05000336/LER-1980-002-03, /03L-0:on 800131,during Steady State Operation, Leakage Was Observed from Packing on High Pressure Safety Injection Valve.Caused by Worn Packing.Valve Repacked & Restored to Svc

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/03L-0:on 800131,during Steady State Operation, Leakage Was Observed from Packing on High Pressure Safety Injection Valve.Caused by Worn Packing.Valve Repacked & Restored to Svc
ML19296C595
Person / Time
Site: Millstone Dominion icon.png
Issue date: 02/20/1980
From: Rothgeb R
NORTHEAST UTILITIES
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19296C588 List:
References
LER-80-002-03L, LER-80-2-3L, NUDOCS 8002260688
Download: ML19296C595 (1)


LER-1980-002, /03L-0:on 800131,during Steady State Operation, Leakage Was Observed from Packing on High Pressure Safety Injection Valve.Caused by Worn Packing.Valve Repacked & Restored to Svc
Event date:
Report date:
3361980002R03 - NRC Website

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