05000324/LER-1980-010, Supplemental LER 80-010/03L-1:on 800114,during Normal Plant operation,OD-1 Determined That Max Critical Power Ratio Was Below Tech Specs for Bundle 43-28.Caused by Problems W/Low Power Range Monitor & Core Flow Input.Power Redu

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Supplemental LER 80-010/03L-1:on 800114,during Normal Plant operation,OD-1 Determined That Max Critical Power Ratio Was Below Tech Specs for Bundle 43-28.Caused by Problems W/Low Power Range Monitor & Core Flow Input.Power Reduced
ML19296D449
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 02/27/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19296D444 List:
References
LER-80-010-03L, LER-80-10-3L, NUDOCS 8003040603
Download: ML19296D449 (2)


LER-1980-010, Supplemental LER 80-010/03L-1:on 800114,during Normal Plant operation,OD-1 Determined That Max Critical Power Ratio Was Below Tech Specs for Bundle 43-28.Caused by Problems W/Low Power Range Monitor & Core Flow Input.Power Reduced
Event date:
Report date:
3241980010R00 - NRC Website

text

NRC FORM 366

"DPMTE" REPORT:'~ PREVIOUS LICENSEE EVENT REPORT REPORT DATE 2-11-80 h CONTROL BLOCK: l l

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8 60 61 COCK ET NUM6t R 6d 69 EVENT OATE 74 75 REPORT DATE 80 SOURCE EVENT DESCRIPTION AND PROSABLE CONSEQUENCES h ITTTI I outine normal plant operation, the nuclear engineer performed an OD-1 which determined]

Io1al l that MCPR was 1.281 for bundle 43-28, an 8x8R bundle.

The reportable limit for this l l parameter is <l.29.

Power was being slowly increased following a rod shuffle the 1

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CODE TYPE No.

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] The CPR problem was due to: a) the controlling LPRM had two levels bypassed; I

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[;Til I in specifications. The LPRM will be replaced and the inoperable jet pump input will g l be corrected during the next refueling outage. A " drive flow" vs. " core flow" corre-l lation has been inserted into the comouter to provide more representative indication l gl 80 7

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1010101@Lv/s i a 80 7

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A. C. Tollison, Jr.

PHONE:

NAME OF PREPARER e.

LER CONTINUATION - RO #2-80-10 Facility: BSEP Unit No. 2 Event Date: January 14, 1980 of core flow. Had the proper core flow been seen by the computer, it is believed that this event would not have exceeded any limits.

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