05000324/LER-1980-028-03, /03L-0:on 800212,while Performing PT 2.1.8PC, Reactor Core Isolation Cooling Exhaust Diaphragm Calibr & Functional Test,High Pressure Switches E51-PS-NO12A & C Actuated at 11.9 Psig.Caused by Instrument Drift

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/03L-0:on 800212,while Performing PT 2.1.8PC, Reactor Core Isolation Cooling Exhaust Diaphragm Calibr & Functional Test,High Pressure Switches E51-PS-NO12A & C Actuated at 11.9 Psig.Caused by Instrument Drift
ML19305A828
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 03/12/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19305A825 List:
References
LER-80-028-03L, LER-80-28-3L, NUDOCS 8003180418
Download: ML19305A828 (1)


LER-1980-028, /03L-0:on 800212,while Performing PT 2.1.8PC, Reactor Core Isolation Cooling Exhaust Diaphragm Calibr & Functional Test,High Pressure Switches E51-PS-NO12A & C Actuated at 11.9 Psig.Caused by Instrument Drift
Event date:
Report date:
3241980028R03 - NRC Website

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lo l2l l While performing PT 2.1.8PC, RCIC Exhaust Diaphragm Calibration and Functional j

l o 13 l l Test, RCIC exhaust diaphragm high pressure switches E51--PS-N012A&C actuated at l

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