@l,.2.j@ 1 Z I@ l ZI@ J O! 0!0 ! l .Lj@

( l71ojoIol@

,, , u - l.,NI@ lZ l@ . ,,

causs cesenimcN Anoccansenve acncNs @

titatl The ictual cause of the valve closure is unknown. Evidently someone erron- ;

t i 1.U l ecusiv closed the valve during reoairs in the area on the day before. Since,

,,,2, I the exact cause is unknown, the applicable corrective action was the opening, l.i1.LJ l of the valve and checking the pump for any damage. ,

l i t .1 I 7 e s I ao STATV %PCwtM QTi.tM57Afu5 Di RY CISCOvt4Y Ot3CRirTICM ir i S I [I.j@ l 1 I o IO l@l NA l' [Aj@l operator observation s a, g,y is is = as .e so l-8 .u.. ,me

-1 .

<oCA,,..C,..m..@

...u-.lz.J @ L2J@l NA .. @ l l NA l

'a

.,e.i ...

-.. m., .. .C.i., , @

ITTTl

' 1010 ! 01@lz_J@l NA , , _ _

l

' m o .L'i. Ji3 wuw e. ossenierica@

l'TTil0 l8 0 l o ! ol@ti2 NA 7 it l

" go

'ryfe**"xs'Cn',"tIo'""@

d, W@l . . i.

~ NA _

l

    • e,i," ,,,,,,,, @ uae usa enLv 2 o ,,,,

LN @l NA

s. is I llllfIlIilIll es e, so Newso*Paaranen K. R. Wilson ,ycus, (700 373-8W c .

goo 1090 M 6

! .-,-. - - - - - - - - - - - - - - -- -- - + ~ ~'

7 .

m s tj . ' '

DUKE POWER COMPANY OCONEl'. UNIT 3 Report Number: R0-287/78-7 .

Report Date: March 13, 1978 Occurrence Date: February 8,1978 Facility:- Oconee Unit 3, Seneca, South Carolina Identification of Occurrence: 3LPSW' 123 Found Closed Conditions Prior to Occurrence: 100% Full Power Description of Occurrence:

On February 8,197'8, at 0940, the 3B Low Pressure Service Water (LPSW) pump was started. When the operator noticed that the pump suction valve, 3LPSW-123, was closed, the pump was stopped. Investigation by operating personnel determined that the valve had been closed since approximately 1600 on-February 7, 1978. Therefore, the pump had been ef fectively out-of-service for about 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br />. The pump suction str.ainer had been serviced the pre-vious day at about the time of the valve closure, but the valve had not been required to be. closed by the procedure. The valve was opened and the pump was verified as being undamaged by the incident.

Apparent Cause of Occurrence: '

The exact cause of the valve closure is unknown. There are two. controls, for the valve, one in the control room and one in the area of the pump.

Discussions were held with_ perso'nnel in both areas, but none had any rec-

, ollection as to how the val've was closed or with regard as t,o who closed it.

Analysis of Occurrence:

The closure of 3LPSW' 123 rendered one train of the LPSW system inoperable.

However,'the control room could have opened the valve at any time if the train was needed. Technical Specification 3.3.5 allows one train to be inoperable for a period of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for test or maintenance, since one train is sufficient to provide necessary cooling in an accident situation.

One train was operable although the second train was inoperable for ar cause other than test or maintenance. Pu,blic health and safety were.not endangered by this incident.

Corrective Action:

The valve was opened after evaluation of the occurrence. The pump was vented, restarted, and tested to assure that it had not sustaLned damage.

~

s

.