05000324/LER-1980-019-03, /03L-0:on 800122,while Performing RHR Svc Water Pump Flow test,2B & 2D RHR Svc Water Pumps Did Not Meet Required 4,000 Gpm at 300 Psig Discharge Pressure.Caused by Incorrect Data.Tech Specs Changed

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/03L-0:on 800122,while Performing RHR Svc Water Pump Flow test,2B & 2D RHR Svc Water Pumps Did Not Meet Required 4,000 Gpm at 300 Psig Discharge Pressure.Caused by Incorrect Data.Tech Specs Changed
ML19296B881
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 02/14/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19296B880 List:
References
LER-80-019-03L, LER-80-19-3L, NUDOCS 8002220322
Download: ML19296B881 (2)


LER-1980-019, /03L-0:on 800122,while Performing RHR Svc Water Pump Flow test,2B & 2D RHR Svc Water Pumps Did Not Meet Required 4,000 Gpm at 300 Psig Discharge Pressure.Caused by Incorrect Data.Tech Specs Changed
Event date:
Report date:
3241980019R03 - NRC Website

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60 68 DOCKET NUMBER 68 69 EVENT OATE 74 15 REPORY DATE 80 E JENT DESCRIPTION AND PROSA8LE CONSEQUENCES h M l While performine PT 8.1.4. RHR Service Water Pump Flow Test, it was determined that I

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o l While investicating the RHR SW pumps for ISI testing ourposes, it was discovered thatl W l the data used to establish the 4000 gpm at 300 psig discharge pressure was incorrect.I i 2 l The requirement should have been 4000 gpm at >232 psid pump AP.

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for the Techhical Specification change would be delayed due to a large backlog, and that.we should submit an LER to cover the event. This LER will be used as a " cover LER" for both units for the 4000 gpm 300 psid

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criteria. Should any pump fail the 4000 gpm at >232 psid criteria, that will be treated as..a separate reportable event and reported as such.

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